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| Well ID: 34-087-20649 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Lawrence | |
| Municipality: Union Township | |
| Operator Name: PILLAR ENERGY LLC | |
| Well Pad ID: | |
| Farm/Lease Name: DINGUS | |
| License Status: Producing | |
| License Date: 2006-09-12 | |
| Spud Date: 2006-10-16 | |
| Spud Drilling Contractor: TARGET DRLG | |
| Final Drill Date: 2006-11-01 | |
| Well Total Depth: 2842.00 ft | |
| Configuration: Vertical | |
| Latitude: 38.470000 | |
| Longitude: -82.490000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2006-09-12 | Proposed Formations:BIG LIME, Issued Date:9/12/2006, Expired Date:9/12/2007 6:00:00 AM, Drilling unit acres:443.97, Proposed Well Type:ST, Proposed Well Class:EW |
| Reached Total Depth | 2006-11-01 | |
| Construction Permit Expires | 2007-09-12 | |
| Completion Report Received | 2008-06-18 | |
| Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
| Change of Owner | 2016-02-25 | Operator changed from 7578, ENERVEST OPERATING LLC to 9619, PILLAR ENERGY LLC |
| Record Last Modified | 2017-02-15 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| Not Treated | 0 | 0 | 0 | NOT PERFED OR TREATED; PRODUCING OPEN HOLE FROM LOWER HURON SHALE |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2007 | RANGE RESOURCES-APPALACHIA LLC | 920.00 | 0.00 | 183 |
| 2008 | RANGE RESOURCES-APPALACHIA LLC | 988.00 | 0.00 | 304 |
| 2009 | RANGE RESOURCES-APPALACHIA LLC | 699.00 | 0.00 | 365 |
| 2010 | ENERVEST OPERATING LLC | 672.00 | 0.00 | 365 |
| 2011 | ENERVEST OPERATING LLC | 739.00 | 0.00 | 0 |
| 2012 | ENERVEST OPERATING LLC | 730.00 | 0.00 | 366 |
| 2014 | ENERVEST OPERATING LLC | 657.00 | 0.00 | 365 |
| 2015 | ENERVEST OPERATING LLC | 566.00 | 0.00 | 161 |
| 2016 | PILLAR ENERGY LLC | 388.00 | 0.00 | 365 |
| 2017 | PILLAR ENERGY LLC | 561.00 | 0.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2007 | RANGE RESOURCES-APPALACHIA LLC | Brine | 0 | 183 |
| 2008 | RANGE RESOURCES-APPALACHIA LLC | Brine | 0 | 304 |
| 2009 | RANGE RESOURCES-APPALACHIA LLC | Brine | 0 | 365 |
| 2010 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
| 2011 | ENERVEST OPERATING LLC | Brine | 0 | |
| 2012 | ENERVEST OPERATING LLC | Brine | 0 | 366 |
| 2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
| 2014 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
| 2015 | ENERVEST OPERATING LLC | Brine | 0 | 161 |
| 2016 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
| 2017 | PILLAR ENERGY LLC | Brine | 0 | 365 |
| 2018 | ENERVEST OPERATING LLC | Brine | 0 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1040850683 | 2008-2-28 0:00: | PW | No Violations | |
| -1087692684 | 2007-3-21 0:00: | PL | No Violations | |
| -1310043366 | 2009-3-31 0:00: | PW | No Violations | |
| -1424176014 | 2006-9-25 0:00: | DD | No Violations | |
| -1551545387 | 2007-2-15 0:00: | DD | No Violations | |
| -1556203555 | 2009-6-15 0:00: | PL | No Violations | |
| -1743074816 | 2007-8-7 0:00:0 | PL | No Violations | |
| -1767319922 | 2010-1-6 0:00:0 | PL | No Violations | |
| -178362337 | 2009-5-11 0:00: | AM | No Violations | |
| -1980675337 | 2010-1-6 0:00:0 | PL | No Violations | |
| -1981054127 | 2011-3-28 0:00: | PW | No Violations | |
| -2139559202 | 2007-4-17 0:00: | DD | No Violations | |
| -237158589 | 2007-1-18 0:00: | DD | No Violations | |
| -250739941 | 2013-4-2 0:00:0 | UL | No Violations | 1.50 |
| -558502275 | 2007-3-14 0:00: | DD | No Violations | |
| -756018848 | 2010-1-6 0:00:0 | PL | No Violations | |
| 0068540621 | 2013-04-02 | UrbanPreliminary Restoration | No Violations | Accompanied Morgan Button MRI 2 on inspection of the well. Good identification on the access road gate and the well. Well is producing. Good vegetative cover has been established. |
| 0178362337 | 2009-05-11 | Administrative Inspection | No Violations | Called Mark Moody today 5-11-09 at 1:30 pm. I told Mark of the slip and the brine seep. We also discussed the gas leak at the well head. I told Mark of the similar brine leaks on other horizontal wells and asked that the surface casing be exposed. Mark is going to follow up with the field personnel and get back to me. |
