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34-105-21995

Well Details

Well ID: 34-105-21995
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Country: United States
State: Ohio
County: Meigs
Municipality: Salisbury Township
Operator Name: J D DRILLING COMPANY
Well Pad ID:
Farm/Lease Name: FEENEY-BENNETT POST #128 {ERP#7}
License Status: Final Restoration
License Date: 2014-04-11
Spud Date: 1984-02-01
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1984-02-17
Well Total Depth: 1865.00 ft
Configuration: Vertical
Latitude: 39.060000
Longitude: -82.080000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-10-16 116 J D DRILLING CO GeoDate 10/16/80
CO 1984-01-30 116 J D DRILLING CO GeoDate 1/30/84
Enhanced Recovery 1984-01-30 Issued Date 1/30/84 Expired Date 7/28/84 Acres 0121250 Tool Type NT Proposed Formation BEREA Proposed Depth 01865 Proposed Drill Depth 01865
Original Spud 1984-02-01
Completed 1984-02-17
Reached Total Depth 1984-02-17
First Injection 1984-03-03
Completion Report Received 1984-06-08
CO 1985-12-17 116 J D DRILLING CO GeoDate 12/17/85
Unknown 1985-12-17 Issued Date 12/17/85 Expired Date 12/17/86 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Annulus Pressure Monitoring Approved 1989-06-06
CO 1994-05-02 4807 OHIO BEAR INC GeoDate 12/17/85
CO 1996-07-05 116 J D DRILLING CO GeoDate 12/17/85
Last Compliance Report 2012-10-24
APP 2014-04-11 Proposed Formations:BEREA, Issued Date:4/11/2014, Expired Date:4/10/2016 12:00:00 PM, Drilling unit acres:121.25, Proposed Well Type:OIL, Proposed Well Class:ERP
Plugged/Abandoned 2014-04-24
Construction Permit Expires 2016-04-10
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-25 1704 1712 1
2000-05-25 1773 1777 1
1773 1777 1
1704 1712 1
1704 1712 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1700 Bbl 0 FRAC;H2O
0 0 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2013 J D DRILLING COMPANY 171.00 0.00 365
2016 J D DRILLING COMPANY 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2013 J D DRILLING COMPANY Brine 0 365
2016 J D DRILLING COMPANY Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1005487630 2012-9-4 0:00:0 SW No Violations 3.00
-1005578184 2007-7-17 0:00: ER No Violations
-1014963371 2009-5-5 0:00:0 ER No Violations
-101730823 2013-7-23 0:00: ER No Violations 5.00
-1038319112 2017-12-27 0:00 FR No Violations 4.50
-107393345 2007-10-22 0:00 ER No Violations
-1116345462 2016-6-8 0:00:0 FR No Violations 2.00
-1140019584 2012-5-4 0:00:0 ER No Violations 2.00
-116772739 2009-3-17 0:00: ER No Violations
-1209101016 2012-10-4 0:00: SW No Violations 0.50
-125958640 2016-12-20 0:00 FR No Violations 0.50
-1272795915 2019-3-7 0:00:0 FR No Violations 0.70
-1330542990 2004-5-3 0:00:0 ER No Violations
-1390339643 2013-1-18 0:00: ER No Violations 1.20
-1439178196 2016-4-13 0:00: FR No Violations 2.50
-1454907603 2014-6-17 0:00: FR No Violations 2.50
-1595126566 2014-1-2 0:00:0 AM No Violations 2.00
-16800175 2004-2-5 0:00:0 ER No Violations
-1683044888 2004-7-20 0:00: ER No Violations
-1687047299 2007-2-16 0:00: ER No Violations
-171915957 2014-11-12 0:00 PB No Violations 3.00
-1770751467 2012-5-7 0:00:0 ER No Violations
-17872069 2013-7-23 0:00: SW No Violations 3.20
-1879729485 2013-6-6 0:00:0 SW No Violations 0.50
-1897236552 2005-6-16 0:00: ER No Violations
-2075986878 2013-7-17 0:00: SW No Violations 0.50
-466558000 2011-3-8 0:00:0 ER No Violations
-482192148 2010-3-18 0:00: ER No Violations
-598432561 2004-4-8 0:00:0 ER No Violations
-614040655 2006-10-17 0:00 SW No Violations
-715095397 2012-8-31 0:00: SW No Violations 3.00
-756312217 2006-3-29 0:00: ER No Violations
-778393604 2009-8-18 0:00: ER No Violations
-787117375 2007-4-4 0:00:0 SC No Violations
-791723429 2004-10-8 0:00: ER No Violations
-883836568 2016-3-9 0:00:0 AM No Violations 1.00
-944743234 2006-5-17 0:00: ER No Violations
-965405149 2004-3-9 0:00:0 ER No Violations
000UIC1802 1999-10-20 Salt Water Injection Well No Violations 1501:9-9-05 (A) (9) DIKE MAINTAINENCE
000UIC1803 1999-10-20 Salt Water Injection Well No Violations 1501:9-3-04 DIKE NEEDS EMPTY
0016800175 2004-02-05 Enhanced Recovery Project No Violations Pressures were measured, while the pump was off.
