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34-105-22461

Well Details

Well ID: 34-105-22461
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Country: United States
State: Ohio
County: Meigs
Municipality: Olive Township
Operator Name: MOUNTAINEER STATE OPERATIONS L
Well Pad ID:
Farm/Lease Name: CRAFT CL & ROBERT
License Status: Active Injection
License Date: 1985-07-19
Spud Date: 1982-06-12
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1983-06-15
Well Total Depth: 1960.00 ft
Configuration: Vertical
Latitude: 39.160000
Longitude: -81.840000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-06-04 248 SMITH CARL E PETROL INC GeoDate 6/4/82
Oil and Gas 1982-06-04 Issued Date 6/4/82 Expired Date 12/1/82 Acres 0036320 Tool Type RTAF Proposed Formation BEREA Proposed Depth 01960 Proposed Drill Depth 01960
Original Spud 1982-06-12 PERMIT EXPIRED
Completed 1983-06-15 PERMIT EXPIRED
Reached Total Depth 1983-06-15 PERMIT EXPIRED
Completion Report Received 1983-11-17 PERMIT EXPIRED
CO 1985-07-19 248 SMITH CARL E PETROL INC GeoDate 7/19/85
Conversion to Injector 1985-07-19
Salt Water Injection Well 1985-07-19 Issued Date 7/19/85 Expired Date 7/19/86 Acres 0036320 Tool Type RTAF Proposed Formation BIG INJUN Proposed Depth 00000 Proposed Drill Depth 00000
Storage Well 1985-07-19 Issued Date 7/19/85 Expired Date 7/19/86 Acres 0036320 Tool Type RTAF Proposed Formation BIG INJUN Proposed Depth 00000 Proposed Drill Depth 00000
First Injection 1986-01-28 PERMIT EXPIRED
Construction Permit Expires 1986-07-19 PERMIT EXPIRED
Annulus Pressure Monitoring Approved 1989-03-22 PERMIT EXPIRED
Last Compliance Report 2013-08-12 PERMIT EXPIRED
Change of Owner 2019-03-12 Operator changed from 248, CARL E SMITH PETROLEUM INC to 8473, MOUNTAINEER STATE OPERATIONS LLC
Record Last Modified 2019-03-12 PERMIT EXPIRED

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-02 1395 1425 0
2000-05-02 1845 1853 16
1845 1853 16
1395 1425 0
1395 1425 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0
FOAM 0 250 Gal 30000 FRAC;645BBL H2O,30M# SD

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 CARL E SMITH PETROLEUM INC 490.00 0.00 0
1985 CARL E SMITH PETROLEUM INC 365.00 0.00 0
2009 CARL E SMITH PETROLEUM INC 0.00 0.00 0
2010 CARL E SMITH PETROLEUM INC 0.00 0.00 0
2011 CARL E SMITH PETROLEUM INC 0.00 0.00 0
2012 CARL E SMITH PETROLEUM INC 9.00 0.00 366
2013 CARL E SMITH PETROLEUM INC 0.00 0.00 365
2014 CARL E SMITH PETROLEUM INC 0.00 0.00 365
2015 CARL E SMITH PETROLEUM INC 0.00 0.00 365
2016 CARL E SMITH PETROLEUM INC 0.00 0.00 365
2017 CARL E SMITH PETROLEUM INC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 CARL E SMITH PETROLEUM INC Brine 0 0
1985 CARL E SMITH PETROLEUM INC Brine 0 0
2009 CARL E SMITH PETROLEUM INC Brine 0 0
2010 CARL E SMITH PETROLEUM INC Brine 5880 0
2011 CARL E SMITH PETROLEUM INC Brine 0 0
2012 CARL E SMITH PETROLEUM INC Brine 5628 366
2013 CARL E SMITH PETROLEUM INC Brine 1320 365
2014 CARL E SMITH PETROLEUM INC Brine 1380 365
2015 CARL E SMITH PETROLEUM INC Brine 380 365
2016 CARL E SMITH PETROLEUM INC Brine 0 365
2017 CARL E SMITH PETROLEUM INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1018170063 2005-7-28 0:00: SW No Violations
-1037924716 2017-4-11 0:00: SW No Violations 2.50
-1067600848 2018-5-9 0:00:0 SW No Violations 1.00
-1116407205 2012-10-10 0:00 SW No Violations 3.00
-1141630130 2018-9-14 0:00: SW No Violations 1.40
-1175157537 2012-7-23 0:00: SW No Violations
-1222998948 2014-8-19 0:00: SW No Violations 1.50
-1297660666 2013-9-26 0:00: SW No Violations 0.70
-1301105884 2018-8-31 0:00: SW No Violations 2.70
-1329598600 2013-5-6 0:00:0 SW No Violations
-1330358226 2016-10-24 0:00 SW No Violations 1.00
-1360584588 2019-11-4 0:00: SW No Violations 3.60
-1374084100 2012-2-17 0:00: PW No Violations 1.00
-1381618046 2014-6-18 0:00: SW No Violations 2.50
-1412153767 2012-12-11 0:00 SW No Violations 1.50
-1418072846 2016-5-25 0:00: SW No Violations 1.50
-1507873521 2003-12-4 0:00: SW No Violations
-1545213138 2015-3-12 0:00: SW No Violations 0.70
-1638893080 2011-3-30 0:00: SW No Violations
-1640676888 2019-8-19 0:00: SW No Violations 1.10
