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34-087-20519

Well Details

Well ID: 34-087-20519
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Country: United States
State: Ohio
County: Lawrence
Municipality: Mason Township
Operator Name: PILLAR ENERGY LLC
Well Pad ID:
Farm/Lease Name: HAMM(ERP#1)
License Status: Active Injection
License Date: 2010-06-17
Spud Date: 2001-05-10
Spud Drilling Contractor: CENTURY WELL SERVICES,INC
Final Drill Date: 2001-05-11
Well Total Depth: 980.00 ft
Configuration: Vertical
Latitude: 38.630000
Longitude: -82.430000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2001-04-06 3793 ENERGY SEARCH INC Proposed Formation COW RUN Issued Date 4/6/01 Expired Date 4/6/02 6:00:00 AM
Original Spud 2001-05-10 RBDMS Rec
Completed 2001-05-11 RBDMS Rec
Reached Total Depth 2001-05-11 RBDMS Rec
Completion Report Received 2001-09-07 RBDMS Rec
Change of Owner 2008-02-26 Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2010-06-17 Proposed Formations:COW RUN, Issued Date:6/17/2010, Expired Date:6/17/2011 6:00:00 AM, Drilling unit acres:119.74, Proposed Well Type:EOR, Proposed Well Class:ERP
Construction Permit Expires 2011-06-17 RBDMS Rec
Last Compliance Report 2014-12-15 RBDMS Rec
Change of Owner 2016-02-24 Operator changed from 7578, ENERVEST OPERATING LLC to 9619, PILLAR ENERGY LLC
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2001-10-26 837 845 32
837 845 32
837 845 32

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 202 Bbl 7000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2001 ENERGY SEARCH INC 0.00 402.00 365
2002 ENERGY SEARCH INC 0.00 414.00 365
2003 ENERGY SEARCH INC 0.00 312.00 365
2004 ENERGY SEARCH INC 0.00 302.00 365
2005 ENERGY SEARCH INC 0.00 337.00 365
2006 ENERGY SEARCH INC 0.00 313.00 365
2007 ENERGY SEARCH INC 0.00 200.00 365
2008 EXCO - NORTH COAST ENERGY INC 0.00 69.00 366
2009 ENERVEST OPERATING LLC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 139.00 365
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 43
2016 PILLAR ENERGY LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2001 ENERGY SEARCH INC Brine 0 365
2002 ENERGY SEARCH INC Brine 365
2003 ENERGY SEARCH INC Brine 365
2004 ENERGY SEARCH INC Brine 0 365
2005 ENERGY SEARCH INC Brine 0 365
2006 ENERGY SEARCH INC Brine 170 365
2007 ENERGY SEARCH INC Brine 124 365
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 549 365
2010 ENERVEST OPERATING LLC Brine 109 365
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 43
2016 ENERVEST OPERATING LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1120600324 2014-6-12 0:00: ER No Violations 1.00
-1161297308 2018-10-23 0:00 ER No Violations 1.00
-1195342575 2011-12-9 0:00: ER No Violations
-1226022987 2015-4-22 0:00: ER No Violations 2.30
-1279307198 2020-7-20 0:00: ER No Violations 0.90
-1515880602 2016-1-7 0:00:0 ER No Violations 1.00
-1547047615 2017-6-28 0:00: SW No Violations 1.00
-1755582283 2016-3-30 0:00: ER No Violations 1.00
-1845558468 2019-6-11 0:00: ER No Violations 1.80
-1946910483 2013-10-21 0:00 ER No Violations 0.70
-2050518563 2014-11-20 0:00 ER No Violations 0.50
-226525041 2013-10-21 0:00 AM No Violations 0.10
-287679208 2012-4-5 0:00:0 ER No Violations
-300332356 2012-10-3 0:00: ER No Violations 0.50
-326646634 2019-2-14 0:00: ER No Violations 1.50
-356561039 2004-3-2 0:00:0 PW No Violations
-417238383 2013-12-11 0:00 SC No Violations 2.00
-515688978 2015-10-7 0:00: ER No Violations 1.00
-529162417 2018-6-8 0:00:0 ER No Violations 1.50
-626838114 2016-6-8 0:00:0 ER No Violations 1.00
-652216596 2015-6-16 0:00: ER No Violations 1.50
-676747905 2013-1-3 0:00:0 ER No Violations 1.50
-720113668 2013-1-7 0:00:0 SC No Violations 2.50
-730795559 2013-1-3 0:00:0 ER No Violations 0.70
-807684746 2011-4-1 0:00:0 ER No Violations
-900786011 2010-10-12 0:00 ER No Violations
-920459490 2019-9-4 0:00:0 ER No Violations 1.10
-998764818 2013-7-15 0:00: ER No Violations 0.50
001269i504 2001-11-08 Production Wells No Violations No violations.
