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Well ID: 34-111-20783 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Malaga Township | |
Operator Name: C G O INC | |
Well Pad ID: | |
Farm/Lease Name: ACKERMAN BEN | |
License Status: Final Restoration | |
License Date: 2012-06-28 | |
Spud Date: 1948-05-02 | |
Spud Drilling Contractor: | |
Final Drill Date: 1948-05-22 | |
Well Total Depth: 1321.00 ft | |
Configuration: Vertical | |
Latitude: 39.810000 | |
Longitude: -81.220000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1948-05-02 | |
Completed | 1948-05-22 | |
Reached Total Depth | 1948-05-22 | |
APP | 2012-06-28 | Proposed Formations:KEENER, Issued Date:6/28/2012, Expired Date:6/28/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-09-18 | |
Construction Permit Expires | 2014-06-28 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1999 | C G O INC | 9.00 | 0.00 | 365 |
2000 | C G O INC | 31.00 | 0.00 | 365 |
2001 | C G O INC | 40.00 | 0.00 | 365 |
2002 | C G O INC | 23.00 | 0.00 | 365 |
2003 | C G O INC | 47.00 | 0.00 | 365 |
2004 | C G O INC | 28.00 | 0.00 | 365 |
2005 | C G O INC | 32.00 | 0.00 | 365 |
2006 | C G O INC | 16.00 | 0.00 | 365 |
2007 | C G O INC | 29.00 | 0.00 | 365 |
2008 | C G O INC | 33.00 | 0.00 | 365 |
2009 | C G O INC | 22.00 | 0.00 | 365 |
2010 | C G O INC | 121.00 | 0.00 | 365 |
2011 | C G O INC | 108.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1999 | C G O INC | Brine | 0 | 365 |
2000 | C G O INC | Brine | 0 | 365 |
2001 | C G O INC | Brine | 0 | 365 |
2002 | C G O INC | Brine | 0 | 365 |
2003 | C G O INC | Brine | 0 | 365 |
2004 | C G O INC | Brine | 0 | 365 |
2005 | C G O INC | Brine | 0 | 365 |
2006 | C G O INC | Brine | 0 | 365 |
2007 | C G O INC | Brine | 0 | 365 |
2008 | C G O INC | Brine | 0 | 365 |
2009 | C G O INC | Brine | 0 | 365 |
2010 | C G O INC | Brine | 0 | 365 |
2011 | C G O INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1185309926 | 2012-8-1 0:00:0 | PB | No Violations | 5.00 |
-1485719742 | 2012-7-12 0:00: | WR | No Violations | |
-1521271460 | 2012-7-17 0:00: | PB | No Violations | 5.00 |
-1936031629 | 2012-9-18 0:00: | PB | No Violations | 8.00 |
-1971672800 | 2012-8-14 0:00: | PB | No Violations | 8.00 |
-323598721 | 2012-6-27 0:00: | PB | No Violations | 3.00 |
-615939929 | 2010-3-16 0:00: | PW | No Violations | 0.50 |
-635648005 | 2012-8-13 0:00: | PB | No Violations | 12.00 |
-871579890 | 2012-7-16 0:00: | PB | No Violations | 3.00 |
-907341875 | 2012-3-14 0:00: | PW | No Violations | |
0323598721 | 2012-06-27 | Plug / Plug Back | No Violations | On day of inspection Jet wireline is in running gamma log . Met with Ed Crum and Harmon well service to devise a plan for casing placement for drilling down with cable rig. |
0401313713 | 2012-08-08 | Plug / Plug Back | No Violations | My inspection today finds the operator attempting to clean the hole with a 60L cable tool rig. The rig crew have cleaned down to 118 with 6 bit and tools. They believe they are hitting the top of a piece of casing. |
0437555378 | 2012-10-23 | Final Restoration | No Violations | On the day of my inspection work still needed to be done on this site in order to pass final restoration. Another site has been made for a new well and an application has been submitted by well owner. Final restoration was not due on the day of inspection and I will check back at a later date. No violations noted. |
0615939929 | 2010-03-16 | Production Wells | Violations Noted | On day of inspection well has no id. |
0635648005 | 2012-08-13 | Plug / Plug Back | No Violations | CGO spudding rig is pulling 8.625casing out and attempting to retrieve the 7that is broke off down approximately 62.They will use a spring loaded center spear for the 7attached to the 4.5casing. The spear will prematurely set off. The rig tried to pull 10up about 2 off bottom. They thought 10casing was on 7collar. |
0667050009 | 2012-02-14 | Production Wells | No Violations | FOLLOW UP TO NOV # 1245274149 I received a call from John Ackerman who is concerned about the production of this well. Production has not been submitted for two years. The production that is submitted shows a history of production under the minimum standard. This well is owned by C G O INC. Well shall be plugged or application shall be submitted for temporary inactive status. |
0871579890 | 2012-07-16 | Plug / Plug Back | No Violations | On the day of my inspection inspectors Pat Shreve and Chris Grimm were on location. Harmon well services employees were present. A bailer was run into the hole and they attempted to use the sputter deepen the hole. The eight inch casing stared moving so operations were shut down. We could hear the hole caving in. We will try to run an impression block the next time we meet on location. |
0907341875 | 2012-03-14 | Production Wells | Violations Noted | On the day of my inspection Harmon well services had a rig on location and had been working on the well. They were not working at the time of the inspection. There was a pit on location that did not have a pit liner in it. I tested the water in the pit and it was over 6900 ppm on the chlorides. I called Pat Shreve to aid me in taking samples. Ed Crum (well owner) showed up on location and I spoke with him about the issues on site. GR-Contracting showed up on site with a load of brine water and Pat pulled in at the same time. Pat and I sampled the water in the pit and also took soil samples. I took photos and GPS readings of the samples for documentation purposes. |
