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34-105-23709

Well Details

Well ID: 34-105-23709
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Country: United States
State: Ohio
County: Meigs
Municipality: Columbia Township
Operator Name: BANCEQUITY PETROLEUM CORPORATI
Well Pad ID:
Farm/Lease Name: JORDAN JACK & SHEILA
License Status: Well Drilled
License Date: 2012-09-12
Spud Date: 2012-10-15
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.150000
Longitude: -82.270000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2012-09-12 Proposed Formations:BEREA, Issued Date:9/12/2012, Expired Date:9/12/2014 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:EW
Correction to Well 2012-09-14 CORRECTION TO SURFACE LOCATION.
Completion Report Received 2013-04-24
Construction Permit Expires 2014-09-12
Record Last Modified 2017-10-23

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-04-26 1341 1349 9
1341 1349 9
1341 1349 9

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 0 Producers Service Corporation
2013-04-22 H2O 0 42000 Gal 17000 Producers Service Corporation Berea Sandstone perforated from 1341-1349 with 9 shots.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 BANCEQUITY PETROLEUM CORPORATI 107.00 0.00 250
2014 BANCEQUITY PETROLEUM CORPORATI 1379.00 0.00 365
2015 BANCEQUITY PETROLEUM CORPORATI 310.00 0.00 365
2016 BANCEQUITY PETROLEUM CORPORATI 0.00 30.00 365
2017 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365
2018 BANCEQUITY PETROLEUM CORPORATI 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 BANCEQUITY PETROLEUM CORPORATI Brine 1375 250
2014 BANCEQUITY PETROLEUM CORPORATI Brine 365
2015 BANCEQUITY PETROLEUM CORPORATI Brine 4305 365
2016 BANCEQUITY PETROLEUM CORPORATI Brine 1354 365
2017 BANCEQUITY PETROLEUM CORPORATI Brine 0 365
2018 BANCEQUITY PETROLEUM CORPORATI Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1310508952 2013-4-22 0:00: CT No Violations 9.30
-1511833018 2012-10-22 0:00 DD No Violations 9.00
-1770411102 2012-10-23 0:00 DD No Violations 1.80
-1933511340 2012-10-22 0:00 DD No Violations 6.00
0033785944 2012-10-17 Drill / Deepen / Reopen No Violations Witnessed the installation of a mine string. Two voids were encountered from 300-312 feet and from 340-346 feet. The hole had been reamed out down to 390 feet with a 12 1/4 bit. 389 feet of 9 5/8 casing was ran with a basket set at 280 feet. A balance job of 80 sacks was performed to seal off the lower section of the pipe from 389 feet up to 346 feet. A grout job was performed with 75 sacks to seal the upper section from 280 feet to surface.
0035043195 2012-10-23 Drill / Deepen / Reopen No Violations Upon returning to the well to test the BOP it was noted the mud pump that was being used to generate the pressure was unable to hold the required 500 psi for the time allowed. Nitrogen was used to generate the psi needed to perform the test. Multiple attempts were made to reach the test pressure using nitrogen bottles. Unable to reach the minimum testing pressure.
0167610959 2012-10-23 Drill / Deepen / Reopen No Violations Returned to this well after the 8-hour time interval necessary for surface casing cement to mature to witness the BOP test. It failed possibly due to a dry rotted or missing o-ring gasket.
1310508952 2013-04-22 Completion Testing No Violations The 4 1/2 production casing was perforated from 1341-1349 with 9 shots. 42,000 gallons of water and 170 sacks of 20/40 sand were used to fracture the Berea Sandstone formation at 3 Barrels per minute.
1350335135 2012-10-15 Drill / Deepen / Reopen No Violations I accompanied Josh Garland to well site. Rig was not currently drilling. Conductor was set and surface casing was on site. A large pit was present on location.
1350335266 2012-10-15 Drill / Deepen / Reopen No Violations Not currently drilling. 25 feet of conductor has been set and was grouted with 6 sacks of Portland cement. A large pit had been dug and was lined.
1350560779 2012-10-18 Administrative Inspection No Violations I spoke with Randy Wolfe over the phone and he let me know the cement level had dropped to roughly 10 feet below the bottom of the 9 5/8 casing. A cement mixer will be brought on site and they plan to run 6 yards of 9 sack grout to seal off the pipe.