0106430752 2012-09-17 Enhanced Recovery Project No Violations Random Brine sample taken from 210 barrel storage tank. Jim Ross was on site. Brine sample sent to ODNR Lab.
0189012662 2013-09-24 Administrative Inspection No Violations Jim Ross (Enervest contractor) told me that they had observed communication on the annulus pressure. They have shut in the well until a service rig can be scheduled to work on the well.
0226525041 2013-10-21 Administrative Inspection No Violations Called and talked to Jim Ross and Tim McConaha. They are scheduling a rig to work on the packer and tubing.
0287679208 2012-04-05 Enhanced Recovery Project No Violations Good Identification.
0300332356 2012-10-03 Enhanced Recovery Project No Violations Inspected injection pressure and annulus pressure. Good identification on wellhead. 1/4 ball valve needs to be replaced. Valve body is cracked.
0302048587 2010-09-13 Enhanced Recovery Project No Violations Convert to ERP. Tested multiple times and was not able to get annulus to pass test. Will reset packer and test 9-14-10.
0326646634 2019-02-14 Enhanced Recovery Project No Violations Inspected the containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification is posted at the well. The containment dike is free of fluids.
0334082096 2010-09-14 Enhanced Recovery Project No Violations Released packer and pulled up 1 foot. Reset packer and pulled 25,000 lbs. Tested annulus at 400 psi. After 15 minutes at 398 psi. good test.
0356561039 2004-03-02 Production Wells No Violations No problem observed.
0417238383 2013-12-11 Surface Facility Construction No Violations Inspected the changes that have been made to the pump house injection line manifolds and the change over to a different injection pump. Inspected the unloading pad, containment dike and tanks.
0481225841 2018-03-19 Salt Water Injection Well No Violations I was on location today to check the pressures of this salt water injection well. The annulus pressure was 42 psi, the injection tubing pressure was 81 psi. No violations were noted during my inspection.
0515688978 2015-10-07 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well.
0529162417 2018-06-08 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification is posted at the well. The containment dike is free of fluids.
0534711781 2011-08-02 Enhanced Recovery Project No Violations Good identification. No violations observed during inspection.
0575829873 2016-08-25 Enhanced Recovery Project No Violations Inspected the containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well.
0599996806 2013-10-21 Enhanced Recovery Project Violations Noted Inspected the unloading pad, containment dike, tanks, annulus pressure, and injection pressure. Containment dike is free of water. Good identification at the well head. Injection tubing and annulus are on vacuum. Well is shut in (master valve and injection line valve are closed)
0612636605 2014-02-19 Enhanced Recovery Project No Violations Injection line is disconnected from the injection tubing. Plugs have been placed in both open ends. The well is not capable of injection at this time. I talked to Jim Ross (Enervest contractor) and he told me that Enervest is looking at converting this well back to a production well. He was not able to give me a time table as to when service could be done to the well.
0626838114 2016-06-08 Enhanced Recovery Project No Violations Inspected the injection pressure, annulus pressure, unloading pad, containment dike, tanks, and injection pump. Ezra Schoolcraft and Bo Pinkerman are in the ERP field replacing identifications on the wells today. I talked to Ezra about the need to grade the access roads to prevent erosion. We discussed the need for controlling the runoff with diversion ditches and water bars.
0652216596 2015-06-16 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, pump house, injection pressure and annulus pressure. Good identification posted at the well. The injection line manifold has been shut off due to repairs in the line to the Hamm # 5 ERP well.