-1643148761 2004-8-17 0:00: SW No Violations
-1649729114 2015-9-29 0:00: SW No Violations 0.40
-1655422871 2010-12-16 0:00 SW No Violations
-1662974527 2018-9-18 0:00: SW No Violations 0.50
-1690649312 2005-10-20 0:00 SW No Violations
-1700705447 2010-6-21 0:00: SW No Violations 2.00
-1769705098 2009-3-11 0:00: SW No Violations
-1786436592 2012-7-23 0:00: SW No Violations 0.30
-1797620057 2013-11-21 0:00 SW No Violations 4.00
-193252665 2008-12-3 0:00: SW No Violations
-1942460667 2014-9-24 0:00: SW No Violations 1.20
-2035767506 2009-11-6 0:00: SW No Violations
-2093005892 2019-3-12 0:00: SC No Violations 2.50
-2128940937 2014-9-5 0:00:0 SW No Violations 1.00
-2134957181 2019-1-24 0:00: SW No Violations 3.20
-237514194 2011-12-13 0:00 SW No Violations
-292930104 2019-12-9 0:00: SW No Violations 2.20
-359669366 2011-5-26 0:00: SW No Violations 3.00
-363853365 2013-8-7 0:00:0 SW No Violations 10.00
-449619932 2012-7-5 0:00:0 PL No Violations 0.80
-48034223 2007-2-21 0:00: SW No Violations
-687807558 2019-2-11 0:00: SW No Violations
-747978198 2004-2-5 0:00:0 SW No Violations
-782250667 2018-2-16 0:00: SW No Violations
-802416146 2003-8-21 0:00: SW No Violations
-871236474 2012-3-2 0:00:0 SW No Violations 1.30
-916899097 2002-2-20 0:00: SW No Violations
-953659101 2005-1-12 0:00: SW No Violations
-955938628 2014-2-25 0:00: SW No Violations 0.70
-996915144 2012-2-14 0:00: SW No Violations
000PL11123 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0020041082 2007-07-17 Salt Water Injection Well No Violations No violations were found at the time of inspection.
0048034223 2007-02-21 Salt Water Injection Well No Violations All conditions were acceptable.
0076793142 2011-12-15 Salt Water Injection Well No Violations Accompanied J. Scott on SWIW inspection. Dike has roughly 6 inches of water in bottom of it. No other violations. Well on vacuum.
0120696642 2015-04-29 Salt Water Injection Well No Violations Follow up to 527703964. A Mechanical Integrity Test was performed. The annulus was filled with fresh water the day before. 410 psi was placed on the annulus and only 2 psi was lost during the 15 minute test.
0193252665 2008-12-03 Salt Water Injection Well No Violations No violations were found.
0194209111 2008-06-10 Salt Water Injection Well No Violations No violations were found at the time of inspection.
0237514194 2011-12-13 Salt Water Injection Well No Violations Accompanied by Josh Garland MRI. No violations observed during inspection.
0240283625 2017-07-31 Salt Water Injection Well No Violations UIC quarterly inspection. The annulus pressure was 62 PSI, the injection tubing was on vacuum. Legible identification was posted.
0294491020 2017-02-23 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, injection line, injection pressure, and annulus pressure. Identification is posted. 4 small holes were observed in the containment dike liner with the 3 horizontal tanks. The holes in the liner appear to be made by an animal clawing out of the dike. The holes were marked with orange tape. John Kent was called and notified of the holes in the liner.
0359669366 2011-05-26 Salt Water Injection Well No Violations Accompanied J. Scott on complaint of brine dumping. Roughly 10 pine trees had been killed/stressed by the spill. Owner states it was accidental.
0363853365 2013-08-07 Salt Water Injection Well No Violations Installed new Halliburton R-4 packer with used 2 3/8 10 round tubing. Circulated 40 barrels fresh water through tubing prior to setting packer. (last 20 barrels fresh water had 2 gallons inhibitor ) Set packer at 1305.40 feet. Pulled 13,000 lbs tension. Tested the annulus at 415 psi for 15 minutes. At 5 minutes 415 psi. at 15 minutes 408 psi. Test passed.
0399321842 2006-08-16 Salt Water Injection Well No Violations No violations were found.
0427392225 2003-03-05 Salt Water Injection Well Violations Noted FOLLOW UP TO NOV # 737973241 An inspection of the well revealed there is no fittings on the Injection side or the Annulus side of well to check pressures. NEED 1/4 FIITINGS ON WELL, UNABLE TO CHECK PRESSURES ON WELL.