| 0237158589 | 2007-01-18 | Drill / Deepen / Reopen | No Violations | Well is leaking gas, Have called company they are aware and have scheduled repair. Pit looks good. Needs pumped soon. Mark Moody (Great Lakes) is going to send an request for extension on leaving pit open for longer than 30 days. They are still planning to drill second well soon. The site is such that closing the pit and digging a new one would be difficult and cause damage to the site. Pit has some good mulch and grass on it now. |
| 0250739941 | 2013-04-02 | UrbanPreliminary Restoration | No Violations | Restoration of site appears to have stabilized since Jon Scotts last inspection. Grass is apparently doing well at this site. Some minor issues are present but nothing to prohibit passage of preliminary urban restoration. There is no tank battery associated with this well. |
| 0521914032 | 2007-04-05 | Preliminary Restoration | No Violations | Dale Ross is connecting the main line to the well. The well is still leaking ( bubbling up around wellhead ) Dale said that he will dig up the cellar after he blows down the well. This will allow a better look at the leak. I told Dale that he needs to drain the standing water on the site and that he must drain it through a straw bale sediment catch. |
| 0558502275 | 2007-03-14 | Drill / Deepen / Reopen | Violations Noted | No effort to comply with NOV # 1551545387. Pit is still full and now the Safety fence is down on 75% of the pit perimeter. A diversion ditch has been dug around the side of the pit to divert surface water away from pit. No erosion controls are in place on the diversion ditch. Pipe line work has been done recently down to the well. I called Mark Moody 11:30 am on 3-16-07 and went over this NOV with him. Mark said that Ross will take care of the pit levels and safety fence. They are going to produce this well and see how it does before any more work is done to the well. Restoration is waiting on dry weather.Mark said that the leak at the well head is coming up from the cement job. Between the 7.5 and the conductor. |
| 0629460069 | 2007-05-23 | Drill / Deepen / Reopen | No Violations | Still pumping down pits. No change to site. No erosion controls have been installed. Safety fence is up around pits. |
| 0756018848 | 2010-01-06 | Preliminary Restoration | No Violations | This is a Horizontal portion of well # 34-087-20649-00-00. All restoration reports and NOVs will be listed under #34-087-20649-00-00. |
| 0800046008 | 2008-01-08 | Production Wells | Violations Noted | Id at well is too small to meet urban requirements. Sign is 11 by 7.25 and the lettering is .5 tall. A 4 line has been connected to the well and a 1.25 yellow plastic line has been ran to the well and not connected. No tracer line or pipe line identification was installed with this 1.25 line. No fencing has been installed at the wellhead. The access road has some small slips beside it that have filled in the diversion ditch and blocked a culvert. This diversion ditch drains a steep section of the road and is critical to the erosion control efforts on this site. The access road has a gate that is locked and has no identification. I am requesting a key to the gate per 1501:9-9-05 (E) (3) |
| 0810323960 | 2009-05-19 | Production Wells | No Violations | Meet with Rick Keplar (Range Resources) and his contractor. The slip has moved since my last inspection. Rick agreed to a 2nd meeting with Lawrence County soil and water to discuss how to fix the slip. Meeting next week. I contacted soil and water they will get back to me on a day next week. |
| 0830090874 | 2009-12-17 | Production Wells | No Violations | Site has started to slip again near the pit location. Good vegetative cover was established prior to the slip. The gravel channel and well are not effected by the slip at the time of inspection. Frozen water was observed at the base of the slip. The access road has a large water bar installed at the top of the steep portion of the road. Took pictures of the slip. |