0017872069 2013-07-23 Salt Water Injection Well No Violations Follow up to -2075986878. Roughly 30 gallons of fresh water used to fill the annular space. Multiple MIT tests were performed, the well was unable to hold the required pressures for the allowed times. Further remedial actions will be taken and well will remain shut in untill mechanical integrity is proven.
0043002956 2015-11-05 Final Restoration Violations Noted The containment dike, injection pump and tank have not been removed from the location. Remove the containment dike materials and take to an EPA approved landfill. Remove all equipment associated with the injection facility. Fill in excavation area. Grade and establish vegetative cover to bind the soil and prevent substantial erosion and sedimentation.
0065299480 2005-07-18 Enhanced Recovery Project No Violations Witnessed the packer installation.
0071815089 2006-01-10 Enhanced Recovery Project No Violations No violations at the time.
0073686839 2011-10-25 Salt Water Injection Well No Violations Accompanied J. Scott on SWIW inspection. No violations.
0089580750 2016-08-31 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The concrete containment dike has not been removed from the location. The electric service pole and electric line are on site. There are two 2 inch plastic lines out side of the dike wall.
0093731866 2018-08-23 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. Collected a sample of the containment water and field tested the sample with Low Range Quantab. The Quantab showed no Cl.
0101730823 2013-07-23 Enhanced Recovery Project No Violations Mechanical integrity test of the annulus. Filled annulus with 30 gallons fresh water. Test was attempted multiple times. Unable to pass the test. Each time annulus leaked off more than 5 % in 15 minutes. Well master valve on the injection tubing is closed. Electric to the injection pump has been shut off. A random brine sample was collected and sent to the lab. Injection tubing was on vacuum during the testing of the annulus.
0107393345 2007-10-22 Enhanced Recovery Project No Violations There were no violations at the time.
0116357224 2008-08-22 Enhanced Recovery Project No Violations No violations were found at the time of inspection.
0116772739 2009-03-17 Enhanced Recovery Project No Violations Unable to gauge the annulus pressure. There were no violations at the time of inspection.
0125958640 2016-12-20 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The concrete containment dike remains in place. The containment dike has no equipment or tanks in it. The electric service lines and poles are still in place. There are two 2 black plastic lines located outside of the containment dike.
0171915957 2014-11-12 Plug / Plug Back No Violations Site visit with UIC section Deputy Chief, Supervisor, and Geologist. Met with Jeff Harper to review plans for converting the containment dike into a brine transfer station.
0217052405 2007-04-12 Surface Facility Construction No Violations Flow lines were plumbed and buried.
0297114270 2008-04-21 Enhanced Recovery Project No Violations There were no violations at the time.
0329792946 2014-12-03 Plug / Plug Back No Violations Well has been plugged. Dike on site being used to contain tanks from other wells on lease.
0333909462 2014-07-24 Final Restoration No Violations Follow up to -2075986878. Final restoration requirements met. The tanks, lines, and dike are to be left and used as a transfer tank for two other wells on the lease.
