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34-099-22190

Well Details

Well ID: 34-099-22190
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Country: United States
State: Ohio
County: Mahoning
Municipality: Canfield Township
Operator Name: EVERFLOW EASTERN PARTNERS LP
Well Pad ID:
Farm/Lease Name: KARNDFEL UNIT
License Status: Producing
License Date: 1987-10-21
Spud Date: 1987-12-01
Spud Drilling Contractor: [[JL COATS [COATS-GOFF]]]
Final Drill Date: 1987-12-07
Well Total Depth: 5320.00 ft
Configuration: Vertical
Latitude: 41.060000
Longitude: -80.780000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1987-10-21 Issued Date 10/21/87 Expired Date 10/20/88 Acres 0095160 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05320 Proposed Drill Depth 05320
Original Spud 1987-12-01
Completed 1987-12-07
Reached Total Depth 1987-12-07
CO 1987-12-11 84 EVERFLOW EASTERN PTNS L P GeoDate 10/21/87
Completion Report Received 1987-12-23
Construction Permit Expires 1988-10-20
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5065 5186 0
5065 5186 0
2006-09-11 5078 5138 31
5078 5138 31
5065 5186 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 101230 Gal 65000 FRAC: H2O,SAND42

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1988 EVERFLOW EASTERN PARTNERS LP 0.00 0.00 0
1989 EVERFLOW EASTERN PARTNERS LP 10108.00 0.00 107
1990 EVERFLOW EASTERN PARTNERS LP 13438.00 81.00 365
1991 EVERFLOW EASTERN PARTNERS LP 8842.00 0.00 365
1992 EVERFLOW EASTERN PARTNERS LP 5919.00 0.00 365
1993 EVERFLOW EASTERN PARTNERS LP 5569.00 0.00 365
1994 EVERFLOW EASTERN PARTNERS LP 6392.00 0.00 365
1995 EVERFLOW EASTERN PARTNERS LP 4839.00 0.00 365
1996 EVERFLOW EASTERN PARTNERS LP 5525.00 0.00 365
1997 EVERFLOW EASTERN PARTNERS LP 5332.00 0.00 365
1998 EVERFLOW EASTERN PARTNERS LP 5168.00 70.00 365
1999 EVERFLOW EASTERN PARTNERS LP 4613.00 0.00 365
2000 EVERFLOW EASTERN PARTNERS LP 3191.00 0.00 365
2001 EVERFLOW EASTERN PARTNERS LP 3827.00 0.00 365
2002 EVERFLOW EASTERN PARTNERS LP 2906.00 0.00 365
2003 EVERFLOW EASTERN PARTNERS LP 3721.00 0.00 365
2004 EVERFLOW EASTERN PARTNERS LP 6449.00 0.00 365
2005 EVERFLOW EASTERN PARTNERS LP 3215.00 0.00 365
2006 EVERFLOW EASTERN PARTNERS LP 3409.00 0.00 365
2007 EVERFLOW EASTERN PARTNERS LP 3255.00 0.00 365
2008 EVERFLOW EASTERN PARTNERS LP 2530.00 0.00 365
2009 EVERFLOW EASTERN PARTNERS LP 3460.00 0.00 365
2010 EVERFLOW EASTERN PARTNERS LP 3056.00 0.00 365
2011 EVERFLOW EASTERN PARTNERS LP 3685.00 0.00 365
2012 EVERFLOW EASTERN PARTNERS LP 3038.00 0.00 366
2013 EVERFLOW EASTERN PARTNERS LP 2972.00 0.00 365
2014 EVERFLOW EASTERN PARTNERS LP 2171.00 0.00 275
2015 EVERFLOW EASTERN PARTNERS LP 1414.00 0.00 365
2016 EVERFLOW EASTERN PARTNERS LP 1070.00 0.00 365
2017 EVERFLOW EASTERN PARTNERS LP 2176.00 0.00 365
2018 EVERFLOW EASTERN PARTNERS LP 2052.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1988 EVERFLOW EASTERN PARTNERS LP Brine 0 0
1989 EVERFLOW EASTERN PARTNERS LP Brine 0 107
1990 EVERFLOW EASTERN PARTNERS LP Brine 35 365
1991 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1992 EVERFLOW EASTERN PARTNERS LP Brine 80 365
1993 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1994 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1995 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1996 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1997 EVERFLOW EASTERN PARTNERS LP Brine 60 365
1998 EVERFLOW EASTERN PARTNERS LP Brine 0 365
1999 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2000 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2001 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2002 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2003 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2004 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2005 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2006 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2007 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2008 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2009 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2010 EVERFLOW EASTERN PARTNERS LP Brine 24 365
2011 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2012 EVERFLOW EASTERN PARTNERS LP Brine 0 366
2013 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2014 EVERFLOW EASTERN PARTNERS LP Brine 0 275
2015 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2016 EVERFLOW EASTERN PARTNERS LP Brine 0 365
2017 EVERFLOW EASTERN PARTNERS LP Brine 28 365
2018 EVERFLOW EASTERN PARTNERS LP Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
000PL12619 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1487102730 2017-02-09 Production Wells No Violations I received a call at 10:19 AM from the Austintown Fire Department ( 330-799-8502 ) . They had received a call from a person walking the Mill Creek Hike and Bike about and odor and a sheen of oil inside the tank battery at the above location. Terry Whitehair Northeast Emergency Response Supervisor an myself responded to the call. I called George Stramm from Everflow Eastern and he explained to me that they had discovered a small leak (pen hole) at the 3 fitting at the bottom of the tank. He also had his field foreman Kevin Dow to respond also. The tank at that time had 26 25.8 bbls of fluid. The fluid was removed and the tank was laid over on its side until they can get into the location to remove it. The access road is the property owners yard at this time. There is a dike constructed around the tank battery. The dike had some water and some frozen ice. They will notify me when they remove it. There is a Complaint Status Report # 5529 on this incident
1547491008 2019-01-14 Production Wells No Violations I was on location to perform an inspection on this well and tank battery regarding complaint #5529. A call was received by the Austintown Fire Dept. on 2/8/17 from a hiker who had been walking on the Mill Creek Hike and Bike Trail. The Austintown Fire Dept. Chief said the hiker had seen an oil sheen inside the containment of the dike as the company had been disassembling the tank. The tank was removed by Strawn Oilfield and the site remediated of the oil sheen. A new 50bbl tank has been set in the dike with the existing horizontal separator. The tank battery contains proper identification. The well is a producing plunger lift well with the 8.625 casing plumber to the surface with no violations. The tank battery has been reclaimed and the new production equipment installed. At this time the complaint can be closed.
PL12619 PL No Violations

For data sources see[9]

References