0449619932 2012-07-05 Preliminary Restoration No Violations Water still in dike. A hose was noticed running over the edge of the dike into the wood line. There is no pump means to gravity feed water out of the dike using the hose. And there does not appear to be any affected vegetation outside the dike where the hose terminates.
0506861824 2009-11-05 Surface Facility Construction No Violations Reconstruction of dike. Dike measures 21 by 46 by 2. Submitted dike plan to Tom Tomastik for approval.
0514524137 2013-01-24 Salt Water Injection Well No Violations Dikes are free of water. Some work has been done to the fence near the well and the identification is on the ground. Inspected the injection tubing pressure and the annulus pressure.
0527703964 2015-04-28 Salt Water Injection Well Violations Noted The injection tubing and the annulus were both on a slight vacuum. A pressure test shall be performed in order to demonstrate mechanical integrity.
0635380578 2019-04-22 Salt Water Injection Well No Violations Inspected the unloading pad, containment dikes, tanks, injection line, injection pressure and annulus pressure. Identification is posted. The containment dikes are free of fluids.
0656929786 2009-06-09 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0667869530 2011-08-24 Salt Water Injection Well No Violations Water in dikes. Called Tom Stone, he said that he will take care of the water.
0687807558 2019-02-11 Salt Water Injection Well Violations Noted The Division has not received the 2nd, 3rd, & 4th quarter brine disposal fees for 2018. Please forward disposal fees and sheets to the Division by 3/12/2019.
0704144641 2009-11-06 Surface Facility Construction No Violations Reconstruction of dike and liner. Install 30 mil liner in dike with 3-6000 gallon tanks. 6 of sand was placed below the liner and 6 of sand was placed on top of the liner.
0724406249 2005-05-10 Salt Water Injection Well No Violations There were no violations. However, additional tanks on site appear to have an inadequate dike capacity.
0736867213 2016-01-06 Salt Water Injection Well No Violations No noted violations. Facility does not appear to have been used lately according to log book.
0737973241 2003-03-05 Salt Water Injection Well Violations Noted An inspection of the well revealed there is no fittings on the Injection side or the Annulus side of well to check pressures. NEED 1/4 FIITINGS ON WELL, UNABLE TO CHECK PRESSURES ON WELL.
0739669403 2011-09-27 Salt Water Injection Well No Violations Fresh water in dikes from recent rain event.
0742004490 2009-11-24 Salt Water Injection Well No Violations Three 6,000 gallon tanks are in the new dike and are connected to injection equipment. The second dike liner has not been patched. Damage appears to be from deer in the dike.
0746814585 2008-03-10 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0747978198 2004-02-05 Salt Water Injection Well No Violations No violations at the time of inspection.
0753515775 2018-09-11 Salt Water Injection Well No Violations Compliance Notice # 1534352012 follow up inspection. Good vegetative growth on the remediation area. The containment dike is full of water with an oil sheen. I called Ron the well tender. Ron told me that they have Harmon Services brine truck scheduled to pump out the dikes.
0778986041 2004-05-03 Salt Water Injection Well No Violations Unable to access 1/4 inch female fitting on the tubing, because the plug started to round-off.
0782250667 2018-02-16 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarter of 2017 . Please submit the appropriate reports by March 17, 2018. Reports Received 5/2/2018
0802416146 2003-08-21 Salt Water Injection Well No Violations No violations at the time of inspection.
0861642675 2013-10-30 Salt Water Injection Well No Violations Follow up to -1297660666. The injection tubing was equipped with a fitting to monitor mechanical integrity.
0871236474 2012-03-02 Salt Water Injection Well No Violations The pits are being emptied.
0916899097 2002-02-20 Salt Water Injection Well No Violations
0953659101 2005-01-12 Salt Water Injection Well No Violations There were no violations at the time of inspection.
0955938628 2014-02-25 Salt Water Injection Well No Violations No noted violations.
0996915144 2012-02-14 Salt Water Injection Well Violations Noted Dikes are full of water with an ice layer on top. I called John Kent and told him to remove the water from the dikes. He said that he will have someone do it no later than the 2-15-12.
1000205479 2010-09-14 Administrative Inspection No Violations Received call at 11:21 am from Tom Stone Re: Dike construction for two 100 bbl tanks. Tom told me that the dike dimensions are 42 by 28 by 4 with the tanks sitting on an mound of dirt in middle of dike. Liner will be over the mound of dirt. They will place sand under the liner and on top of liner.
1007804655 2020-3-5 0:00:0 SW No Violations
1018170063 2005-07-28 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1037924716 2017-04-11 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, unloading pad, injection line, injection pressure and annulus pressure. Identification is posted. The containment dikes had 3 inches of water in them.
