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34-103-23917

Well Details

Well ID: 34-103-23917
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Country: United States
State: Ohio
County: Medina
Municipality: Wadsworth Township
Operator Name: BASS ENERGY CO INC
Well Pad ID:
Farm/Lease Name: MOWERY UNIT
License Status: Plugged and Abandoned
License Date: 2014-04-25
Spud Date: 1985-02-05
Spud Drilling Contractor: NANCY DRLG
Final Drill Date: 1985-02-11
Well Total Depth: 3560.00 ft
Configuration: Vertical
Latitude: 41.040000
Longitude: -81.780000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-10-16 1639 BASS ENERGY CO INC GeoDate 10/16/84
Oil and Gas 1984-10-16 Issued Date 10/16/84 Expired Date 4/14/85 Acres 0020000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 03560 Proposed Drill Depth 03560
Original Spud 1985-02-05 CHG IN FTG. 2-16-85
Completed 1985-02-11 CHG IN FTG. 2-16-85
Reached Total Depth 1985-02-11 CHG IN FTG. 2-16-85
Completion Report Received 1985-03-07 CHG IN FTG. 2-16-85
APP 2014-04-25 Proposed Formations:CLINTON, Issued Date:4/25/2014, Expired Date:4/24/2016 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-07-10 CHG IN FTG. 2-16-85
Construction Permit Expires 2016-04-24 CHG IN FTG. 2-16-85
Record Last Modified 2017-02-15 CHG IN FTG. 2-16-85