0676747905 2013-01-03 Enhanced Recovery Project No Violations Continued bimonthly inspection and monitoring injection and annulus pressures on ERP wells in Enervests Greasy Ridge Field with Jon Scott.
0720113668 2013-01-07 Surface Facility Construction No Violations Concrete dike pad has been poured. Concrete block and mortar is on site. Extended concrete apron to unloading pad.
0723864271 2014-02-19 Enhanced Recovery Project No Violations Conducted bimonthly inspection on injection wells with Jon Scott. The wellhead and identification sign is in good shape. The wells injection line was disconnected to insure the well will not be used as an injection well until its packer is repaired or replaced and a MIT is performed on the well. The repair will be performed this spring. In the meantime this well is shut in.
0730795559 2013-01-03 Enhanced Recovery Project No Violations Inspected enhanced recovery well injection tubing pressure and annulus pressure. Good identification at well head. Accompanied by Morgan Button MRI 2.
0807684746 2011-04-01 Enhanced Recovery Project No Violations Corrosion inhibiter and water on the ground at wellhead. Appears that a 1/4 ball valve has frozen and caused the loss in pressure. A new valve has been installed and annulus had 178 psi. I talked to Jim Ross and he is going to clean up the well site.
0886196344 2012-04-05 Enhanced Recovery Project No Violations No violations at the time of inspection.
0900786011 2010-10-12 Enhanced Recovery Project No Violations ERP well conversion line test. Tested line from where it tied into the manifold line. New line is isolatable by a new ball valve. Ball valve was shut and the injection tubing was shut. Line was full of fluid and was tested at 258 psi. after 5 minutes 252 psi, after 15 minutes 248 psi. New line is 2 black plastic SDR 7. Line is buried.
0998764818 2013-07-15 Enhanced Recovery Project No Violations Inspected injection pressure, annulus pressure, Containment dike, tanks, pump, and unloading pad. Good identification.
106430752 2012-9-17 0:00: ER No Violations 3.00
1120600324 2014-06-12 Enhanced Recovery Project No Violations Inspected injection pressure, annulus pressure and walked the pipe line right of way. Good identification at the well.
1123713236 2013-09-05 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, annulus pressure, and injection pressure. Containment dike is free of water. Good identification at the wellhead.
1161297308 2018-10-23 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well. The containment dike is free of fluids.
1195342575 2011-12-09 Enhanced Recovery Project No Violations No violations observed during inspection.
1226022987 2015-04-22 Enhanced Recovery Project No Violations No noted violations.
1269i504 2001-11-8 0:00: PW No Violations
1276702900 2010-06-04 Enhanced Recovery Project No Violations Received memo requesting site evaluation for conversion to ERP from Tom Tomastik UIC Geologist. Well is located on a wooded hillside. Well is 553 feet from an intermittent stream that flows to Buckeye Creek. A search of the ground water well data base with a 1/2 mile radius listed no water wells with in 1/2 mile of proposed ERP conversion well. Well is currently equipped with tubing, rods, pump jack, electric service and electric motor. Well is connected to production line. Id has not been updated from North coast to Enervest at the time of inspection. A 3 foot by 3 foot by 2 foot deep hole was excavated beside the well to expose the casing annulus.
1363724945 2004-03-02 Preliminary Restoration No Violations Passed.
1366805482 2012-10-03 Enhanced Recovery Project No Violations Inspected wells with Jon Scott. Measured Injection and Annulus pressure for wells in this field. Well ID was good. The 1/4-inch ball valve on the injection tubing needs to be replaced, The valve is cracked and leaks. Discussed the leaking valve found during our inspection and measurement of pressures with Jim Ross, Contract Operator for this field.
1368209055 2013-05-03 Enhanced Recovery Project No Violations Inspected the injection pressure, annulus pressure. Good identification. Access road has been graded.
1380801348 2013-09-26 Enhanced Recovery Project No Violations Inspected the injection pressure and the annulus pressure. I received notification from Jim Ross (Enervest contractor) that they observed communication with the annulus and injection tubing on 9-24-13. Jim shut the injection valve and the master valve on the wellhead. The well was shut in and not injecting during the inspection. The tubing and annulus were equalized at 24 psi. I talked to Jim and he told me they are scheduling a rig as soon as possible.