1042410009 2012-11-29 Production Wells No Violations Follow up to inspection 1354126946. The contaminated soils have been removed. The remaining soil was field tested for pH and my test strips read between 6 and 7.
1067600848 2018-05-09 Salt Water Injection Well No Violations Inspected the unloading pad, containment dikes, tanks, injection line, injection pressure and annulus pressure. Identification is posted.
1116407205 2012-10-10 Salt Water Injection Well No Violations FOLLOW UP TO NOV # 1350659426 Injection tubing is full of fluid. Unloading pad drain has soil with vegetation growing out of the grate. Both dikes have water in them (6-12 inches). Brine hauling log on site shows only one small load hauled on 9-21-12 from tank compressor 1000 gallon tank. Load was put into # 2 tank. Called John Kent and we discussed the need to keep water out of the dikes. We also discussed the wells condition and the fact that they are not injecting water at this time. John told me that they are planning an acid treatment to help open up the formation. They are hauling their production water to Athens injection well.
1124911254 2004-03-09 Salt Water Injection Well No Violations No violations at the time of inspection.
1128616425 2018-08-16 Salt Water Injection Well No Violations Compliance Notice # 1534352012 follow up inspection. ODNR DOGRM ER Lane on location. Tested the scald area with conductivity meter and determined that the scald is from oil spray. Absorbent material has been spread on oil and brine in containment dike. Nothing has been applied to the scald areas outside of the containment dike.
1138651007 2006-01-18 Salt Water Injection Well No Violations No violations at this time.
1141630130 2018-09-14 Salt Water Injection Well No Violations Compliance Notice # 1534352012 follow up inspection. The containment dike has had 15 inches of fluid pumped out of it. There are still 6 inches of fluid with an oil sheen in the dike with the two 100 barrel tanks. The second dike with three horizontal tanks has 8 inches of fluid in it. There is good vegetative growth on the remediation areas outside of the dike. I called Ron the well tender and left a message about needing to have the containment dikes free of fluids.
1153166584 2006-06-22 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1165081060 2004-07-15 Salt Water Injection Well No Violations No violations.
1175157537 2012-07-23 Salt Water Injection Well No Violations Zero pressure on injection tubing. Last recorded brine transport in log book dated 12-14-11. 1000 gallons from compressor yard. Last recorded company annulus test (monthly test) on 6-4-12.
1184353497 2013-05-13 Salt Water Injection Well No Violations Checked injection pressure and annulus pressure. Containment dikes have 4 of water in the low areas of the dike. (recent rain event) I called and talked to John Kent about the dike water and the need to extend the unloading pad so that their truck will fit on it. John told me that they are scheduling a service rig to pull and replace the tubing and packer.
120696642 2015-4-29 0:00: SW No Violations 1.30
1216370383 2013-08-06 Salt Water Injection Well No Violations Francis Brothers service rig on well. Released packer and pulled packer and tubing out of the well. Shut in well head. All valves are closed.
1222998948 2014-08-19 Salt Water Injection Well Violations Noted Unable to test the annular space because the gauge was rounded off and I was unable to remove it.
1251299827 2007-04-12 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1252004373 2009-08-27 Salt Water Injection Well Violations Noted Zero pressure on injection. 100psi on annulus. 3storage tanks 6000 gallons each are located in a dike. They appear to be for storage and possible filtering. The dike liner is torn and damaged in multiple areas. 2 100bbl tanks are also located on site in a different dike. This dike liner appears intact. I called Adam Schoppe and discussed the violations and he is going to arrange the necessary work in the field. I told Adam that the liner needs to be 30 mil with 4 sand under and 4washed gravel over the liner. I also mentioned that they need to check the dike capacity and make sure that it will hold the correct amount.
1262709163 2009-10-13 Administrative Inspection No Violations Received a call from Adam Schope (Mountaineer) Re: What is the minimum thickness for the liner. I told Adam a 30 mil liner needs to be installed. Adam will call me when they get ready to replace the liner.
1271072997 2010-03-17 Salt Water Injection Well Violations Noted Dike has water in dike with the three 6000 gallon tanks. The dike with the two 100 bbl tanks has some small holes in side of dike liner from deer walking over the dike. I have called Adam Schoppe and have given him an verbal NOV for the water in dike needing to be removed and that they need to repair or replace the 100 bbl dike liner. I called Adam on 3-18-10 at 10:24 am. Pictures were taken. Well has good id. Well is connected for disposal.
1284500155 2010-09-10 Administrative Inspection No Violations Received call from Tom Stone Re: Tanks will be delivered Monday. Plan to install pit liner on Tuesday 9-14-10. I reminded Tom and John Kent that the dike must be able to hold 110% of tank capacity.
1296183907 2018-03-14 Salt Water Injection Well No Violations My inspection revealed the salt water injection well had 0 psi on the tubing and 130 psi on the annulus. The dike was free of fluids. Legible identification was posted.