| 0845679450 | 2007-06-12 | Drill / Deepen / Reopen | No Violations | Dale Ross excavated the cellar around the well head. The gas leak is coming up around the 7 inch. Dave Cumberledge (Great Lakes Southern Area Production Supervisor) Was on site to witness the leak and to come up with a solution to the problem. The pits have been filled in and site has been graded. |
| 0904711070 | 2010-04-08 | Administrative Inspection | No Violations | Ownership change from Range to Enervest. |
| 0996675568 | 2006-10-23 | Drill / Deepen / Reopen | No Violations | Cement in 250 of surface casing. |
| 1003441633 | 2010-01-06 | Preliminary Restoration | No Violations | This is a Horizontal portion of well # 34-087-20649-00-00. All restoration reports and NOVs will be listed under #34-087-20649-00-00. |
| 1040850683 | 2008-02-28 | Production Wells | No Violations | The slip is worse than the last inspection. Trees are down across the road and surface water is flowing down the access road. The slip is starting to impact the hillside. The id has not been posted at the gate. The wellhead still has the small id as described in NOV. A regulator and gas meter have been installed for house gas. This whole assortment of equipment is being supported by an upside down plastic milk crate. |
| 1087692684 | 2007-03-21 | Preliminary Restoration | No Violations | Meeting on site with Greg Mills and Gary Green to evaluate the site and come up with a restoration plan. |
| 1099447627 | 2011-02-08 | Production Wells | No Violations | Slip is holding water at top. Pit location is seeping brine. No change since last inspection. Took pictures. |
| 1160271426 | 2011-09-28 | Production Wells | No Violations | Slip repair. Site has been graded. Good vegetative cover established. 10 by 6 area is bare and deer tracks are all through it. High end Quantab 1616 ppm cl. I called Jim Ross and he is going to repair the bare area. |
| 1161891285 | 2006-10-05 | Drill / Deepen / Reopen | No Violations | Urban Site Review request: Accompanied by Mr. Rick Keppler of Great Lakes Energy, Mr. Steve Kravatts, Target Drilling and Mr. Dale Ross of Ross Construction. Conducted urban site review on the three Dingus wells (50) apart. |
| 1169567790 | 2007-01-22 | Drill / Deepen / Reopen | No Violations | Have received a letter from Great Lakes requesting an extension for closing the pits. They plan to drill 2 more wells on site and want to use the existing pits. This is reasonable because of the location of the site. The pit has some erosion control in place and is completely fenced off. |
| 1178117362 | 2007-05-02 | Drill / Deepen / Reopen | Violations Noted | Dale Ross is pumping the pits down, however there is some pit water that has been pumped into a shallow ditch near the wellhead. This water is the yellow color of the pit water and has some brine in it. The ditch is not lined so the pit water is going into the ground. I called Mark Moody (Great Lakes) and told him what is going on. Mark is going to call Dale Ross. I left a note for Ross on the lease road gate tellig him to pump out the water in the shallow pit and to fill it in now. |
| 1178799566 | 2007-05-08 | Drill / Deepen / Reopen | No Violations | The small unlined pit north of the wellhead has been filled in. One straw bale has been placed on site for sediment control (it is not staked down). Well head is still bubbling a lot looks like boiling water. The drilling pits are still being pumped down. The lease road has some slips along its bank. No id on site. |
| 1182787648 | 2007-06-05 | Drill / Deepen / Reopen | No Violations | Dale Ross is reclaiming the site. Pits are not closed. Plan to solidify pits on the 6-07-07. |
| 1183009061 | 2007-07-18 | Administrative Inspection | No Violations | Called 330-877-6747 at 1:35pm on 7-18-07 and left a voice mail message for Mark Moody ( Great Lakes) I informed him of the errosion on the lease road and the lack of drainage on the flat area around the wellhead. The Run off is causing erosion on the site. |
