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34-087-20206

Well Details

Well ID: 34-087-20206
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Country: United States
State: Ohio
County: Lawrence
Municipality: Windsor Township
Operator Name: EQUITY OIL & GAS FUNDS INC
Well Pad ID:
Farm/Lease Name: BUCKLEW FARM
License Status: Final Restoration
License Date: 2009-05-06
Spud Date: 2009-09-17
Spud Drilling Contractor:
Final Drill Date: 1968-03-08
Well Total Depth: 3490.00 ft
Configuration: Vertical
Latitude: 38.560000
Longitude: -82.480000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1968-01-02
Completed 1968-03-08
Reached Total Depth 1968-03-08
CO 1989-07-14 25 HOLROYD PRODUCTION CO GeoDate 7/14/89
Unknown 1989-07-14 Issued Date 7/14/89 Expired Date 7/14/90 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
Change of Owner 2001-03-30 Operator changed from 25, HOLROYD PRODUCTION CO to 2657, G/G&W PLASTIC WINEBRENNER, GRE
Change of Owner 2001-10-22 Operator changed from 2657, G/G&W PLASTIC WINEBRENNER, GRE to 516, MURPHY OIL CO
Change of Owner 2009-02-12 Operator changed from 516, MURPHY OIL CO to 1171, EQUITY OIL & GAS FUNDS IN
APP 2009-05-06 Proposed Formations:CLINTON, Issued Date:5/6/2009, Expired Date:5/6/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2009-09-29
Construction Permit Expires 2010-05-06
Record Last Modified 2015-09-24