1297660666 2013-09-26 Salt Water Injection Well Violations Noted Unable to test injection pressure because the line had been disconnected. The tubing ended in a 2 ball valve, a 90 degree elbow, and a plug. The company has recently reset the packer and plans to perform an acid job by the end of the month. After the acid job the well shall be fitted with valve and connection in order to monitor mechanical integrity.
1300926899 2014-05-20 Salt Water Injection Well No Violations No noted violation.
1301105884 2018-08-31 Salt Water Injection Well No Violations Compliance Notice # 1534352012 follow up inspection. The containment dike with the two 100 barrel steel tanks has 12 inches of fluid in it. The affected areas outside of the containment dike has been remediated with seed and mulch applied. Good vegetative cover is starting to establish.
1327924250 2018-11-05 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, unloading pad, injection pressure and annulus pressure. Identification is posted. The injection tubing master valve is closed. The injection line from the 100 barrel tank is closed. The containment dike has water in it from rain event. Ron the well tender was called about pumping out the containment dike water.
1329598600 2013-05-06 Salt Water Injection Well No Violations FOLLOW UP TO NOV # 1350659426. There was not a significant amount of water in the dike (raining at time of inspection), the drain on the offloading pad had been cleaned out and was functioning, the manifest at the well states the last time of drop off was 5/1/13 and the well was tested by the company.
1330358226 2016-10-24 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, injection line, injection pressure, annulus pressure , and unloading pad. Identification is posted.
1330871870 2008-09-10 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1340632907 2012-06-25 Salt Water Injection Well No Violations A small amount of water is in the lower side of the large dike. The 3/4 plug is rounded off and was difficult to remove.
1341849755 2012-07-09 Salt Water Injection Well No Violations Water still in dike. The valve on the annular space was replaced but was replaced with too large a fitting. I notified the company and will be back in a few days to check on the progress.
1347600437 2013-10-25 Salt Water Injection Well No Violations Follow up to -1297660666. The fitting on the injection tubing have not yet been installed to allow for mechanical integrity testing.
1350659426 2012-10-10 Salt Water Injection Well Violations Noted Injection tubing is full of fluid. Unloading pad drain has soil with vegetation growing out of the grate. Both dikes have water in them (6-12 inches). Brine hauling log on site shows only one small load hauled on 9-21-12 from tank compressor 1000 gallon tank. Load was put into # 2 tank. Called John Kent and we discussed the need to keep water out of the dikes. We also discussed the wells condition and the fact that they are not injecting water at this time. John told me that they are planning an acid treatment to help open up the formation. They are hauling their production water to Athens injection well.
1354126946 2012-11-28 Production Wells Violations Noted Witnessing an acid job. Three Barrels of a 28% Iron Acid -20M was mixed in the tubs with 6 Barrels of fresh water for the acid treatment. The diluted acid mixture was allow to sit in the mix tub too long and corroded through the welds on the tubs. The mixture then mixed with the limestone along the lease road creating a caustic foam that impacted the area. Roughly 480 square feet of limestone lined lease road was impacted under the truck and roughly 40 square feet of soil was impacted near the well head. The acid ran along a ditch roughly 45 feet before encountering a culvert. The acid does not appear to have traveled through the culvert. Contaminated soils and gravel shall be removed and disposed of properly. If a significant amount of impacted soil is removed topsoil shall be replaced to restore the surface to its original grade. Impacted are shall be seeded and mulched and steps shall be taken to encourage vegetative cover.
1354287102 2012-11-30 Production Wells No Violations Follow up to inspection 1354126946. The limestone gravel has been replaced. The contaminated soil has been replaced and fresh top soil has been laid down. The area has been seeded and mulched in order to encourage vegetative cover. Landscaping mesh has been laid down over the mulch to ensure the mulch remains on site. The culvert has been cleaned out. The soil in the lease road was field tested for acidity and it registered a pH of 7. Pictures of the reclamation taken. The UIC numbers and log of a Viking Well Services Brine truck on site were also verified.
1354290366 2012-11-29 Administrative Inspection No Violations I called and talked to John Kent Re: what is their plan for getting the well capable for injection. John told me that they are rescheduling the acid stimulation for the 1st week of December 2012.
1355248202 2012-12-11 Salt Water Injection Well No Violations Company attempted an acid treatment on well. Three Barrels of 28% Iron Acid were pumped into tubing but were never displaced into formation. Pressure was raised to 300 psi multiple times but the acid never left the tubing. The tubing will be swabbed clean and acid will be stored in a plastic tank for future use. The annular pressure was monitored during the treatment and there was no sign of communication. During the treatment the annular space had no pressure on it while the injection tubing had 300 psi.
1359490911 2013-01-29 Salt Water Injection Well No Violations There is still roughly 1-1.5 feet of water in the dike. The drain on the offloading pad is still plugged and full of water.
1365788127 2013-04-12 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, unloading pad, injection pressure and annulus pressure. Identification at wellhead.
