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34-105-20975

Well Details

Well ID: 34-105-20975
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Country: United States
State: Ohio
County: Meigs
Municipality: Olive Township
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name: STATE OF OHIO
License Status: Historical Production Well
License Date:
Spud Date: 1951-05-07
Spud Drilling Contractor:
Final Drill Date: 1951-05-25
Well Total Depth: 2003.00 ft
Configuration: Vertical
Latitude: 39.100000
Longitude: -81.780000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1951-05-07 UPDATE LOCATION PER MATT FULK 2/12/18 ALE.
Completed 1951-05-25 UPDATE LOCATION PER MATT FULK 2/12/18 ALE.
Reached Total Depth 1951-05-25 UPDATE LOCATION PER MATT FULK 2/12/18 ALE.
Record Last Modified 2018-02-12 UPDATE LOCATION PER MATT FULK 2/12/18 ALE.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1079239657 2018-9-11 0:00: PW No Violations 0.70
-235977451 2013-8-20 0:00: PW No Violations 1.00
-800881295 2013-8-12 0:00: PW No Violations 1.00
0082258774 2018-07-16 Production Wells No Violations The fuel that spilled from the fuel tank is cleaned up. The affected soils have been removed. The fuel tank has been raised up and is sitting on blocking. There also appeared as though a hydraulic hose was leaking and is now being contained in a plastic container. I texted Billy Putnam the owner of the well about when he would finish the work on this location.
0235977451 2013-08-20 Production Wells No Violations Follow up to 1372711334. Roughly 95% of the fluids have been removed from the dike.
0364795933 2013-07-01 Production Wells No Violations Verified location and API number with producer. No tanks. Well equipped with 13 conductor, 7 casing, 4 1/2 on a packer. Service work currently being done on well.
0495082003 2014-12-03 Production Wells No Violations follow up to 1372711334. Pit has been filled and contaminated soils removed. Vegetative cover established at the site. The rig and equipment remain on the well.
0543699861 2018-09-18 Production Wells No Violations Billy Putnam placed his identification at the wellhead.
0800881295 2013-08-12 Production Wells No Violations Follow up to 1372711334. The fluid level in the pit is at the same level, the pit liner is still missing in the corner.
0839575825 2013-07-23 Production Wells No Violations Follow up to 1372711334. The pit has not been emptied yet and no remediation has taken place.
1059936347 2013-08-13 Administrative Inspection No Violations Spoke with the producer about timeline regarding emptying of the pits and clean up at the site.
1079239657 2018-09-11 Production Wells No Violations The rig is still on location and well still has no identification posted. Texted Billy Putnam and he said the signs were in his truck he just couldnt find the API number.
1113347087 2018-02-08 Production Wells No Violations There is a service rig that is rigged down and next to the well. I also believe that this is one of Billys wells. Josh Garland met Billy at his wells in 2013 and this is one they went to. This well is also plotted wrong in RBDMS it is over a mile from the correct coordinates in RBDMS.
1372711334 2013-07-01 Production Wells Violations Noted There is a large pit on site roughly 30 x 35 and is full of water. The liner has slipped in the corner and about 1/3 of the pit is now unlined. The water in the pit was tested and found to have 6508+ ppm Cl- content. The company appears to have been drilling out the well, there is a mud pump and 47 joints of tubing on site. The pit shall be emptied and the water shall be disposed of properly. Any contaminated soils shall be removed. After the pit is closed, any affected areas at the surface shall be seeded, mulched, and steps shall be taken to encourage vegetative cover.
1374850251 2013-07-26 Production Wells No Violations Met with forest manager and District manager to review remediation effort at well site.
1378390264 2013-09-05 Production Wells No Violations Follow up to 1372711334. The contaminated soils are being removed from the pit area and taken to a landfill.
1378992030 2013-09-11 Production Wells No Violations Follow up to 1372711334. The majority of the contaminated soils appear to have been removed.
1382635949 2013-10-24 Production Wells No Violations Follow up to 1372711334. Witnessed sides of pit containing contaminated soils being removed. Field sampled cleaned areas with Quan tab test strips to verify Chloride content of soil left on site.
1454508723 2018-05-22 Production Wells No Violations Billy Putnams rig is rigged up on the well. This will need transferred to his name. It went from his Grandfather to historic. This well was never transferred. I emailed Grubaugh, Putnam and my supervisors about this matter.
1938228919 2018-05-07 Production Wells No Violations Well is idle, I suspect that it is Billy Putnams well it was just never transferred. There is a service rig at the location. There are railroad ties chunked up around the wellhead. The wellhead has no flowlines attached, there is only a relatively new and shiny swage nipple from 4-2 with a valve in the closed position.
1986437831 2013-09-12 Production Wells No Violations Follow up to 1372711334. Soil samples along wall of pits taken. The first pit had CaCl- levels around 100-150 ppm. The second pit had CaCl- levels around 600 ppm.
2019578488 2013-09-06 Production Wells No Violations Follow up to 1372711334. Not currently working.
2078743548 2013-12-24 Production Wells No Violations Follow up to 1372711334. The pits have been closed, there is no vegetative cover. The rig is still on the well.
364795933 2013-7-1 0:00:0 PW No Violations 0.20
495082003 2014-12-3 0:00: PW No Violations 1.50
543699861 2018-9-18 0:00: PW No Violations
82258774 2018-7-16 0:00: PW No Violations 0.40
839575825 2013-7-23 0:00: PW No Violations 1.20

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1372711334 US-OH-111051 2014-12-09 Well operation causing pollution and contamination
1372711334 US-OH-111052 2014-12-09 Dike or pit not able to prevent escape of brine or other wastes

For data sources see[3]

References