| 1184173046 | 2007-07-09 | Preliminary Restoration | No Violations | Good vegetative cover on site. Grass is growing. Lease road needs more work done to it. There are not enough ditches to divert the water off of the road. As a result of the water on the road there are channels eroding in the road. There are slips along the road cut that need to be fixed. Silt is building up at bottom of the lease road near the last culvert. The new culvert that was installed on the bend in the road is causing erosion at the point of discharge. The gas leak around the 7 can still be heard and smelled at the well head. A lack of drainage on the site is causing erosion to move off site. The runoff has turned the old logging road into a stream bed. The reclaimed area at the wellhead is 600 feet by 180 feet. This is not including the lease road area. |
| 1212597699 | 2008-04-30 | Production Wells | No Violations | No Urban Id on Access Road Gate. Gate was not locked. I requested a key to the lock and have not received one. The slip on the access road has got worse. Trees are now blocking the access road. This blockage will hinder an Emergency Responder from getting to the wellhead in a timely manner. The diversion ditch is completely filled in. Surface water is eroding the roadway. Wellhead has the same little id. No work has been done since the last inspection. |
| 1219233327 | 2008-07-23 | Production Wells | No Violations | Access road gate has urban identification posted. The slip beside the access road has not been fixed. Access road is blocked with three downed trees from the slip. A new id has been placed at the wellhead this id is small with 1/2 inch lettering. |
| 1233145687 | 2007-06-07 | Drill / Deepen / Reopen | No Violations | Dale Ross is solidifing the pits today. They are using two bulk trucks with dry cement. Ross is mixing the cement into the pits with a track hoe. |
| 1267461014 | 2010-03-01 | Administrative Inspection | No Violations | Called and talked to Rick Kepler (Drilling Supervisor) at 11:27am Re: site has slipped again. I asked for them to formulate a plan to fix the slip and get back to me. Rick said that he will talk to his supervisor and get back to me. I verified that Rick has my phone number. |
| 1298908032 | 2011-01-19 | Production Wells | No Violations | Slip has not been fixed. Still holding water at the top of the slip. New 4 black corrugated drain pipe was installed in ditch with out gravel around it. The 4 drain is not draining water from the site. Pit area is seeping brine. High End quantabs were used 1st in excavated area near pit side read 9 on the strip. 2nd in scald area near wood line read 8 on the strip. Took photos. |
| 1310043366 | 2009-03-31 | Production Wells | No Violations | Access road has been cleared. Slip along access road has been worked on and diversion ditch is now functioning properly. Site needs seed and mulch applied to establish vegetative growth. An Inspection of the wellhead revealed a new slip near the drill pit location. Water is seeping out of the ground at this slip site. Deer tracks and salt smell at seep suggested brine. I tested the water with a High Range Quantab the results were 7.6 on the strip. Which is 4477 ppm Cl. Pieces of black plastic pit liner were exposed due to the slip. A sample of the brine was sent to the Lab. Seep sample site GPS N38.47311 W082.49854. I called and Talked to Mark Moody about the seep and the slip. Mark is going to send field personnel to location. They will call to set up a meeting. Fix slip site and determine where the brine source is. Schedule a meeting in field to discuss plans. |
| 1424176014 | 2006-09-25 | Drill / Deepen / Reopen | No Violations | Checked road work into Dingus well site, fencing at entry to site and site preparation. |
| 1446927371 | 2006-10-18 | Drill / Deepen / Reopen | No Violations | Rig has moved onsite; checked mud pit and site conditions. Mud pit has caved in on two walls and driller is in process of pumping fluid from pit into the frac tank so that the pit may be worked on and a new liner installed. Also introduced new inspector |
| 1540264672 | 2010-06-14 | Production Wells | No Violations | Id is good shows current owner and phone number. Jim Ross has moved a backhoe on location to work on the well head and the drain around the slip. No one on location during inspection. |
