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34-083-22279

Well Details

Well ID: 34-083-22279
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Country: United States
State: Ohio
County: Knox
Municipality: Jackson Township
Operator Name: DUGAN GUY E
Well Pad ID:
Farm/Lease Name: MCDONALD WILBUR
License Status: Final Restoration
License Date: 2010-07-13
Spud Date: 1976-06-16
Spud Drilling Contractor: DON MCKEE DRLG
Final Drill Date: 1976-07-08
Well Total Depth: 2875.00 ft
Configuration: Vertical
Latitude: 40.270000
Longitude: -82.280000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-06-16
Completed 1976-07-08
Reached Total Depth 1976-07-08
CO 1980-07-29 757 McDONALD WILBUR H GeoDate 7/29/80
Oil and Gas 1980-07-29 Issued Date 7/29/80 Expired Date 7/29/81 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
CO 1984-08-22 5034 TAYLOR DALLAS A JR GeoDate 7/29/80
Change of Owner 2002-01-17 Operator changed from 5034, TAYLOR DALLAS A JR to 882, DUGAN GUY E
APP 2010-07-13 Proposed Formations:CLINTON, Issued Date:7/13/2010, Expired Date:7/12/2012 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2012-05-15
Construction Permit Expires 2012-07-12
Record Last Modified 2017-02-15

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1700 Bbl 20000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2001 DUGAN GUY E 0.00 75.00 60
2002 DUGAN GUY E 0.00 0.00 156
2003 DUGAN GUY E 0.00 101.00 156
2004 DUGAN GUY E 0.00 108.00 156
2005 DUGAN GUY E 0.00 0.00 260
2006 DUGAN GUY E 0.00 0.00 260
2007 DUGAN GUY E 0.00 0.00 260
2008 DUGAN GUY E 0.00 0.00 156
2009 DUGAN GUY E 0.00 0.00 260
2010 DUGAN GUY E 0.00 0.00 104
2011 DUGAN GUY E 0.00 0.00 104
2012 DUGAN GUY E 0.00 0.00 260

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2001 DUGAN GUY E Brine 0 60
2002 DUGAN GUY E Brine 0 156
2003 DUGAN GUY E Brine 25 156
2004 DUGAN GUY E Brine 0 156
2005 DUGAN GUY E Brine 30 260
2006 DUGAN GUY E Brine 0 260
2007 DUGAN GUY E Brine 60 260
2008 DUGAN GUY E Brine 0 156
2009 DUGAN GUY E Brine 0 260
2010 DUGAN GUY E Brine 30 104
2011 DUGAN GUY E Brine 0 104
2012 DUGAN GUY E Brine 0 260

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1262530449 2012-5-15 0:00: PW No Violations
-660284028 2012-5-15 0:00: PW No Violations
0168237122 2015-04-10 Final Restoration No Violations This area is an established pasture field with vegetation growing no sigh of a well being here .
0660284028 2012-05-15 Production Wells No Violations I arrived at the well at 4:45 PM. I was informed by Gene Matheny that all of the 8 surface casing was removed. Clay was washed in from the 7 seat to the surface. During the inspection Gene was grading the surface with a dozer.
1262530449 2012-05-15 Production Wells No Violations I arrived at the well at approximately 8:45 AM. During this inspection I was informed that the pre-cast plug was dropped on the 7 seat at approximately 873 feet that morning. Gene Matheny was in the process of hauling clay for the surface plug.
1337201817 2012-05-14 Production Wells No Violations Today I witnessed plugging operations as Gene Matheny set a bottom plug with prepared clay. Approximately 8 tons of clay was washed on bottom and the 5.5 production casing was ripped at approximately 2449.
168237122 2015-4-10 0:00: FR No Violations

For data sources see[8]

References