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3386 3444 0
3386 3444 0
2006-09-11 3402 3425 17
3402 3425 17
3386 3444 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 50000 FRAC;H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 BASS ENERGY CO INC 3205.00 470.00 245
1986 BASS ENERGY CO INC 3869.00 203.00 365
1987 BASS ENERGY CO INC 2866.00 176.00 365
1988 BASS ENERGY CO INC 2561.00 84.00 365
1989 BASS ENERGY CO INC 2021.00 106.00 365
1990 BASS ENERGY CO INC 1493.00 68.00 365
1991 BASS ENERGY CO INC 1276.00 26.00 365
1992 BASS ENERGY CO INC 824.00 38.00 365
1993 BASS ENERGY CO INC 433.00 34.00 365
1994 BASS ENERGY CO INC 15.00 0.00 365
1995 BASS ENERGY CO INC 299.00 0.00 365
1996 BASS ENERGY CO INC 233.00 56.00 365
1997 BASS ENERGY CO INC 117.00 0.00 365
1998 BASS ENERGY CO INC 157.00 0.00 365
1999 BASS ENERGY CO INC 4.00 0.00 365
2000 BASS ENERGY CO INC 0.00 0.00 0
2001 BASS ENERGY CO INC 0.00 0.00 0
2002 BASS ENERGY CO INC 0.00 0.00 0
2003 BASS ENERGY CO INC 0.00 0.00 0
2004 BASS ENERGY CO INC 0.00 63.00 365
2005 BASS ENERGY CO INC 0.00 0.00 0
2006 BASS ENERGY CO INC 0.00 0.00 0
2007 BASS ENERGY CO INC 0.00 0.00 0
2008 BASS ENERGY CO INC 0.00 0.00 0
2009 BASS ENERGY CO INC 0.00 0.00 0
2012 BASS ENERGY CO INC 0.00 0.00 0
2013 BASS ENERGY CO INC 0.00 0.00 0
2014 BASS ENERGY CO INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 BASS ENERGY CO INC Brine 60 245
1986 BASS ENERGY CO INC Brine 0 365
1987 BASS ENERGY CO INC Brine 0 365
1988 BASS ENERGY CO INC Brine 5 365
1989 BASS ENERGY CO INC Brine 0 365
1990 BASS ENERGY CO INC Brine 20 365
1991 BASS ENERGY CO INC Brine 0 365
1992 BASS ENERGY CO INC Brine 0 365
1993 BASS ENERGY CO INC Brine 0 365
1994 BASS ENERGY CO INC Brine 0 365
1995 BASS ENERGY CO INC Brine 0 365
1996 BASS ENERGY CO INC Brine 0 365
1997 BASS ENERGY CO INC Brine 0 365
1998 BASS ENERGY CO INC Brine 0 365
1999 BASS ENERGY CO INC Brine 0 365
2000 BASS ENERGY CO INC Brine 0 0
2001 BASS ENERGY CO INC Brine 0 0
2002 BASS ENERGY CO INC Brine 0 0
2003 BASS ENERGY CO INC Brine 0 0
2004 BASS ENERGY CO INC Brine 0 365
2005 BASS ENERGY CO INC Brine 0 0
2006 BASS ENERGY CO INC Brine 0 0
2007 BASS ENERGY CO INC Brine 0 0
2008 BASS ENERGY CO INC Brine 0 0
2009 BASS ENERGY CO INC Brine 0 0
2012 BASS ENERGY CO INC Brine 0 0
2013 BASS ENERGY CO INC Brine 0 0
2014 BASS ENERGY CO INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1444126332 2015-7-27 0:00: FR No Violations
-1734674536 2015-7-20 0:00: FR No Violations
-721213231 2015-7-9 0:00:0 PB No Violations
000PL11540 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0662303422 2015-07-10 Plug / Plug Back No Violations Visited location on 07/10/2015 to witness plugging operations at the Mowery Unit #3 well. Nicks Well Plugging finished pulling tubing. Loaded hole. Ran in hole with ripping tool. Ripped production casing at 2,366. Pulled 1 joint of casing, broke circulation, and set Big Lime/Oriskany plug from 2,324-2,024. Pulled out 41 joints of casing, broke circulation, and set Berea/Surface casing plug from 616-416. Pulled out 10 joints of casing, broke circulation, and set top plug from 200-surface. Pulled out last 5 joints of casing. Cement fell back approximately 1. Topped off with pre-mixed cement. No problems were encountered during plugging operations.
0721213231 2015-07-09 Plug / Plug Back No Violations Visited location on 07/09/2015 to witness plugging operations of the Mowery Unit #3 well. Finished moving in and rigging up Nicks Well Plugging. Blew well down. Ran in hole with 1 1/2 tubing to bottom. Waited on water truck, which kept breaking down on the lease road. Got water truck on-site and rigged up. Set Clinton (bottom) plug through tubing from 3,475-3,075. Tripped out of hole with tubing - 1,500 left in hole to continue pulling in the morning.
1043592855 2015-08-03 Final Restoration No Violations Visited location on 08/03/2015 to follow-up on the status of location reclamation. The location has been completely graded, seeded, fertilized, and covered with straw. Will wait on grass to begin growing, then final restoration will be approved.
1249375767 2015-06-04 Production Wells No Violations Visited location on 06/04/2015 with Bill Hlavin and Ralph Gregory with Bass Energy to locate the well and attempt to figure out how to access it to plug it. The well is equipped with a wellhead with a swedge. All tanks and production equipment were removed ~10+ years ago. There is currently no access to the well. Met with landowners to discuss access. Will continue to monitor the situation until the well is plugged.
1444126332 2015-07-27 Final Restoration No Violations Visited location on 07/27/2015 to check on status of location reclamation. The lease road has been filled-in, and grass seed and fertilizer has been laid down. Plan to get straw laid down by the end of the day. Will continue to follow-up.
1648001225 2015-07-16 Plug / Plug Back No Violations Visited location on 07/16/2015 to check on location reclamation from plug job. Pit has been filled in, but no other reclamation has been done. Talked to Ralph Gregory with Bass Energy - reclamation is waiting on weather conditions to improve and is expected to begin next week.
1734674536 2015-07-20 Final Restoration No Violations Visited location on 07/20/2015 to follow-up on the status of location reclamation. Reclamation has not yet been completed due to poor weather conditions. Will contact operator to determine plan forward.
662303422 2015-7-10 0:00: PB No Violations
PL11540 PL No Violations

For data sources see[9]

References