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Well ID: 34-103-24648 | Loading map...
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Country: United States | |
State: Ohio | |
County: Medina | |
Municipality: Chatham Township | |
Operator Name: KING OIL COMPANY INC | |
Well Pad ID: | |
Farm/Lease Name: WALKDEN-PACKARD | |
License Status: Final Restoration | |
License Date: 2006-04-05 | |
Spud Date: 1991-09-09 | |
Spud Drilling Contractor: M&G OIL CO. | |
Final Drill Date: 1991-10-31 | |
Well Total Depth: 518.00 ft | |
Configuration: Vertical | |
Latitude: 41.130000 | |
Longitude: -82.040000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Enhanced Recovery | 1991-07-22 | Issued Date 7/22/91 Expired Date 7/21/92 Acres 0071000 Tool Type RTF Proposed Formation BEREA Proposed Depth 00518 Proposed Drill Depth 00518 |
Original Spud | 1991-09-09 | |
Completed | 1991-10-31 | |
Reached Total Depth | 1991-10-31 | |
CO | 1992-02-15 | 3803 LASALLE EXPLORATION INC GeoDate 7/22/91 |
First Injection | 1992-02-15 | |
Completion Report Received | 1992-02-18 | |
Annulus Pressure Monitoring Approved | 1994-10-25 | |
Last Compliance Report | 2000-03-14 | |
Change of Owner | 2004-12-21 | Operator changed from 3803, LASALLE EXPLORATION INC to 6748, HEARTLAND OIL & GAS |
APP | 2006-04-05 | Proposed Formations:BEREA, Issued Date:4/5/2006, Expired Date:4/5/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:EOR, Proposed Well Class:ERP |
Plugged/Abandoned | 2006-08-02 | |
Construction Permit Expires | 2007-04-05 | |
Change of Owner | 2009-10-01 | Operator changed from 6748, HEARTLAND OIL & GAS to 8547, KING OIL COMPANY INC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 370 | 388 | 0 |
2000-05-25 | 354 | 481 | 0 |
354 | 481 | 0 | |
370 | 388 | 0 | |
354 | 481 | 0 | |
2006-09-11 | 450 | 486 | 0 |
2006-09-11 | 410 | 440 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | SHOTS WITH NITRO |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1249581141 | 2005-8-30 0:00: | ER | No Violations | 0.50 |
-2120833615 | 2005-3-8 0:00:0 | ER | No Violations | 0.50 |
0000012901 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 6/9/92 INSPECTOR HAROLD MORAVY DATE 06/0919/92 DATA FROM OLD VAX INFO | |
0008575404 | 2005-05-18 | Enhanced Recovery Project | Violations Noted | Injection well remains idle. 2 tubing in well pit with valves closed. No pressure on injection tubing. Pump house is flooded and idle. No response to NOV. Brine contamination inside and outside dike. 5x 20 scald area. Production wells are producing on ERP 59 project. Requesting Chiefs Order to plug or inject well. Photos taken of well and tank battery. Sun, 60 degrees. |
0014678825 | 2002-02-05 | Enhanced Recovery Project | No Violations | Idle Injection well. Pumps are shut down leading to this well. 0 psi on gauge. 2 of snow on ground and 20 degrees. |
0140054119 | 2005-07-25 | Enhanced Recovery Project | Violations Noted | C.O. 2005-36 in non compliance. |
0520995796 | 2008-03-19 | Final Restoration | No Violations | Final restoration approved. Crop field. P&A 8-2-2006 |
0646929201 | 2005-06-22 | Enhanced Recovery Project | Violations Noted | CO-2005-36 in non-compliance. Well remains idle. No response to Chiefs Order or NOV. |
0806343918 | 2005-10-21 | Enhanced Recovery Project | Violations Noted | Non-compliance with Chiefs Order 2005-36. No response to plug or inject well. Request Bond Forfeiture. |
1153487243 | 2006-07-21 | Plug / Plug Back | No Violations | Order # 2005-99. Due date is 7-28-2006. Began to circulate well thru tubing and returns were immediate. Tubing is parted up hole. Shut down job to check tubing integrity. |
1154553163 | 2006-08-02 | Enhanced Recovery Project | Violations Noted | CO 2005-99 in compliance well was plugged on 8-02-2006. |
1249581141 | 2005-08-30 | Enhanced Recovery Project | Violations Noted | Non-compliance with CO 2005-36. Well remains idle. Rain, 75 degrees. |
12901 | PL | No Violations | ||
140054119 | 2005-7-25 0:00: | ER | No Violations | 1.00 |
14678825 | 2002-2-5 0:00:0 | ER | No Violations | 0.10 |
2120833615 | 2005-03-08 | Enhanced Recovery Project | Violations Noted | Idle injection well. Pumps are shut down and water has flooded the pump house. No injection since 2002. Snow 25 degrees. |
520995796 | 2008-3-19 0:00: | FR | No Violations | 1.00 |
646929201 | 2005-6-22 0:00: | ER | No Violations | 0.50 |
806343918 | 2005-10-21 0:00 | ER | No Violations | 1.00 |
8575404 | 2005-5-18 0:00: | ER | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0008575404 | US-OH-129772 | 2005-05-18 | Contamination at storage facility (permit after 6/1/82) | |
0008575404 | US-OH-129773 | 2005-05-18 | Well incapable of inj./production | |
0140054119 | US-OH-111861 | 2005-07-25 | Contamination at storage facility (permit after 6/1/82) | |
0140054119 | US-OH-111862 | 2005-07-25 | Well incapable of inj./production | |
0646929201 | US-OH-127336 | 2005-06-22 | Contamination at storage facility (permit after 6/1/82) | |
0646929201 | US-OH-127337 | 2005-06-22 | Well incapable of inj./production | |
0806343918 | US-OH-129060 | 2005-07-25 | Contamination at storage facility (permit after 6/1/82) | |
0806343918 | US-OH-129061 | 2005-10-21 | Well incapable of inj./production | |
1154553163 | US-OH-104039 | 2005-07-25 | Contamination at storage facility (permit after 6/1/82) | |
1154553163 | US-OH-104040 | 2005-08-30 | Well incapable of inj./production | |
1249581141 | US-OH-106679 | 2005-07-25 | Contamination at storage facility (permit after 6/1/82) | |
1249581141 | US-OH-106680 | 2005-08-30 | Well incapable of inj./production | |
2120833615 | US-OH-121727 | 2005-07-25 | Contamination at storage facility (permit after 6/1/82) | |
2120833615 | US-OH-121728 | 2005-03-08 | Well incapable of inj./production |
For data sources see[5]