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34-111-24098

Well Details

Well ID: 34-111-24098
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Country: United States
State: Ohio
County: Monroe
Municipality: Green Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: THOMPSON DON
License Status: Producing
License Date: 2007-04-23
Spud Date: 2007-04-30
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC
Final Drill Date: 2007-05-02
Well Total Depth: 2815.00 ft
Configuration: Vertical
Latitude: 39.710000
Longitude: -81.020000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-04-23 Proposed Formations:BEREA/30 FOOT/GORDON, Issued Date:4/23/2007, Expired Date:4/22/2008 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EOUT
Completed 2007-05-02
Reached Total Depth 2007-05-02
Completion Report Received 2007-10-30
Construction Permit Expires 2008-04-22
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2008-02-14 2460 2490 65
2008-02-14 2176 2186 25
2176 2186 25
2650 2720 10
2554 2610 40
2460 2490 65
2176 2186 25
2008-02-14 2650 2720 10
2008-02-14 2554 2610 40

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 202070 Gal 0 1ST STAGE OF 3-STAGE FRAC, & INCLUDED FIFTH SAND… SINGLE FRAC WATER VOLUME REPORTED FOR ENTIRE 3-STAGE FRAC… NO SAND USED IN FRAC… NO PRESSURES REPORTED… GM
H2O 0 0 0 2ND STAGE OF 3-STAGE FRAC… SINGLE FRAC WATER VOLUME REPORTED FOR ENTIRE 3-STAGE FRAC… NO SAND USED IN FRAC… NO PRESSURES REPORTED… GM
H2O 0 0 0 3RD STAGE OF 3-STAGE FRAC… SINGLE FRAC WATER VOLUME REPORTED FOR ENTIRE 3-STAGE FRAC… NO SAND USED IN FRAC… NO PRESSURES REPORTED… GM

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 BECK ENERGY CORPORATION 407.00 0.00 0
2008 BECK ENERGY CORPORATION 557.00 21.00 365
2009 BECK ENERGY CORPORATION 658.00 12.00 365
2010 BECK ENERGY CORPORATION 965.00 1.00 365
2011 BECK ENERGY CORPORATION 1337.00 1.00 365
2012 BECK ENERGY CORPORATION 1043.00 0.00 366
2013 BECK ENERGY CORPORATION 1210.00 3.00 365
2014 BECK ENERGY CORPORATION 639.00 0.00 365
2015 BECK ENERGY CORPORATION 1089.00 0.00 365
2016 BECK ENERGY CORPORATION 1081.00 2.00 365
2017 BECK ENERGY CORPORATION 983.00 0.00 365
2018 BECK ENERGY CORPORATION 810.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 BECK ENERGY CORPORATION Brine 0
2008 BECK ENERGY CORPORATION Brine 59 365
2009 BECK ENERGY CORPORATION Brine 64 365
2010 BECK ENERGY CORPORATION Brine 80 365
2011 BECK ENERGY CORPORATION Brine 83 365
2012 BECK ENERGY CORPORATION Brine 0 366
2013 BECK ENERGY CORPORATION Brine 77 365
2014 BECK ENERGY CORPORATION Brine 73 365
2015 BECK ENERGY CORPORATION Brine 0 365
2016 BECK ENERGY CORPORATION Brine 85 365
2017 BECK ENERGY CORPORATION Brine 0 365
2018 BECK ENERGY CORPORATION Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1423247927 2018-3-29 0:00: PW No Violations 0.50
-2099988211 2007-12-6 0:00: PL No Violations
1423247927 2018-03-29 Production Wells No Violations On this day, I found the well equipped with 4.5 inch diameter casing with the valve open and 1.9 inch diameter tubing with the valve open. It is produced by means of a pumping unit with a gas engine, tubing, and rods. There is (1) 100 barrel steel tank, a drip tank, vertical separator, and an orifice meter all contained within an earthen dike. The tank is properly identified and the production records are current. The well appears to provide domestic gas. It will be noted that there is a slight leak at a fitting on the domestic hook-up, so the company will be informed of the issue.
1585842962 2020-4-2 0:00:0 PW No Violations 0.40
2099988211 2007-12-06 Preliminary Restoration No Violations Restoration work at site satisfactory, well is equipped with tubing and production casing and 1-100 bbl tank with dike in place(rabbit well).

For data sources see[9]

References