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-116531345 2009-9-22 0:00: PB No Violations
-1179704353 2007-7-18 0:00: AM No Violations
-1438869994 2006-1-27 0:00: PW No Violations
-1472342804 2007-9-12 0:00: AM No Violations
-1530333138 2009-9-17 0:00: PB No Violations
-1612389942 2007-7-13 0:00: AM No Violations
-1726523897 2007-7-10 0:00: AM No Violations
-2072987963 2009-9-28 0:00: PB No Violations
-293415005 2007-8-21 0:00: PW No Violations
-31373732 2009-11-4 0:00: FR No Violations
-453435440 2006-1-27 0:00: PW No Violations
-458756012 2009-9-24 0:00: PB No Violations
-717012640 2009-2-10 0:00: PW No Violations
-845116638 2008-8-18 0:00: PW No Violations
-926806558 2008-12-29 0:00 PW No Violations
0031373732 2009-11-04 Final Restoration No Violations Pit is filled in. Site graded. Seed and mulch applied. Vegetative growth is starting.
0114113799 2009-12-17 Final Restoration No Violations Good vegetative cover growing. No production equipment or lines on location. No violations observed during inspection.
0116531345 2009-09-22 Plug / Plug Back No Violations Rig pulled on 4.5 casing and it parted at 5 down hole. Directly above a collar. Rig down and move to # 207 while they excavate around 10 and cut off 10 to expose 4.5 collar.
0293415005 2007-08-21 Production Wells No Violations Well is disconnected and idle. No work has been done to the well.
0432323847 2007-04-17 Production Wells Violations Noted Well is idle. Well is not connected to any production equipment or pipe line. Id is fadded no emergency company phone numbers.
0453435440 2006-01-27 Production Wells Violations Noted Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head.
0458756012 2009-09-24 Plug / Plug Back No Violations Rip 4.5 casing at 1918 Casing not free, Run tubing to 1918. Pump cement plug from 1918 to 1718. Unable to circulate. Plug pumped through tubing. Wait and tag TOC plug before continuing.
0608509602 2009-09-29 Plug / Plug Back No Violations Tried to pump on 4.5 it locked up. 4.5 full of water. Pressured up to 800psi. Ran tools down inside 4.5 tools sat down at 490. Pulling all 4.5 out of hole. Then run tubing back down. 5 joints of 4.5 have cement in them. Tubing ran to 700 and tag TOC plug. Pump gel and circulate to surface. Pump 300 plug pull tubing to 400 circulate hole to surface. Pump another 300 plug. Pull tubing to 100 circulate to surface. Pump 100 to surface. Top off with cement hose. Cement stayed at surface.
0717012640 2009-02-10 Production Wells No Violations Craig Ross has his swab rig on the well and they are swabbing now. They are making a lot of water. John Murphy (Well owner) has not decided if going to plug or produce the well.
0823393498 2014-12-31 Preliminary Restoration No Violations Preliminary restoration requirements met.
0845116638 2008-08-18 Production Wells No Violations I showed Craig Ross (contractor for Murphy Oil) the location of the well and discussed the NOV and that they need to get a correct id on the well and then the well needs to be capable of production or plugged. The well is not connected to any lines. No lines have been ran to the well. The valves are corroded shut. A small amount of gas is leaking from the well. The well is located in a hay field and has easy access from the road.
0926806558 2008-12-29 Production Wells No Violations No identification. Wellhead is disconnected. 4 casing has a valve that is closed but leaking a small amount of gas through the valve. No pipe line or production equipment is on location. The well is located off a township road and is in a hay field.
114113799 2009-12-17 0:00 FR No Violations
1179704353 2007-07-18 Administrative Inspection No Violations I talked to John Murphy at 740-215-1011 at 1:00 pm on 7-18-07 about this wells status. John said that he sent a letter asking for an extension on the NOV to Joe Hoerst. John said that it is not cost effective to produce the well due to the low price that he is getting for gas right now. He also stated that it is hard to get a rig down there. I told John that I will follow up with Joe to see what action is taken.
1199897804 2008-01-08 Production Wells No Violations Well is disconnected and idle. No production equipment is on site. The only work that has been done is the clearing of the brush around the wellhead. Well is leaking a small amount of gas. The Id is damaged and was face down in the mud. I moved the Id.
1238598205 2009-02-26 Production Wells No Violations Well has been swabbed by Craig Ross. Well is being monitored at this time.
1242061032 2009-05-11 Administrative Inspection No Violations Talked to John Murphy 12:42pm. I informed him that the plug permit has been issued. John told me that they are writing a letter to outline the plug plans. He also said that they want to wait until July and plug 4 or 5 wells in Lawrence County. I told John to submit a written plan this week.
1260362792 2009-09-09 Administrative Inspection No Violations I talked to John Murphy (Equity Oil & Gas) and he informed me that Knox will be moving a plug rig in this week. He wanted to review the plug depths and methods to plug with cement. He asked that I coordinate with Bill Mitton (Knox). I told John that would be fine.
1260374937 2009-09-18 Plug / Plug Back No Violations Run tubing to 2650. Fluid at approximately 800. Attempted to circulate water using 1/2 bag flake (12.5 lbs). Pumped a total of 86 bbls fluid. LCM material mixed with the 86bbls is 1.5 bags cotton seed hulls (45lbs each bag), 1 gallon polymer, 20 lbs flake (Total including the 12.5 lbs mentioned ) Did not achieve circulation. Water truck had mechanical problems had to be repaired on site. After repairs another 68 bbls was pumped in effort to achieve circulation. John Murphy decided to pump cement plug. Pumped 500 cement plug from 2650 to 2150. After plug pumped tubing was pulled. Fluid level could be seen on tubing at 460.
1438869994 2006-01-27 Production Wells Violations Noted FOLLOW UP TO NOV # -453435440 Has good ID; well is shut-off; pumper stated that cannot control water inflow into well; need to clear multi-flora from around well head.
1472342804 2007-09-12 Administrative Inspection No Violations Called and left a message for John Murphy Re: Well is disconnected and idle. No work has been done to the well. I asked for a update on the well status and asked for a return phone call.
1530333138 2009-09-17 Plug / Plug Back No Violations Knox plug rig moving on location from #207. Ran tools to 2758.
1612389942 2007-07-13 Administrative Inspection No Violations I called John Murphy 740-215-1011 on 7-13-07 at 7:58am and left a voice mail about his NOVs for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged.
1726523897 2007-07-10 Administrative Inspection No Violations I called John Murphy 740-215-1011 on 7-10-07 at 1:14pm and left a voice mail about his NOVs for #294, #207, #206. All three wells are disconnected from any pipe lines and are idle. I wanted to check their status as far as a time line for getting the wells back capable of production or plugged.
1858224102 2009-09-21 Plug / Plug Back No Violations TD TOC plug at 2450. Pumped cement plug from 2450 to 2150 used 28 sacks cement. Brian Jasper (Formation Cementing) pumped the plug. I was unable to witness the plug. I arrived on location after plug set and tubing pulled. Brian did not give me a cement ticket. He told me that he wants to add it to the next days ticket.
2016145019 2009-09-30 Plug / Plug Back No Violations Measure TOC plug at 20. Top off with sack cement.
2064754156 2009-01-14 Administrative Inspection No Violations Talked to Craig Ross (Contractor) he is going to the well today to test for pressure and to look at the well. He told me that he will have his rig on location in 2 weeks to start swabbing and evaluating the well.
2072987963 2009-09-28 Plug / Plug Back No Violations Run tubing back to 1918. Cement plug fell. Was able to achieve circulation to the surface. On both the inside and outside of the 4.5 casing. A piece of wooden 4 by 4 by 24 was circulated to the surface from the backside of the 4.5 casing along with some oil and water. Pumped cement plug from 1918 to 1500. Rip 4.5 at 1480. Pull 2 joints, pump gel spacer and circulate. Then pull 1 joint and circulate to surface. Pump a 600 plug. Pull 10 joints to clear cement and then pull 3 more and shut down. Haul 1 load pit water to injection well.
432323847 2007-4-17 0:00: PW No Violations
608509602 2009-9-29 0:00: PB No Violations
823393498 2014-12-31 0:00 PL No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0432323847 US-OH-124628 2007-04-20 Well shall be plugged
0453435440 US-OH-124911 2006-01-31 Well shall be plugged
1438869994 US-OH-112795 2006-01-31 Well shall be plugged

For data sources see[3]

References