0404719357 2010-09-27 Enhanced Recovery Project Violations Noted Brine in dike. 12 inches deep. 100 bbl tank overflowing. Pump has broken belts. Electric lines at the dike are a hazard. Yellow romex # 12 wires are ran through the air and spliced with tape. Power lines run into dike and are exposed to water. Wiring needs to be redone by an licensed Electrician. Swedge is leaking brine and has been covered with a rag. Replace all leaking fittings and pump out dike into tank. Identification is not legible. Well must have identification: Well owner, lease name, well number, permit number, county, emergency telephone number.
0466558000 2011-03-08 Enhanced Recovery Project No Violations 1.5 water in dike. Water level is over the lower portion of the pump wheel. Pumper was on site pumping out water into tank when I arrived on location. Pump failed and allowed rain event to fill dike. I was unable to test well due to water level in dike. I called Jonathan Reese and talked to him about the pump.
0482192148 2010-03-18 Enhanced Recovery Project No Violations Id on tank. Water in dike. 10 I called pumper and he came to site and turned on the sump pump to drain the dike.
0508593066 2011-03-30 Enhanced Recovery Project No Violations Dike is free of water.
0573965713 2004-08-17 Enhanced Recovery Project No Violations No violations.
0598432561 2004-04-08 Enhanced Recovery Project No Violations Bad valve on tubing.
0614040655 2006-10-17 Salt Water Injection Well No Violations No violations. Accompanied by Jon Scott.
0621678957 2008-09-11 Enhanced Recovery Project No Violations There were no violations found at the time of inspection.
0628429454 2003-08-14 Salt Water Injection Well No Violations No violations at the time of inspection.
0657333446 2007-06-04 Enhanced Recovery Project No Violations There were no violations at the time of inspection.
0673232016 2012-05-07 Enhanced Recovery Project No Violations Administered Mechanical Integrity Test with Jon Scott. 15-18 Barrels of fresh water run down annulus. Unable to pressure up on annular space. Test Failed.
0706649979 2013-12-19 Enhanced Recovery Project No Violations Well is shut in. Rebuilding packer.
0715095397 2012-08-31 Salt Water Injection Well No Violations 10-12 gallons of fresh water were used to fill the annular space. A fresh water mechanical integrity test was administered to attempt to prove mechanical integrity. The test was administered three times, each time the annular space was unable to hold pressure for the required times. The well was shut in.
0756312217 2006-03-29 Enhanced Recovery Project No Violations Pressures were measured while the pump was off.
0762638953 2003-02-26 Enhanced Recovery Project No Violations
0776235991 2012-08-22 Enhanced Recovery Project Violations Noted Upon inspection it was noted the injection tubing and the annular space were both on vacuum. Injection operations shall cease immediately and a mechanical integrity test shall be performed.
0778393604 2009-08-18 Enhanced Recovery Project No Violations Good id. Concrete dike needs patched. I informed Spence Carpenter.
0787117375 2007-04-04 Surface Facility Construction No Violations Concrete dike was completed. Dimensions were measured at 43 by 24 feet.

Both tanks (400 and 100 bbl.) were set. All was according to the approved plan.

0791723429 2004-10-08 Enhanced Recovery Project No Violations There were no violations at the time of inspection.
0840121334 2012-08-29 Administrative Inspection No Violations I spoke with Spence Carpenter about the companies plans to make corrective actions to the well. he has asked to perform the actions 8/31/12. An extension was granted because the company is currently drilling a new well.
0882914956 2010-11-24 Enhanced Recovery Project No Violations Good identification on tank. Rewired pumps and electric box. Removed yellow # 12 Romex wire and replaced with Grey # 12 AWG Type UFB Sunlight Resistant wire. Brine leak is fixed. Dike is free of water.
0883836568 2016-03-09 Administrative Inspection No Violations Found tank, electric and concrete pit still at site. Will call Jon Scott and discuss the current situation of the resoration.