1185309926 | 2012-08-01 | Plug / Plug Back | No Violations | On the day of my inspection Harmon well services were working on the well. 63 of 10 pipe had been set and it was landing on 7 pipe in the hole. Efforts will be made to center the 7 so that 10 can be set further down. No violations were noted. |
1245274149 | 2012-02-14 | Production Wells | Violations Noted | I received a call from John Ackerman who is concerned about the production of this well. Production has not been submitted for two years. The production that is submitted shows a history of production under the minimum standard. This well is owned by C G O INC. Well shall be plugged or application shall be submitted for temporary inactive status. |
1271767294 | 2010-03-16 | Production Wells | Violations Noted | John Ackerman called with complaint on well not producing. Well is supplied by a 7casing head and 2tubing. Well is shut in and idle. Well not capable.CGO is the owner. Will call Ed Crum with the verbal NOV. Need to get on Bond and file production. |
1294279419 | 2010-10-29 | Production Wells | No Violations | On day of inspection well is capable and supplied with id and production has been filed.NOV resolved |
1331964279 | 2012-07-17 | Plug / Plug Back | No Violations | On the day of my inspection an impression block was run into the hole. The results did not provide enough information to determine exactly what was down hole. We will try to spear the loose casing and create a solid working string for further attempts to deepen the hole. |
1332784826 | 2012-03-14 | Production Wells | No Violations | On day of inspection I met with Andrew Corder and helped take samples at site. Well was plugged back in 1949.Well was bought by Ed Crum from Nova Christman.At some time well was opened back up and a newer piece of 7was placed in well. There was no reopen permit issued. Ed Crum will apply for plugging permit. pudding rig will be brought in to drive obstruction down to bottom. Andrew will issue a Compliance Notice to CGO. Several truck loads of brine have been placed into well bore as a drilling medium. |
1342101084 | 2012-07-02 | Production Wells | No Violations | On the day of inspection the unlined pit that had previously held brine water had been filed in. GnR contracting advised that water was disposed of by them in a proper manner and documentation was available upon request. Ed Crum has applied for a plugging permit; the plugging of this well and the pit closure satisfies the prior compliance notice. Compliance notice resolved 07/02/2012 |
1342744673 | 2012-07-18 | Plug / Plug Back | No Violations | I received a phone call from Troy Harmon or Harmon well services and he is attempting to locate a spear so that we can try to retrieve more casing from the well. |
1342797903 | 2012-07-16 | Drill / Deepen / Reopen | No Violations | I was on location with ODNR inspector Pat Shreve to witness CGO cable tool rig drilling through an obstruction in the well which is to be plugged. The drillers were at a depth of 116 when they shut down for the day. |
1344525026 | 2012-08-02 | Production Wells | No Violations | On the day of my inspection Harmon well services were using 8 casing with a seringe type cut on the bottom to center the 7 in the hole to all for the 10 to be lowered further. The 8 went around the 7 and reached 83 down hole. |
1345114725 | 2012-08-15 | Plug / Plug Back | No Violations | Rig crew on CGO cable tool rig is running 8.625casing in to 91. The rig crew will try to get in to get impression reading on top of there lost tools down hole. |
1348018341 | 2012-09-18 | Plug / Plug Back | No Violations | On the day of my inspection Harmon Well Services and Formation Cementing were plugging the well. Plug was set from 120 to surface. No violations were noted. |
1352141354 | 2012-11-05 | Final Restoration | No Violations | The said well was plugged to surface on 9-18-2012, As of this day of inspection the casing has not been cut off 30 below grade and a steel plate applied to the top of it identifying the well, all service equipment and excess casing is still on location, it appears that the owner of the equipment has been painting and servicing equipment on site, no final restoration work has yet to be commenced per 1509.072 ORC. Also noted that the landowner has made notice that the operator has commenced building a drill site on the property without a current lease or drilling permit from the Division. |
1352219061 | 2012-11-06 | Administrative Inspection | No Violations | Inspector spoke to well owner ED Crum on this day concerning the completion of the Final Restoration of the well and well site. Mr. Crum stated that He had no intentions of completing the restoration work until next spring. Inspector did request that Mr. Crum immediately commence with restoration work according to ORC 1509.072 and also made Mr. Crum aware that no extensions had been issued on the restoration work. The inspector also spoke with Mr. Crum concerning the work on additional wells in the area that are not registered with the Division in His name. |