1386868896 2013-12-11 Enhanced Recovery Project No Violations Well is shut in. Injection line valve is closed. Currently scheduling a service rig.
1389617210 2014-01-10 Enhanced Recovery Project No Violations Well is shut in with injection line valve closed. Annulus and injection tubing had slight vacuum. Talked to well tenders and service rig crew from Berry Well service. The service rig is in the area. They plan to come to work on the packer after plugging two wells.
1395337652 2014-03-20 Enhanced Recovery Project No Violations Test annulus. Annulus tested at 300 psi, at 5 minutes 298 psi, at 15 minutes 294 psi. Injection line has been connected to the injection tubing. Inspected annulus pressure (after test the annulus pressure was reduced to 90psi), injection pressure, injection line, containment dike, tanks, and injection pump.
1416949735 2014-11-25 Enhanced Recovery Project No Violations Service rig released packer (pulled 30,000 lbs.) Pulled tubing and packer out of well. Packer element was damaged and it was decided to replace the packer. The well is currently shut in with a closed valve while a packer is located.
1418666743 2014-12-15 Enhanced Recovery Project No Violations Installed 805.50 feet of used tubing with a new Parmaco Packer (5.2 feet). Packer is set at 810.70 feet. Pulled 6000 lbs. over tubing string weight to set packer. Filled annulus with 8.75 barrels fresh water and one gallon inhibitor. Tested annulus at 370 psi for 15 minutes with a loss of 2 psi. Annulus pressure at 15 minutes 368 psi.
1515880602 2016-01-07 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification posted at the well.
1547047615 2017-06-28 Salt Water Injection Well No Violations Salt water injection well inspection. The annulus pressure was 21 psi, the injection tubing pressure was 42 psi. No violations were noted during my inspection.
1559416542 2018-09-04 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pressure and annulus pressure. Identification is posted at the well. The containment dike is free of fluids.
1598755325 2013-03-14 Enhanced Recovery Project No Violations Inspected injection pressure and annulus pressure. Good identification at wellhead.
1625223055 2014-08-19 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pump, walked the injection line, checked the injection pressure and annulus pressure. Good identification at wellhead.
1719419871 2010-09-08 Enhanced Recovery Project No Violations Conversion to ERP. Set packer at789.90. Pulled 25000 lbs on tubing. Test did not pass. Possible too much air in annulus. Let set for few days then re-test.
1755582283 2016-03-30 Enhanced Recovery Project No Violations Inspected the unloading pad, containment dike, tanks, injection pump, injection pressure and annulus pressure. Identification has not been changed from Enervest to Pillar Energy.
1765838814 2010-12-29 Enhanced Recovery Project No Violations Converted to ERP well. No identification posted. I talked to Jim Ross and he has the blank Ids and is in the process of filling in the information for the entire ERP field.
1768327945 2019-10-15 0:00 ER No Violations 0.40
189012662 2013-9-24 0:00: AM No Violations
1946910483 2013-10-21 Enhanced Recovery Project No Violations FOLLOW UP TO NOV # 599996806 Inspected the unloading pad, containment dike, tanks, annulus pressure, and injection pressure. Containment dike is free of water. Good identification at the well head. Injection tubing and annulus are on vacuum. Well is shut in (master valve and injection line valve are closed)
2050518563 2014-11-20 Enhanced Recovery Project No Violations Well is shut in waiting on service rig to release packer and pull packer and tubing.
302048587 2010-9-13 0:00: ER No Violations 4.00
334082096 2010-9-14 0:00: ER No Violations 2.00
481225841 2018-3-19 0:00: SW No Violations 0.30
534711781 2011-8-2 0:00:0 ER No Violations
575829873 2016-8-25 0:00: ER No Violations 0.70
599996806 2013-10-21 0:00 ER No Violations 0.70
612636605 2014-2-19 0:00: ER No Violations 0.70
723864271 2014-2-19 0:00: ER No Violations 0.70
791090606 2020-6-17 0:00: ER No Violations 0.50
878959727 2020-1-21 0:00: ER No Violations 1.00
886196344 2012-4-5 0:00:0 ER No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0599996806 US-OH-126774 2014-04-10 Mechanical failure/contamination

For data sources see[9]

References