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34-111-23687

Well Details

Well ID: 34-111-23687
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Country: United States
State: Ohio
County: Monroe
Municipality: Ohio Township
Operator Name: GENESIS RESOURCES LLC
Well Pad ID:
Farm/Lease Name: ISLAY UNIT
License Status: Producing
License Date: 1992-12-18
Spud Date: 1992-12-26
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 1993-03-01
Well Total Depth: 3152.00 ft
Configuration: Vertical
Latitude: 39.670000
Longitude: -80.900000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1992-12-18 Issued Date 12/18/92 Expired Date 12/18/93 Acres 0020000 Tool Type RTA Proposed Formation BEREA/OHIO SHALE Proposed Depth 03152 Proposed Drill Depth 03152
Original Spud 1992-12-26
Completed 1993-03-01
Reached Total Depth 1993-03-01
CO 1993-08-16 1815 TRANS ATLANTIC ENER CORP GeoDate 12/18/92
Completion Report Received 1993-08-30
Construction Permit Expires 1993-12-18
CO 1994-08-11 4884 EASTERN STATES OIL & GAS GeoDate 12/18/92
Change of Owner 2005-06-07 Operator changed from 4884, EASTERN STATES OIL & GAS INC to 7849, NCL NATURAL RESOURCES LLC
Change of Owner 2006-02-15 Operator changed from 7849, NCL NATURAL RESOURCES LLC to 1634, NORTHWOOD ENERGY CORP
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2998 3035 0
2998 3035 0
2006-09-11 3008 3036 38
3008 3036 38
2998 3035 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 71480 Gal 60000 FRAC W/71,740 GAL H20 & 6M# SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 TRANS ATLANTIC ENER CORP 2741.00 0.00 365
1994 EASTERN STATES OIL & GAS INC 1712.00 0.00 365
1996 EASTERN STATES OIL & GAS INC 1045.00 0.00 365
1997 EASTERN STATES OIL & GAS INC 909.00 0.00 365
1998 EASTERN STATES OIL & GAS INC 995.00 0.00 365
1999 EASTERN STATES OIL & GAS INC 652.00 0.00 365
2000 EASTERN STATES OIL & GAS INC 524.00 0.00 365
2001 EASTERN STATES OIL & GAS INC 477.00 0.00 365
2002 EASTERN STATES OIL & GAS INC 626.00 0.00 365
2003 EASTERN STATES OIL & GAS INC 564.00 0.00 365
2004 EASTERN STATES OIL & GAS INC 564.00 0.00 366
2005 NCL NATURAL RESOURCES LLC 213.00 0.00 214
2006 NORTHWOOD ENERGY CORP 364.00 0.00 365
2007 NORTHWOOD ENERGY CORP 344.00 0.00 365
2008 NORTHWOOD ENERGY CORP 282.00 0.00 365
2009 NORTHWOOD ENERGY CORP 263.00 0.00 365
2010 NORTHWOOD ENERGY CORP 257.00 0.00 365
2011 NORTHWOOD ENERGY CORP 127.00 0.00 0
2012 NORTHWOOD ENERGY CORP 384.00 0.00 366
2013 NORTHWOOD ENERGY CORP 373.00 0.00 365
2014 NORTHWOOD ENERGY CORP 423.00 0.00 365
2015 NORTHWOOD ENERGY CORP 237.00 0.00 365
2016 NORTHWOOD ENERGY CORP 484.00 0.00 365
2017 NORTHWOOD ENERGY CORP 432.00 0.00 365
2018 NORTHWOOD ENERGY CORP 353.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 TRANS ATLANTIC ENER CORP Brine 0 365
1994 EASTERN STATES OIL & GAS INC Brine 0 365
1996 EASTERN STATES OIL & GAS INC Brine 0 365
1997 EASTERN STATES OIL & GAS INC Brine 365
1998 EASTERN STATES OIL & GAS INC Brine 365
1999 EASTERN STATES OIL & GAS INC Brine 365
2000 EASTERN STATES OIL & GAS INC Brine 365
2001 EASTERN STATES OIL & GAS INC Brine 0 365
2002 EASTERN STATES OIL & GAS INC Brine 0 365
2003 EASTERN STATES OIL & GAS INC Brine 365
2004 EASTERN STATES OIL & GAS INC Brine 366
2005 EQUITABLE PRODUCTION COMPANY Brine 0 151
2006 NORTHWOOD ENERGY CORP Brine 0 365
2007 NORTHWOOD ENERGY CORP Brine 0 365
2008 NORTHWOOD ENERGY CORP Brine 0 365
2009 NORTHWOOD ENERGY CORP Brine 0 365
2010 NORTHWOOD ENERGY CORP Brine 0 365
2011 NORTHWOOD ENERGY CORP Brine 0
2012 NORTHWOOD ENERGY CORP Brine 0 366
2013 NORTHWOOD ENERGY CORP Brine 0 365
2014 NORTHWOOD ENERGY CORP Brine 0 365
2015 NORTHWOOD ENERGY CORP Brine 0 365
2016 NORTHWOOD ENERGY CORP Brine 0 365
2017 NORTHWOOD ENERGY CORP Brine 0 365
2018 NORTHWOOD ENERGY CORP Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1165909686 2019-5-15 0:00: PW No Violations 0.70
-1697987029 2020-2-18 0:00: PW No Violations 1.00
-1794721834 2009-1-5 0:00:0 PW No Violations
0000009828 Preliminary Restoration No Violations PASSED Y WITNESSED 10/7/93 INSPECTOR CLYDE DOBBIN DATE 10/0719/93 DATA FROM OLD VAX INFO
1165909686 2019-05-15 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection in regard to Complaint #6084. No progress has been made to gain compliance. Oily fluid remains at the base of the 210 barrel steel storage tank. A voicemail was left with Northwood Representative Corey McCudden, requesting a callback in reference to the issue. Thick vegetation surrounds the pumping unit. The casing valve is open to a domestic meter and the tubing valve is open to production. A chart dated 4/1/19 is present within the sales meter. Updated photographs were taken.
1551110907 2019-02-25 Production Wells Violations Noted On this day, I am conducting an inspection in reference to Complaint #6084 per request of landowner Charles Meyer, and am accompanied by his relative, Mr. Roy Ensinger during the inspection. Mr. Meyer stated that the storage tank associated with the well is leaking. I found the tank to have potential integrity issues causing pollution and contamination around the base, with fluid pooling in the immediate vicinity. Multiple pictures were taken. The affected area will need to be removed, and the tank will need to be addressed to prevent any further issues. On 2/25/2019, I spoke with Northwood Representative Corey McCudden to notify him of the issue. I found the well equipped with 4.5 inch diameter casing and 1.9 inch diameter tubing with the production valves open. It is setup to be produced by means of a pumping unit with rods and a gas engine. There is a domestic sales meter present at the wellhead, along with a low pressure regulator. The production facility consists of (1) 210 barrel steel tank, drip tank, vertical separator, and an orifice sales meter with a current chart all contained within an earthen dike. The production records are current through 2017.
1794721834 2009-01-05 Production Wells No Violations WELL IS SUPPLIED WITH PUMPJACK AND 210 BBL TANK.NO PRODUCTION SINCE 2006.NO VIOLATIONS NOTED.WILL CONTACT NORTHWOOD.
1936031842 2019-03-14 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection to Complaint #6084. No progress has been made to address the issue. Oily pooled fluid continues to reside at the base of the 210 barrel steel storage tank. Updated photographs were taken.
9828 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1551110907 US-OH-115063 2019-02-25 Well operation causing pollution and contamination

For data sources see[9]

References