1365087292 | 2013-04-04 | Final Restoration | No Violations | John Ackerman called on this day and asked me to follow up on the site restoration because He would like to plow the field. Upon inspection I found the well site itself does meet 1509:072 but the lease road needs restored. I have spoke with Ed Crum several times on the restoration work and will call Ed again and remind Him to complete the restoration. |
1366985750 | 2013-04-26 | Final Restoration | No Violations | Restoration work meets 1509.072. Final Restoration Approved. |
1468024696 | 2012-03-14 | Production Wells | No Violations | FOLLOW UP TO NOV # -907341875 On the day of my inspection Harmon well services had a rig on location and had been working on the well. They were not working at the time of the inspection. There was a pit on location that did not have a pit liner in it. I tested the water in the pit and it was over 6900 ppm on the chlorides. I called Pat Shreve to aid me in taking samples. Ed Crum (well owner) showed up on location and I spoke with him about the issues on site. GR-Contracting showed up on site with a load of brine water and Pat pulled in at the same time. Pat and I sampled the water in the pit and also took soil samples. I took photos and GPS readings of the samples for documentation purposes. |
1485719742 | 2012-07-12 | Work Over Reconditioning | No Violations | Stopped by service rig while doing random inspections and found rig on hole with app 40 of 7 surface casing on ground that had been recovered from well bore with 4.5 production casing on location to go back into well bore, rig hand commented that extensive efforts had been made with both a power swivel and the sputter rig to get back down into the original well bore. Inspector will not that the 7 appears to be parted down hole. |
1491540876 | 2012-04-26 | Production Wells | No Violations | On the day of my inspection there was a spudding rig on site. A surveyor was also present. The lower unlined pit that had contained the brine water has been closed. No violations were noted. |
1521271460 | 2012-07-17 | Plug / Plug Back | No Violations | On the day of my inspection an impression block was ran into the hole to determine down hole conditions. The block was ran twice and did not provide clear evidence of what lay down hole. Attempts to spear pipe in hole will begin on 07/19/2012. No violations were noted. |
1821804512 | 2012-08-08 | Drill / Deepen / Reopen | No Violations | CGO ran 62of 10.75casing in as drive pipe. 82of 8.625casing and is engulfed about 20. Rig is at depth of 118 with 6tools. Rig is talking about running in with 4.5casing and getting past bad section so hole can be made. |
1936031629 | 2012-09-18 | Plug / Plug Back | No Violations | CGO Rig is plugging well back to surface from 126-0. Ran tubing in to depth of 126 and set down on tools in hole that were lost. Pulled 85of 8.625casing and circulated 146 sacks to surface. No oil or gas was present upon breaking circulation. This plug job was due to lost hole after a clean out could not be performed. Temperature of mix water was 63 Degrees Fahrenheit. The PH of the water was at 7. |
1971672800 | 2012-08-14 | Plug / Plug Back | No Violations | CGO rig crew was running in to check depth with 1.5tubing. They were only able to get to 120down and set on top of tools in hole. I talked to old cable tool companies in Muskingum county for advice on fishing the 7casing out. The rig made a tool that would go over the 7collar and allow it to come out by means of tabs bent in on the 8.625casing. The rig crew tried about three attempts and failed. |
1982128435 | 2012-11-20 | Final Restoration | No Violations | Inspection of well site to check status of the final restoration found that the casing has been cut off and some restoration of the site has taken place. Final Restoration still not complete. |
401313713 | 2012-8-8 0:00:0 | PB | No Violations | 5.00 |
437555378 | 2012-10-23 0:00 | FR | No Violations | 0.50 |
667050009 | 2012-2-14 0:00: | PW | No Violations | 0.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0615939929 | US-OH-126957 | 2010-04-20 | Failure to legibly identify well | |
0907341875 | US-OH-130351 | 2012-03-19 | Well operation causing pollution and contamination | |
0907341875 | US-OH-130352 | 2012-03-19 | General Safety | |
0907341875 | US-OH-130353 | 2012-03-19 | Unlawful method of storage or disposal of brine or other wastes | |
0907341875 | US-OH-130354 | 2012-03-19 | Dike or pit not able to prevent escape of brine or other wastes | |
0907341875 | US-OH-130355 | 2012-03-19 | Unlawful use of pit for temporary storage of brine or other wastes | |
0907341875 | US-OH-130356 | 2012-03-19 | Failure to keep dike or pit free of brine or other wastes | |
1245274149 | US-OH-106429 | 2012-02-13 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1245274149 | US-OH-106430 | 2012-02-13 | Statement of annual production not filed | |
1271767294 | US-OH-107571 | 2010-04-20 | Well shall be plugged | |
1271767294 | US-OH-107572 | 2010-04-20 | Failure to register/obtain or maintain bond/insurance | |
1271767294 | US-OH-107573 | 2010-04-20 | Statement of annual production not filed |
For data sources see[7]