1350700810 2012-10-19 Drill / Deepen / Reopen No Violations Witnessed second remedial grout of mine string. The fluid level was tagged and the hole dynamics between the water flowing through the mine void into the hole were evaluated. The hole was filled with water and allowed to settle out. Then 80 sacks of class A cement were pumped into the hole under very low pressures. 18 Barrels of water were placed behind the cement and was allowed to balance out.
1351086398 2012-10-24 Administrative Inspection No Violations I received a call from Randy Wolfe letting me know the BOP was tested this morning and it was able to hold 500 psi for 15 minutes with less than 5% loss in pressure.
1351128550 2012-10-24 Drill / Deepen / Reopen No Violations Witnessed cementing of the longstring. 1444 of 4 1/2 set in 1450 of 6 1/4 borehole with 66 sacks of Class A. displaced with 22.9 Barrels of fresh water. A latch down plug was ran.
1376418328 2013-08-13 Preliminary Restoration No Violations Well equipped with a pumping unit with an electric motor. The tank battery consists of four 100 barrel steel tanks, a separator, and a meter. There is good vegetative cover, no erosion, pits are closed, and there is no drilling equipment on site.
1511833018 2012-10-22 Drill / Deepen / Reopen No Violations I witnessed the installation of the 7-inch surface casing from 1033-feet to surface. During drilling near the surface, the drill bit penetrated a mine adit. To protect this interval the company ran and cemented a string of 9-5/8 inch casing over this interval. Therefore the amount of cement needed to fill the annular space/volume was based on the calculation of the space between 9-5/8 inch mine casing string from the surface to a depth of 398 feet plus 8-1/2 inch borehole from 398 feet to 1050 feet and the 7-inch casing from 1053 feet to the surface. Using neat cement material without gel, we calculated 185 sacks of cement required to cement 7-inch from current TD to surface. With 1% gel added to cement and 30% excess, actual cement tally was reduced to 160 sacks.
1587790363 2012-12-27 Drill / Deepen / Reopen No Violations The pits have been closed for the 2 month restoration requirements.
167610959 2012-10-23 0:00 DD No Violations 3.00
1677229361 2012-10-18 Drill / Deepen / Reopen No Violations I spoke with a crew member on site, he informed me the cement mixer had just left and they had placed the recommended 6 yards of 9 sack down the casing.
1770411102 2012-10-23 Drill / Deepen / Reopen No Violations The Blow Out Preventer was unable to hold the required 500 psi. the rubber O-ring around the top seal was deteriorated and had to be replaced.
1875272960 2012-10-16 Drill / Deepen / Reopen No Violations At 810 feet the rig switched from air over to water to handle the fluid in the Big Injun. Shortly there after circulation was lost. Though a mine void was never encountered directly it is the suspected cause of the lost circulation. The hole is currently being reamed out with a 12 1/4 bit in order to set an intermediate mine string. The rig is currently drilling at 60 feet. The mine void is suspected to be around 300 feet.
1933511340 2012-10-22 Drill / Deepen / Reopen No Violations 1033 feet of 7 surface casing set in 1050 feet of hole. The first 386 feet of 9 5/8 mine string and the remaining 664 feet are 8 3/4 open hole. 160 sacks of Class A cement with 1% gel were circulated to the surface. The elevators were used to hold the pipe in the hole so it was impossible to verify visually whether or not the cement top dropped significantly. However, the conductor had been grouted in, circulation was established quickly at the beginning of the job, 30% excess cement was used, roughly 3-5 barrels of good cement returns were circulated to the surface, the surface casing string held 500 psi for 15 minutes with no loss in pressure, and a small rock was dropped in the space between the elevators and the casing and hit the cement top almost immediately.
33785944 2012-10-17 0:00 DD No Violations 3.50
35043195 2012-10-23 0:00 DD No Violations 2.00

For data sources see[9]

References