0944743234 2006-05-17 Enhanced Recovery Project No Violations There were no violations.
0965405149 2004-03-09 Enhanced Recovery Project No Violations Dike full of water. Notified operator.
1005487630 2012-09-04 Salt Water Injection Well No Violations Arrived on location with Josh Garland and Jake Glascock. JD Drillings Service rig and water truck were on location. They were rigged up waiting on a tool to lift the production tubing packer, R4, to reseat it before the mechanical integrity test was performed. According to Josh they have already tried once on an earlier date to conduct this test and it did not pass. Annular space was already loaded with fresh water on top of the packer before we arrived. Josh put his 1000 psi gauge on the annular space and they used air pressure to raise pressure on the water column to 505 psi to start the 15-minute integrity test. At the end of the test, the well pressure measured 481 psi and met compliance by 1.25 psi ( 505 X .95 = 479.75 psi & 481 - 479.75= 1.25 psi). Josh then measured the injection pressure at 0 psi.
1005578184 2007-07-17 Enhanced Recovery Project No Violations No violations were found at the time of inspection.
1014963371 2009-05-05 Enhanced Recovery Project No Violations There were no violations.
1038319112 2017-12-27 Final Restoration No Violations I met with JD Drilling field superintendent Johnathon Reece concerning the remaining items that are left on site. The concrete vault remains along with 5 telephone poles with wire attached to the poles. Johnathon claimed they have a signed landowner waiver. I asked to see the waiver and I was told it would be emailed to me. I told Johnathon I need to see what was waved before the well could be written off for final restoration.
1113347954 2005-05-13 Enhanced Recovery Project Violations Noted
1116345462 2016-06-08 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The steel tank has been removed from the concrete containment dike. No effort has been made to remove the containment dike. Electric service lines are connected to the pole outside of the dike. Two 2 black plastic lines have been cut off outside of the dike.
1131384446 2005-10-26 Enhanced Recovery Project No Violations Overall findings were acceptable.
1140019584 2012-05-04 Enhanced Recovery Project Violations Noted Injection tubing and Annulus were both on vacuum. Mechanical Integrity Test Shall be performed. Well shall cease injection operations immediately.
116357224 2008-8-22 0:00: ER No Violations
1172314155 2007-04-18 Enhanced Recovery Project No Violations Facility construction was completed. The area around the well site will require seed and mulch.
1189433151 2007-09-10 Enhanced Recovery Project No Violations No violations were found.
1202734941 2008-06-02 Enhanced Recovery Project No Violations No violations were found at the time of inspection.
1209101016 2012-10-04 Salt Water Injection Well No Violations Inspector Jon Scott had cited JD Drilling for cracks in the dike needing to be sealed on 8/5/11. The cracks have been sealed. I also checked the pressures on the injection tubing and the annulus.
1212214396 2009-11-24 Enhanced Recovery Project No Violations Good identification. Well is in compliance.
1272795915 2019-03-07 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The concrete containment dike has not been removed. The dike is full of fresh water and ice. The electric lines are still attached to a pole next to the dike.
1311950937 2012-06-11 Enhanced Recovery Project No Violations Injection tubing and annulus have communication. Company attempting to reset packer with service rig. Was unable to fill annulus with fresh water and inhibitor. Pulled tubing and packer. 20th tubing joint had holes in side of tubing. Pulled packer out.
1319554638 2011-10-25 Enhanced Recovery Project No Violations Concrete dike cracks have been sealed. No violations observed during inspection.
1330542990 2004-05-03 Enhanced Recovery Project Violations Noted Unable to measure the pressure on the tubing, because the valve is corroded shut.
1339444875 2012-06-11 Salt Water Injection Well No Violations Packer was released and then reset two feet higher. Freshwater and corrosion inhibitor was placed in the annular space above the packer. When pressurized water flowed out of the tubing. Tubing was pulled and a large hole was found in one of the joints.
1386926567 2012-09-04 Enhanced Recovery Project No Violations Administered fresh water Mechanical Integrity Test. Less than 5 gallons fresh water used to fill the annular space. Annular space was able to hold the required pressure with the allowed decrease in psi for the test period.
