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34-111-20548

Well Details

Well ID: 34-111-20548
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Country: United States
State: Ohio
County: Monroe
Municipality: Seneca Township
Operator Name: C G O INC
Well Pad ID:
Farm/Lease Name: WEISEND BARBARA
License Status: Final Restoration
License Date: 2016-01-29
Spud Date: 1954-06-15
Spud Drilling Contractor:
Final Drill Date: 1954-06-28
Well Total Depth: 1832.00 ft
Configuration: Vertical
Latitude: 39.810000
Longitude: -81.260000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1954-06-15 CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER TO OWNER 12/24/2015.
Completed 1954-06-28 CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER TO OWNER 12/24/2015.
Reached Total Depth 1954-06-28 CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER TO OWNER 12/24/2015.
Change of Owner 2015-12-24 Operator changed from 9998, HISTORIC OWNER to 2849, C G O INC
APP 2016-01-29 Proposed Formations:BEREA, Issued Date:1/29/2016, Expired Date:1/28/2018 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-04-08 CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER TO OWNER 12/24/2015.
Record Last Modified 2017-05-25 CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER TO OWNER 12/24/2015.
Construction Permit Expires 2018-01-28 CHANGED STATUS OF WELL FROM HP TO PR PER TRANSFER FROM HISTORIC OWNER TO OWNER 12/24/2015.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1820 1826 0
1820 1826 0
1820 1826 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 95 Lbs 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 C G O INC 251.00 0.00 365
1992 C G O INC 825.00 0.00 365
1993 C G O INC 200.00 0.00 365
1994 C G O INC 425.00 0.00 365
1995 C G O INC 702.00 0.00 365
1996 C G O INC 353.00 0.00 365
1997 C G O INC 316.00 0.00 365
1998 C G O INC 93.00 0.00 365
1999 C G O INC 84.00 0.00 365
2000 C G O INC 284.00 0.00 365
2001 C G O INC 286.00 0.00 365
2002 C G O INC 306.00 0.00 365
2003 C G O INC 327.00 0.00 365
2004 C G O INC 307.00 0.00 365
2005 C G O INC 265.00 0.00 365
2006 C G O INC 271.00 0.00 365
2007 C G O INC 231.00 0.00 365
2008 C G O INC 243.00 0.00 365
2009 C G O INC 283.00 0.00 365
2010 C G O INC 297.00 0.00 365
2011 C G O INC 283.00 0.00 365
2012 C G O INC 314.00 0.00 366
2015 C G O INC 63.00 0.00 270
2016 C G O INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 C G O INC Brine 0 365
1992 C G O INC Brine 0 365
1993 C G O INC Brine 0 365
1994 C G O INC Brine 0 365
1995 C G O INC Brine 0 365
1996 C G O INC Brine 0 365
1997 C G O INC Brine 0 365
1998 C G O INC Brine 0 365
1999 C G O INC Brine 0 365
2000 C G O INC Brine 0 365
2001 C G O INC Brine 0 365
2002 C G O INC Brine 0 365
2003 C G O INC Brine 0 365
2004 C G O INC Brine 0 365
2005 C G O INC Brine 0 365
2006 C G O INC Brine 0 365
2007 C G O INC Brine 0 365
2008 C G O INC Brine 0 365
2009 C G O INC Brine 0 365
2010 C G O INC Brine 0 365
2011 C G O INC Brine 0 365
2012 C G O INC Brine 0 366
2015 C G O INC Brine 0 270
2016 C G O INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1459957252 2016-04-06 Plug / Plug Back No Violations On site inspection to witness the running of the well bore bond log by Appalachian Wire Line Service. Harmons Well Service rig is on the hole as the plugging contractor. It was observed that 2 pipe is present in the well bore as the primary casing -tubing string combination with a total well bore depth found to be 1,819 with a formation packer set at 1,756 to 1,760, the log indicated the 2 was free above the formation packer up to 630. Plugging shall resume on 04/08/2016.
1460131604 2016-04-08 Plug / Plug Back No Violations Onsite inspection to witness the well plugging process found Harmons Well Service on location and has ran 1 tubing inside the existing 2 production - tubing string to a depth of 1,819. Formation Cementing set a bottom10 sack plug through the 1 to cover the open hole below the formation packer set on the 2 at 1,756. The 1 tubing was then pulled out of the hole and Appalachian Wireline service perforated the 2 tubing at 1,698 to 1,708 and 1,010 to 1,020, with 2 perforations at each point with 10 spacing in between. The 1 tubing was then be ran back in the hole and the well bore cemented with a (2) 315 50 sack plugs set through the 1 tubing at 1,708 and 1,020 with the final plug set from 400 to surface.
1816974110 2016-06-07 Final Restoration No Violations The well site restoration meets ORC 1509.072.

For data sources see[9]

References