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34-087-20262

Well Details

Well ID: 34-087-20262
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Country: United States
State: Ohio
County: Lawrence
Municipality: Hamilton Township
Operator Name: ORPHAN WELL PROGRAM
Well Pad ID:
Farm/Lease Name: UNITED STATES OF AMERICA
License Status: Final Restoration
License Date: 2012-02-13
Spud Date: 1979-01-10
Spud Drilling Contractor:
Final Drill Date: 1979-02-19
Well Total Depth: 2970.00 ft
Configuration: Vertical
Latitude: 38.570000
Longitude: -82.710000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-12-06 155 PIN OAK PETROLEUM INC GeoDate 12/6/78
Unknown 1978-12-06 Issued Date 12/6/78 Expired Date 12/6/79 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1979-01-10 SENT TO FIELD FOR ORPHAN WELL REFERRAL 3/24/05. R.L. 1-3-79 PF=SILT.
Completed 1979-02-19 SENT TO FIELD FOR ORPHAN WELL REFERRAL 3/24/05. R.L. 1-3-79 PF=SILT.
Reached Total Depth 1979-02-19 SENT TO FIELD FOR ORPHAN WELL REFERRAL 3/24/05. R.L. 1-3-79 PF=SILT.
APP 2012-02-13 Proposed Formations:CLINTON/MEDINA, Issued Date:2/13/2012, Expired Date:2/12/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2012-03-13 Plugged by Orphan Well Program
Plugged/Abandoned 2012-03-13 SENT TO FIELD FOR ORPHAN WELL REFERRAL 3/24/05. R.L. 1-3-79 PF=SILT.
Record Last Modified 2013-03-14 SENT TO FIELD FOR ORPHAN WELL REFERRAL 3/24/05. R.L. 1-3-79 PF=SILT.
Construction Permit Expires 2014-02-12 SENT TO FIELD FOR ORPHAN WELL REFERRAL 3/24/05. R.L. 1-3-79 PF=SILT.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1294 1295 4
1294 1295 4
1294 1295 4

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1270535467 2012-4-5 0:00:0 PB No Violations
-1334490529 2012-3-6 0:00:0 PB No Violations
-1391594572 2010-8-30 0:00: OR No Violations 3.00
-1436497497 2012-2-28 0:00: PB No Violations
-1542938037 2012-5-10 0:00: FR No Violations
-1555048930 2009-3-3 0:00:0 OR No Violations
-2030054491 2012-3-9 0:00:0 PB No Violations
-216798928 2012-5-17 0:00: FR No Violations
-990303667 2003-12-11 0:00 PW No Violations
0056521218 2012-03-13 Plug / Plug Back No Violations Cement plug is at the surface. Barry Bowers is rigging down and moving equipment off location. Excavated casing and cut off casing at 30 inches below grade. Installed monument with permit number. Filled in excavation. Graded location and applied grass seed.
0203274505 2012-03-06 Administrative Inspection No Violations Barry Bowers called and said they are at 1485 feet. He said that it drilled solid for 50 feet then washed fine clay then was free. He hit solid again at 1480 feet.
0216798928 2012-05-17 Final Restoration No Violations Received waiver form for the roadway being not reclaimed.
0297529341 2012-02-13 Plug / Plug Back No Violations Wayne National Forest Idle and Orphan plugging project. Review access to well with Barry Bowers (contractor).
0990303667 2003-12-11 Production Wells No Violations Well was found incapable of production. Well was equipped with 8 and 4 1/2 inch casings, swage and valve. No other production equipment present.

Well Lat & Long update.

1270535467 2012-04-05 Plug / Plug Back No Violations Grass is growing. Needs to continue to germinate to achieve good vegetative cover.
1285072154 2010-05-17 Orphan No Violations Orphan well inspection. I took Scott Means USFS to well site. Well is leaking small amount gas from slips. Well tubing has a bullet hole below the valve. Took pictures.
1331169529 2012-03-07 Plug / Plug Back No Violations Witnessed bottom hole plug. Bottom plug set at 1525 with 47 sacks through tubing . Production casing shot at 958 feet.
1334490529 2012-03-06 Plug / Plug Back No Violations 5.5 inch casing set at 1484. Drilled to 50 feet below 5.5 inch casing at 1535 feet still drilling cement. Drilling with 4.75 inch bit. Circulate hole with fresh water.
1391594572 2010-08-30 Orphan No Violations Orphan well referral follow up inspection. USFS has installed orange safety fence around wellhead with 3 metal posts set in a triangle. Well has been marked with red marking tape. Slight gas leak was observed at base of wellhead. No gas was observed coming out of the bullet hole in the 2 tubing. Took pictures of the well site and the access road. 15-20 trees will need to be cut down to allow access to the well along the current ORV trail. Tree size ranges from 2 to 12 in diameter.
1436497497 2012-02-28 Plug / Plug Back No Violations Barry Bowers (Orphan well contractor) hit an obstruction at 1261 feet.
1542938037 2012-05-10 Final Restoration No Violations Final restoration inspection with Scott Means USFS. Good vegetative cover. No erosion. Well site and access road are part of the USFS Hanging Rock ORV Trail system. A waiver form was requested due to the roadway being left and not reclaimed.
1555048930 2009-03-03 Orphan No Violations Received request for inspection on 2-25-09 regarding the status of this well from Rich Jones, Lands Program Manager USFS Ironton Office. Wellhead is located at an intersection of ORV trails at the Hanging Rock Trailhead. Well is idle. Well is not connected to production equipment or lines. Wellhead consists of 8 5/8 inch surface casing, 5 1/2 inch production casing with a swedge to 2 inch with a 2 inch valve attached. 2 inch valve is closed. Wellhead has been damaged and the top of the swedge is bent. The 2 inch coupling on top of the swedge is starting to break due to the damage. No gas leaks were detected at the time of inspection. A review of the scanned images for this well revealed that the well has been plugged back on 1-10-1979 to the top of the Big Lime. Pictures were taken.
1647275188 2012-03-07 Plug / Plug Back No Violations Plug through tubing ran to 1525 feet. Circulated water prior to pumping cement. Pumped 5 sacks then had problems with water jet. Had to circulate cement back out of well. Repaired water jet. Achieved good circulation and pumped plug 45 sacks. Pulled 1.5 inch tubing. Appalachian Well Survey ran a wire line bond log looking for free point on 5.5 inch casing. Casing free at 990 feet. Used casing cutter at 958 feet. Casing is free.
1843426989 2012-04-30 Final Restoration No Violations Well site and access road are part of the Wayne National Forest Off Road Vehicle trails. Site has good vegetative cover except on trail (which is in use). Contacted Rich Jones Re: Landowner Waiver for the road being left in place.
2030054491 2012-03-09 Plug / Plug Back No Violations Big Injun plug 874 feet to 724 feet. Load hole with gel prior to pumping cement. Ran tubing to 874 feet. Achieved circulation prior to pumping cement plug 43 sacks. Pulled 7 joints tubing for bottom of surface casing plug 641 feet to 441 62 sacks cement. Good circulation during plug. Pull 16 joints tubing for 100 foot to surface plug, 33 sacks cement. Circulated prior to pumping cement. Good cement at surface.
203274505 2012-3-6 0:00:0 AM No Violations
2121009704 2012-03-05 Plug / Plug Back No Violations Drilling out obstruction today. Cement returns at surface.
297529341 2012-2-13 0:00: PB No Violations
56521218 2012-3-13 0:00: PB No Violations

For data sources see[4]

References