1387301668 2013-12-17 Salt Water Injection Well No Violations Follow up to -2075986878. Well has been shut in since last inspection 7/17/13. Haliburton R4 packer is currently set under tension at 1629 feet on 2 3/8 tubing inside 4 1/2 casing. 17.1 Barrels (Bbl) required to fill annular space. 1.3 gallons corrosion inhibitor mixed with 3 Bbl fresh water was used to top off annulus. Company pulled up to 10,500 lbs on packer and tested annulus three times, each test resulted in a failure to demonstrat Mechanical Integrity. Company pulled up to 19,000 lbs on packer and tested a fourth time, resulting in failure. Company unseated packer and reset at 1628 then tested a fifth time. The company was unable to pass the test.
1387386870 2013-12-18 Salt Water Injection Well No Violations Follow up to -2075986878. Testing yesterday indicated possible lek in tubing high in hole. Pulled 5 joints of 2 3/8 tubing and reset packer. The annular space was filled with fresh water and a Mechanical Integrity Test was performed. Annular space unable to hold pressure. Company will pull another 5 joints and test again.
1387544517 2013-12-17 Enhanced Recovery Project No Violations Mechanical Integrity Test. Added 1 gallon inhibitor and 3 barrels of fresh water to annulus. Pulled additional 3,000 lbs on tubing tension. Tested 3 times each test lost more than 5% in 15 minutes. Pulled more tension for a total of 19,000 lbs. Retest annulus, test lost more than 5% in 15 minutes. Released packer and pulled up 18 and reset the packer with 21,000 lbs. filled annulus with fresh water and inhibitor. Tested the annulus, test failed. Lost more than 5% in 15 minutes.
1387817951 2013-12-23 Salt Water Injection Well No Violations Follow up to -2075986878. A rebuilt Haliburton R-4 packer was installed and set under tension at 11,000 pounds using the same tubing at 1626 feet. The annular space was tested three times and the well was unable to pass any of the MIT tests.
1387824519 2013-12-23 Annular Disposal No Violations I accompanied Josh Garland to witness JD Drilling reset packer and perform an annular test.
1390339643 2013-01-18 Enhanced Recovery Project No Violations No violations.
1392754897 2014-02-18 Enhanced Recovery Project No Violations Witnessed new 2 3/8 tubing and a rebuilt Halliburton R-4 packer being installed in the well. Set packer at 1665 and filled annulus with fresh water and inhibitor. Tested annulus 4 times. All lost more than 5% in 15 minutes. Released packer and pulled 2 joints tubing and set packer at 1607 and filled annulus with fresh water and inhibitor. Tested 2 times both lost more than 5% in 15 minutes. Rig pulled more tension on tubing and sheared the pins in the packer. Pulled tubing and packer back out of the well. Company plans to rebuild the packer and also expose the top of the 7 well head to look for any signs of leaks.
1392917453 2014-02-20 Salt Water Injection Well No Violations Follow up to -2075986878. Packer was set on tubing inside 4 1/2 last night and 570 psi was placed in side annulus according to company. This morning I tested the annulus and recorded 575 psi. Today 10 more joints of tubing ran and packer reset at 1212 feet. A MIT was administered with 550 psi on the anulus. The well was not able to hold pressure and the MIT failed.
1396323234 2013-12-18 Enhanced Recovery Project No Violations Released packer and pulled 5 joints of tubing out of the well. Set packer filled annulus and tested annulus to determine cause of leak. Test failed. Pulled additional 10 joints (15 total) and set packer , filled annulus with fresh water and tested. Test failed. Pulled all tubing and packer out of well.