1374084100 2012-02-17 Production Wells Violations Noted Follow up to a verbal compliance notice originally issued 2/14/12 by Jon Scott for water in the dikes at the injection facility. Upon inspection there was roughly a foot of water in both of the containment dikes. Dikes shall be kept empty of all fluids.
1377085894 2013-08-15 Salt Water Injection Well No Violations Injection line is disconnected from the injection tubing. John Kent is scheduling an acid stimulation prior to placing well back into service. Both containment dikes have 5 of water in them from the last rain event.
1381618046 2014-06-18 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, unloading pad, injection pressure and annulus pressure. Identification posted at well. Well is connected for injection. The containment dike with the two 100 barrel steel tanks has approximately 10 inches of water in it. I called John Kent and left a message about the water in the dike and that he needs to remove it and keep the dike free of fluids.
1385559389 2013-11-22 Administrative Inspection No Violations Talked to Tom Stone about the acid job on 11-15-13. Tom said that they spilled 1.5 gallons of acid and cleaned it up and applied lime to the site. I asked for a job report from the service company. Tom said that he will ask John Kent to send one to me.
1398681394 2004-04-08 Salt Water Injection Well No Violations No violations at the time of inspection.
1403943332 2013-01-17 Production Wells No Violations Follow up to inspection done 10/10/12. The drain under the off-loading pad was full of water and is incapable of functioning correctly. The lower dike contained 1-2 feet of water. The drain in the off-loading pad shall be repaired or replaced in order to allow the off-loading pad to drain fluids. The water shall be removed from the lower dike.
1406885551 2010-09-27 Salt Water Injection Well No Violations Replaced two 100 bbl steel tanks and rebuilt dike with new 30 mil liner. Tanks are plumbed and in operation.
1410955294 2014-09-16 Salt Water Injection Well No Violations Follow up to -1222998948. Still unable to test annulus. Called company to correct fittings.
1412153767 2012-12-11 Salt Water Injection Well No Violations Acid job. Josh Garland MRI 2 was on site. I stopped by to check on the progress. Unable to pump through tubing. Acid started to cause leaks on the pump truck. Operation was shut down. I discussed with Tom Stone the need to clean out the well prior to another acid job.
1418072846 2016-05-25 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, unloading pad, injection line, injection pressure and annulus pressure. Identification posted.
1445286044 2015-10-09 Salt Water Injection Well No Violations No noted violations.
1447936836 2015-11-18 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, injection line, injection pressure, annulus pressure and unloading pad. Discussed updates to the facility with the field crew from Mountaineer. The crew was pumping the water from the containment dikes into tanks.
1469707431 2016-07-26 Salt Water Injection Well No Violations Inspected the containment dikes, tanks, unload pad, injection line, injection pressure and annulus pressure. Identification posted. Containment dikes are free of fluids.
1471281353 2006-04-04 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1488488081 2017-02-28 Salt Water Injection Well No Violations Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarters of 2016. Please submit the appropriate reports by March 14, 2017. Reports received 3/21/2017
1489085299 2017-03-07 Surface Facility Construction No Violations Holes in the dike liner have been repaired.
1489442712 2017-03-13 Salt Water Injection Well No Violations Inspected the surface facility that consists of a plastic lined earthen containment dike with three 8,000 gallon steel tanks connected in a series, one 8,000 gallon tank was 2/3 full of fluid, the other two 8,000 gallon tanks are empty, A second plastic lined earthen containment dike with two 100 barrel steel tanks ( both 100 barrel tanks are empty), an unloading pad with a buried vault, Injection line (valve closed) with inline filter housing. The injection line is connected to the injection tubing. The injection pressure is zero. The injection tubing master valve is open. The annulus pressure is 20 psi. Both containment dikes have 3 inches of water in the deep ends of the dikes. Identification is posted at the well site.
1507873521 2003-12-04 Salt Water Injection Well No Violations No violations at the time of inspection.
1534352012 2018-08-15 Salt Water Injection Well Violations Noted Inspected the unloading pad, containment dikes, tanks, injection line, injection pressure and annulus pressure. Multiple scald areas were observed during the inspection. 1st. 15 feet West of the injection well 24 feet by 21 feet. 2nd 36 feet south oh the well 45 feet by 18 feet (area with distressed and dead vegetation.) 3rd. 6 feet east of the well 8 feet by 6 feet. There is 10 inches of oil and brine in the down slope section of the containment dike. The containment dike has two 100 barrel steel tanks. The two inch valve on the injection line is open. I called John Kent at 12:25 pm, and left a message with his receptionist about the release and the need to clean up the contamination. ODNR DOGRM duty officer was notified along with the ODNR DOGRM UIC supervisor. All contaminated material must be disposed of at an EPA approved landfill. The containment dike must be kept free of brine and oil.