| 1551545387 | 2007-02-15 | Drill / Deepen / Reopen | Violations Noted | Well head is still leaking. I called Mark Moody on 1-18-07 about this leak and the fluid levels in the pits. He said that they would get right on it. Nothing has changed. Pit needs pumped and the gas leak needs fixed. |
| 1556203555 | 2009-06-15 | Preliminary Restoration | No Violations | Meet with George Chapman (Contractor for Range). 894-6793. George is installing a gravel drain at the base of the hillside to intercept the water and divert it away from the well site. He has dug a trench with fall and has a layer of gravel then felt then gravel with a 4 PVC pipe in the center. |
| 1743074816 | 2007-08-07 | Preliminary Restoration | No Violations | Good vegetative cover on site. No identification at wellhead or on access road gate. Access road is very steep and does not have proper drainage controls installed to handle the watershed that the access road is exposed to. The diversion ditch needs to extend all the way to the top of the road. A series of water bars need to be installed on the access road to prevent erosion. There are two small subsidence areas on the flat wellhead site. Probably caused by buried trees and debris. Mark Moody told me that Dale Ross and a Great lakes representative would call me about these problems. No one has called as of today. I will call Mark Moody again. |
| 1767319922 | 2010-01-06 | Preliminary Restoration | No Violations | This is a Horizontal portion of well # 34-087-20649-00-00. All restoration reports and NOVs will be listed under #34-087-20649-00-00. |
| 1980675337 | 2010-01-06 | Preliminary Restoration | No Violations | This is a Horizontal portion of well # 34-087-20649-00-00. All restoration reports and NOVs will be listed under #34-087-20649-00-00. |
| 1981054127 | 2011-03-28 | Production Wells | No Violations | Slip inspection with Robert Stonerock ODNR South Region Supervisor, Tim McConaha and Jim Ross from Enervest. Discussed corrective procedures for slip remediation. |
| 2039295135 | 2008-08-13 | Production Wells | No Violations | Good urban id on access road gate. No work has been done to fix the slip or to clear the access road. |
| 2041532467 | 2008-08-25 | Administrative Inspection | No Violations | Received a call from Company that their contractor is moving on location today to fix the slip. |
| 2139559202 | 2007-04-17 | Drill / Deepen / Reopen | No Violations | Well is still leaking. Pit still has water in it. Mark Moody said that they are going to fill in the pit and reclaim the site. They have no plans to drill 2nd hole at this time. Lease rd. is eroding badly. Pit safety fence is down in several places. No sediment controls are in place on site. |
| 521914032 | 2007-4-5 0:00:0 | PL | No Violations | |
| 629460069 | 2007-5-23 0:00: | DD | No Violations | |
| 68540621 | 2013-4-2 0:00:0 | UL | No Violations | 1.00 |
| 800046008 | 2008-1-8 0:00:0 | PW | No Violations | |
| 810323960 | 2009-5-19 0:00: | PW | No Violations | |
| 830090874 | 2009-12-17 0:00 | PW | No Violations | |
| 845679450 | 2007-6-12 0:00: | DD | No Violations | |
| 904711070 | 2010-4-8 0:00:0 | AM | No Violations | |
| 996675568 | 2006-10-23 0:00 | DD | No Violations |
| Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
|---|---|---|---|---|
| 0558502275 | US-OH-126153 | 2007-03-16 | Pit insufficient size to contain oil, brine, cuttings | |
| 0558502275 | US-OH-126154 | 2007-03-16 | General Safety | |
| 0558502275 | US-OH-126155 | 2007-03-16 | Well insufficiently equipped to prevent escape of oil and gas | |
| 0800046008 | US-OH-129095 | 2008-01-24 | Failure to comply with permit conditions | |
| 1178117362 | US-OH-104736 | 2007-05-02 | Drilling operation causing pollution and contamination | |
| 1178117362 | US-OH-104737 | 2007-05-02 | Use of pit for ultimate disposal of brine or other wastes | |
| 1551545387 | US-OH-115069 | 2007-02-16 | Drilling operation causing pollution and contamination | |
| 1551545387 | US-OH-115070 | 2007-02-16 | Pit insufficient size to contain oil, brine, cuttings |
For data sources see[8]