1398371181 2014-04-24 Plug / Plug Back No Violations Plug Job. JD Drilling service rig and water trucks. Formation Cementing. Ran tubing to 1727. Berea perfs are from 1704 to 1712. Pumped 25 sacks class A cement with 2% gel and 4% Cacl. Mixed in Cotton seed hulls as lost circulation material. Tag top of 1st plug at 1318. Attempted to rip 4.5 casing at 1298 and again at 1264 there was no telegraph at surface (holes were cut in 4.5) Pulled up 100 and attempted to find free point, continued at 100 intervals with no success. Free point was established at 272. Fluid level at approximately 400. Attempted to circulate water around 4.5 casing to surface. Pumped 50 barrels fresh water with no returns to surface (air could be felt flowing around 4.5 while pumping water). Bullheaded a 500 cement plug down 4.5 from 1298 to 798. Displaced 13 barrels inside 4.5. Locked in and waited for cement to set. Ripped 4.5 at 375. Circulate fresh water to surface. Circulated a large amount of sand and small gravel water was a red brown color. Conditioned the well with Super Mud and was able to circulate and free the 4.5 casing. Pump cement plug from 375 to surface (in two stages 1st 200 then 175 to surface). Water circulated and stayed at the surface during the entire process. Cement returns to surface.
1439178196 2016-04-13 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The concrete containment dike has one 100 barrel steel tank that is connected on top of the tank by two 2 plastic lines. The electric service is still connected to the poles at the containment dike. The brine pump has been removed from the location.
1454907603 2014-06-17 Final Restoration No Violations Lease road has been graded and gravel has been applied to 3/4 of the road. The lease road is still in use for production wells on the lease. The concrete containment dike, one 100 barrel steel tank, injection pump, lines, and electric service has not been removed. I called Spence Carpenter and Spence told me that they are not sure if they are going to remove the containment dike or reuse the dike and tank for production on the lease. I told Spence that He needs to remove the dike and equipment or submit a waiver form to the UIC section.
1534361534 2018-08-13 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The concrete containment dike is intact and 3/4 full of water. The electric service is still in place and a 2 inch plastic line is cut off just outside the containment.
1555336820 2007-04-10 Surface Facility Construction No Violations No action has taken place since the last inspection.
1558623071 2019-05-23 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. The landowner waiver form for the concrete dike to remain on site has been approved. The concrete dike is full of fresh water. The site has good vegetative cover. Pictures were taken of the dike.
1595126566 2014-01-02 Administrative Inspection No Violations Meeting at JD Drilling office with Spence Carpenter (JD Drilling), and Inspector Josh Garland. We discussed the plans for getting the well in compliance. Spence told us that the plan is to rebuild the R4 packer and install it with a string of new tubing some time next week between 6th and 10th of January 2014. Weather permitting.
1683044888 2004-07-20 Enhanced Recovery Project No Violations The previous violation of tubing/fitting requirements has been remedied. A new valve and gauge have been installed on the tubing. Unable to remove pressure gauge, on the tubing, with an adjustable wrench. This gauge is showing a pressure of 0 psi., however this may actually be a vacuum.
1687047299 2007-02-16 Enhanced Recovery Project No Violations Liner will need replaced.
1722711926 2008-02-25 Enhanced Recovery Project No Violations There were no violations at the time of inspection.
1770751467 2012-05-07 Enhanced Recovery Project No Violations Annulus is on vacuum. Filled annulus with 15 barrels fresh water and inhibitor, and attempted to test. Unable to pressure up on annulus. Spence Carpenter said it could be up to two months before they could get a rig on the well to pull the tubing and packer. Injection is shut down.
1841817771 2011-08-05 Enhanced Recovery Project Violations Noted Good Identification. Concrete dike has cracks that need to be filled. Photos were taken. I called Jonathan Reese and he will have the cracks filled next week then call me for re-inspection.
1848304136 2006-12-18 Enhanced Recovery Project No Violations No violations were found at the time.
1863526457 2005-07-19 Enhanced Recovery Project No Violations Performed a mechanical integrity test on the well.
1866627840 2005-01-14 Salt Water Injection Well No Violations Could not remove the gauge on the tubing.
1879729485 2013-06-06 Salt Water Injection Well No Violations No violations.
1897236552 2005-06-16 Enhanced Recovery Project No Violations Upon arrival, the pump was not operating and there was no pressure on the tubing.