1537367583 2018-09-19 Salt Water Injection Well No Violations Compliance Notice # 1534352012 follow up inspection. Both containment dikes are free of fluids. Good vegetative cover has been established on the remediated areas outside of the containment dike. The injection line and injection tubing master valves are closed. Checked injection tubing pressure and annulus pressure. Identification is posted.
1537757963 2008-04-21 Salt Water Injection Well No Violations There were no violations at the time.
1545213138 2015-03-12 Salt Water Injection Well No Violations No noted violations.
1638893080 2011-03-30 Salt Water Injection Well No Violations No violations at this time.
1643148761 2004-08-17 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1646434182 2013-07-10 Salt Water Injection Well No Violations The vault in the unloading pad was functioning correctly. Tanks are being painted. The last load at the facility was delivered about 6 months ago according to the manifest at the well.
1649729114 2015-09-29 Salt Water Injection Well No Violations No noted violations.
1655422871 2010-12-16 Salt Water Injection Well No Violations Good identification. Dikes looked good.
1662974527 2018-09-18 Salt Water Injection Well No Violations compliance Notice # 1534352012 follow up inspection. There is 10 inches of fluid with an oil sheen in the 100 barrel tank dike. There is 10 inches of fluid in the horizontal tank dike.
1667580863 2006-12-18 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1690649312 2005-10-20 Salt Water Injection Well Violations Noted FAILURE TO SUBMIT ANNUAL SALTWATER INJECTION WELL REPORTS FOR 2003 AND 2004
1700705447 2010-06-21 Salt Water Injection Well Violations Noted Water in dike with 3- 6000 gal tanks. Needs pumped out. Leaking 100 bbl tank, also dike liner with 2- 100 bbl tanks has a cut and assorted small holes in the liner. I called and talked to Tom Stone about these issues and he told me that John Kent will be calling me to discuss the violations and to come up with a plan to correct the problems. 100 bbl tank needs to be replaced. New dike liner installed.
1769705098 2009-03-11 Salt Water Injection Well No Violations No violations were found.
1777673751 2004-10-07 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1783058637 2006-10-17 Salt Water Injection Well No Violations There were no violations. Accompanied by Jon Scott.
1783493449 2005-06-23 Salt Water Injection Well No Violations There were no violations at the time of inspection.
1786436592 2012-07-23 Salt Water Injection Well No Violations The fittings have been changed to the appropriate size. There is still water in the dike. Jon Scott had taken the pressures earlier today, I did not check them.
1795553448 2016-03-16 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on February 15th for 2015, despite a letter that was sent March 1, 2016 with a deadline of March 15, 2016 to submit the reports requested. REPORTS RECEIVED
1797620057 2013-11-21 Salt Water Injection Well No Violations Inspected the unloading pad, containment dikes, tanks, injection pressure and annulus pressure. Injection tubing has a valve that is closed. The injection tubing is not connected to injection line due to a well stimulation on 11-15-13. The landowner Mr. Craft told me that acid was spilled on the location during the well stimulation on 11-15-13. Lime powder was observed in multiple locations. Mr. Craft told me that most of the acid went into the dike and was removed with a vacuum truck. I called John Kent and asked about the release. John said that he did not know about it and would ask the field staff about the details. I requested to know the quantity and type of acid that was released and what was done to remediate the site after the release. Both dikes are free of fluids.
1799272176 2019-04-29 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on April 15th for 2018, Please submit the Form 204 to the Division by 5/29/2019.
1812297949 2003-05-20 Salt Water Injection Well No Violations Follow-up on NOV, In-Compliance, met company at well site.
1819623827 2019-6-18 0:00: SW No Violations 3.00
1859388636 2005-10-14 Salt Water Injection Well No Violations There were no violations at the time.
1875603861 2007-06-04 Salt Water Injection Well No Violations No violations were found.
1936518435 2010-08-31 Salt Water Injection Well No Violations 2 100 bbl steel tanks have been drained. New 30 mil liner has come in. Company is waiting on 2 new 100bbl steel tanks to arrive before starting the project. The second dike with 3-6000 gallon tanks has been pumped down 12, dike still has between 1 and 3 of water in low areas of dike.
194209111 2008-6-10 0:00: SW No Violations
1942460667 2014-09-24 Salt Water Injection Well No Violations Follow up to -1222998948. The fittings have been replaced.
1963958168 2009-05-06 Salt Water Injection Well No Violations No violations were found at the time.
1995672921 2020-9-2 0:00:0 SW No Violations 3.00
20041082 2007-7-17 0:00: SW No Violations
2010419901 2006-06-06 Salt Water Injection Well No Violations There were no violations at the time of inspection.
2010913366 2019-11-1 0:00: SW No Violations 1.00
2035767506 2009-11-06 Salt Water Injection Well No Violations Good identification. The injection operation was not in use at the time of inspection.
2038694724 2010-06-24 Administrative Inspection No Violations Talked to Tom Stone Re: leaking 100 bbl tank and replacing dike. Along with pumping out the fresh water in 3-6000 gal. tank dike. Tom said that they are going to replace both 100 bbl tanks and will look into replacing the dike liner at the same time. Tom told me that he has both 100 bbl tanks emptied.
2039398735 2014-11-19 Salt Water Injection Well No Violations No noted violations at facility.
2078873787 2019-02-04 Salt Water Injection Well No Violations Annulus mini test. Tested at 300 psi for 15 minutes with no loss in pressure.
2082190644 2012-07-23 Administrative Inspection No Violations Talked to John Kent and Tom Stone about the injection well status. They told me that they are planning an acid job soon.
2093005892 2019-03-12 Surface Facility Construction No Violations A tree fell on the electric service line and broke the electric pole. The transfer pump on the line between the two containment dikes has been removed for service.
2097863273 2020-4-27 0:00: SW No Violations 3.00
2119402806 2020-2-13 0:00: SC No Violations 3.00
2128940937 2014-09-05 Salt Water Injection Well No Violations Follow up to -1222998948. Still unable to test annulus. Called company and spoke to field supervisor and asked him to correct fittings.
2134957181 2019-01-24 Salt Water Injection Well No Violations Inspected the unloading pad, containment dikes, tanks, injection line, injection pressure and annulus pressure. Identification is posted. The injection tubing master valve is closed. The containment dikes have water and ice approximately 6 inches. Company was notified that a mini test needs to be done on the annulus.
240283625 2017-7-31 0:00: SW No Violations
294491020 2017-2-23 0:00: SW No Violations 1.00
399321842 2006-8-16 0:00: SW No Violations
427392225 2003-3-5 0:00:0 SW No Violations
506861824 2009-11-5 0:00: SC No Violations
514524137 2013-1-24 0:00: SW No Violations 1.00
527703964 2015-4-28 0:00: SW No Violations 0.50
635380578 2019-4-22 0:00: SW No Violations 4.00
656929786 2009-6-9 0:00:0 SW No Violations
667869530 2011-8-24 0:00: SW No Violations
704144641 2009-11-6 0:00: SC No Violations
724406249 2005-5-10 0:00: SW No Violations
736867213 2016-1-6 0:00:0 SW No Violations 0.70
737973241 2003-3-5 0:00:0 SW No Violations
739669403 2011-9-27 0:00: SW No Violations
742004490 2009-11-24 0:00 SW No Violations
746814585 2008-3-10 0:00: SW No Violations
753515775 2018-9-11 0:00: SW No Violations 1.30
76793142 2011-12-15 0:00 SW No Violations 1.00
778986041 2004-5-3 0:00:0 SW No Violations
783723975 2020-2-10 0:00: SW No Violations 2.50
861642675 2013-10-30 0:00 SW No Violations 0.60
PL11123 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0427392225 US-OH-124557 2003-03-06 Violation of injection tubing/fitting requirements
0427392225 US-OH-124558 2003-03-06 Failure to monitor pressures/volumes
0527703964 US-OH-125764 2015-05-11 Failure to monitor annulus pressure
0687807558 US-OH-127790 2019-04-08 Failure to report disposal fees
0737973241 US-OH-128390 2003-03-06 Violation of injection tubing/fitting requirements
0737973241 US-OH-128391 2003-03-06 Failure to monitor pressures/volumes
0782250667 US-OH-128898 2018-08-03 NONE Failure to report disposal fees
0996915144 US-OH-131451 2012-03-07 No SPCC dike/or failure to keep dike free of water or oil
1222998948 US-OH-106004 2014-09-29 Violation of injection tubing/fitting requirements
1252004373 US-OH-106761 2009-09-03 Pits not liquid tight/Improper construction or use
1271072997 US-OH-107545 2010-04-12 Failure to keep dike or pit free of brine or other wastes
1297660666 US-OH-108370 2014-04-23 Violation of injection tubing/fitting requirements
1350659426 US-OH-110162 2012-10-19 No SPCC dike/or failure to keep dike free of water or oil
1354126946 US-OH-110247 2012-12-10 Well operation causing pollution and contamination
1374084100 US-OH-111077 2012-02-17 No SPCC dike/or failure to keep dike free of water or oil
1534352012 US-OH-114760 2018-08-16 9-3-04(A) Pollution/Contamination
1534352012 US-OH-114761 2018-08-16 9-3-05(A)6 Contamination at surface facility (permit after 6-1-82)
1690649312 US-OH-116756 2005-10-20 Failure to monitor pressures/volumes
1700705447 US-OH-116861 2010-06-29 Pollution/Contamination
1700705447 US-OH-116862 2010-06-29 Pits not liquid tight/Improper construction or use
1700705447 US-OH-116863 2010-06-29 Tanks not liquid tight/Improper burial
1795553448 US-OH-117919 2016-05-25 Failure to file salt water injection annual report
1799272176 US-OH-117959 2019-05-09 Failure to file salt water injection annual report

For data sources see[9]

References