Attempted to increase the annular pressure. However, the pressure would not exceed 80 psi..

 Instructed the well owners representative (Spencer Carpenter) to shut down the operation and requested a suspension order.
1898392404 2005-08-02 Enhanced Recovery Project No Violations Making repairs to the pump and dike.
1989582395 2016-09-28 Final Restoration No Violations Compliance Notice # 43002956 follow up inspection. On location with Jonathan Reese (JD Drilling field supervisor). Jonathan collected two soil samples from the down slope side of the containment dike. Sample # 1 GPS N39.06289/ W082.08139. Sample # 2 GPS N39.06289/ W082.08145. Sample # 3 Control sample was collected at GPS 39.06284/ W082.08069. The containment dike is free of fluids. JD Drilling has requested to use the dike for production operations for the two production wells on the lease.
2016226726 2012-06-12 Enhanced Recovery Project No Violations Install new Halliburton R-4 packer on a different string of used tubing. 3 shear pins were installed on packer (19,000 and 20,000). Packer set at 1629 pulled 7500 lbs over string weight to set packer. Fill annulus with fresh water and inhibitor. Test at 495 psi for 15 minutes. Lost 10 psi. Passed test.
2070615580 2006-07-11 Enhanced Recovery Project No Violations There were no violations at the time of inspection.
2075986878 2013-07-17 Salt Water Injection Well Violations Noted The injection tubing was on vacuum. Gauges read no pressure on the annular space, but after opening the needle valve it was noticed the annular space was full of pressurized gas, not fluid. Pressure differential exists between injection tubing and annular space, mechanical integrity is still intact. However annular space should be full of fluid. An MIT mini test shall be performed and the well must remain shut in until mechanical integrity is proven.
217052405 2007-4-12 0:00: SC No Violations
297114270 2008-4-21 0:00: ER No Violations
329792946 2014-12-3 0:00: PB No Violations 1.50
333909462 2014-7-24 0:00: FR No Violations 0.50
404719357 2010-9-27 0:00: ER No Violations
43002956 2015-11-5 0:00: FR No Violations 1.00
508593066 2011-3-30 0:00: ER No Violations
573965713 2004-8-17 0:00: ER No Violations
621678957 2008-9-11 0:00: ER No Violations
628429454 2003-8-14 0:00: SW No Violations
65299480 2005-7-18 0:00: ER No Violations
657333446 2007-6-4 0:00:0 ER No Violations
673232016 2012-5-7 0:00:0 ER No Violations 1.50
706649979 2013-12-19 0:00 ER No Violations 0.50
71815089 2006-1-10 0:00: ER No Violations
73686839 2011-10-25 0:00 SW No Violations 1.00
762638953 2003-2-26 0:00: ER No Violations
776235991 2012-8-22 0:00: ER No Violations 0.50
840121334 2012-8-29 0:00: AM No Violations 0.30
882914956 2010-11-24 0:00 ER No Violations
89580750 2016-8-31 0:00: FR No Violations 2.00
93731866 2018-8-23 0:00: FR No Violations 1.00
UIC1802 1999-10-20 0:00 SW No Violations
UIC1803 1999-10-20 0:00 SW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0043002956 US-OH-124599 2019-06-05 NONE3 Failure to complete final restoration within six months
0404719357 US-OH-124310 2010-09-28 Mechanical failure/contamination
0404719357 US-OH-124311 2010-09-28 Insufficient/No identification
0776235991 US-OH-128815 2012-09-21 Mechanical failure/contamination
1113347954 US-OH-102855 2005-05-16 Violation of injection tubing/fitting requirements
1113347954 US-OH-102856 2005-05-16 Failure to perform Mechanical Integrity Test
1140019584 US-OH-103536 2012-05-04 Mechanical failure/contamination
1330542990 US-OH-109467 2004-05-11 Violation of injection tubing/fitting requirements
1841817771 US-OH-118399 2011-08-13 Pits not liquid tight/Improper construction or use
2075986878 US-OH-121184 2014-12-09 Mechanical failure/contamination

For data sources see[9]

References