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| Well ID: 34-083-20788 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Knox | |
| Municipality: Jackson Township | |
| Operator Name: DUGAN OIL AND GAS LLC | |
| Well Pad ID: | |
| Farm/Lease Name: DUGAN JEFFERY & AMANDA | |
| License Status: Producing | |
| License Date: 2016-09-26 | |
| Spud Date: 2016-10-03 | |
| Spud Drilling Contractor: CO TOOLS | |
| Final Drill Date: 2016-12-28 | |
| Well Total Depth: 3020.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.240000 | |
| Longitude: -82.200000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1953-02-01 | |
| Completed | 1953-03-07 | |
| Plugged/Abandoned | 1956-12-03 | |
| Change of Owner | 2014-07-25 | Operator changed from 6217, DAVIDSON OSCAR to 9292, DUGAN OIL AND GAS LLC |
| APP | 2016-09-26 | Proposed Formations:CLINTON SAND, Issued Date:9/26/2016, Expired Date:9/26/2018 12:00:00 PM, Drilling unit acres:120, Proposed Well Type:OG, Proposed Well Class:POOL |
| Reached Total Depth | 2016-12-28 | |
| Completion Report Received | 2017-02-15 | |
| Record Last Modified | 2017-10-24 | |
| Construction Permit Expires | 2018-09-26 |
For data sources see[2]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 1953-03-10 | NITR | 0 | 120 Qts | 0 | ||
| 2017-01-03 | H2O | 15 | 63900 Gal | 22000 | Producers Service Corporation |
For data sources see[3]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2018 | DUGAN OIL AND GAS LLC | 0.00 | 74.00 | 260 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2018 | DUGAN OIL AND GAS LLC | Brine | 150 | 260 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1079768706 | 2017-1-3 0:00:0 | DD | No Violations | |
| -124252670 | 2016-10-17 0:00 | DD | No Violations | |
| -1330776807 | 2016-12-7 0:00: | DD | No Violations | |
| -1340897752 | 2016-10-25 0:00 | DD | No Violations | |
| -2125466930 | 2016-12-1 0:00: | DD | No Violations | |
| -625865148 | 2016-12-27 0:00 | DD | No Violations | |
| -990692429 | 2016-12-5 0:00: | DD | No Violations | |
| 0124252670 | 2016-10-17 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing with the reopening of this well. Jet wire services was on site to run a bond log on the surface casing cement job. The log showed that it was a good cement bond. |
| 0205606116 | 2016-09-22 | Drill / Deepen / Reopen | No Violations | They were in the process of moving in the rig and rigging it up to begin reopening this plugged well during this inspection. |
| 0562846521 | 2016-11-25 | Drill / Deepen / Reopen | No Violations | Drilling operations are on going with the reopening of this well. They are currently 2890 feet and cleaning out the bottom of the well bore. |
| 0572713695 | 2016-10-07 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing with the reopening of this well. They are currently cleaning out the main well bore. |
| 0618346500 | 2016-12-08 | Drill / Deepen / Reopen | No Violations | Drilling operations are on going with this well construction. They ran the 4 1/2 inch production casing today and Cemenco Services Inc. was on site to cement in the casing. |
| 0625453828 | 2016-11-04 | Drill / Deepen / Reopen | No Violations | Operations are ongoing with the reopening of this well. They are currently 730 feet deep with no issues during this inspection. |
| 0625865148 | 2016-12-27 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing with this well they have lost tools and some cable down hole and are in the process of fishing them out. |
| 0681191052 | 2016-09-29 | Drill / Deepen / Reopen | No Violations | Drilling operations are underway with the clean out of this plugged well. They are currently rigging up on location. |
| 0842622887 | 2016-11-10 | Drill / Deepen / Reopen | No Violations | Drilling operations are on going with the reopening of this well. They are currently 800 feet deep and preparing to run and mud in the 7 inch intermediate string. |
| 0990692429 | 2016-12-05 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing with the reopening of this well. They are currently working on the bottom of the hole cleaning it out. |
| 1079768706 | 2017-01-03 | Drill / Deepen / Reopen | No Violations | Producers Service Corporation was on site today to frack this well. |
| 1139657686 | 2017-01-17 | Drill / Deepen / Reopen | No Violations | The well is being set up with the pumping unit. They are in the process of tearing down the rig and moving to a new well location. |
| 1330776807 | 2016-12-07 | Drill / Deepen / Reopen | No Violations | Drilling operations are on going with the clean out of this old well bore. They have finished up cleaning out the bottom of the hole and are now preparing to run the 4 1/2 inch production casing. |
| 1340897752 | 2016-10-25 | Drill / Deepen / Reopen | No Violations | Drilling operations are ongoing with this well. There was no one present during this inspection. |
| 1437347880 | 2016-11-14 | Drill / Deepen / Reopen | No Violations | Cemenco Services Inc. and Mike wheeler was on site to mud in the 7 inch intermediate string of casing today. 4 tons of fire clay was used mudding it in. |
| 1476199932 | 2016-10-11 | Casing String Witnessed | No Violations | On the day of my inspection I found that Dugan Drilling had 8.625 inch casing set at a depth of 488 feet inside of 10 inch hole. Cemenco pumped a mixture of gel and cotton seed hulls prior to mixing cement. The well did not circulate during the mixing stage. They mixed 80 sacks of class A cement and pumped it down the well. The well did not circulate until the displacement stage. There were two brief moments where gel and cotton seed hulls were circulated to surface during displacement, but the mixture fell back down the annulus as soon as Cemenco stopped pumping. I spoke with Knox County inspector Mark McCombs. He claimed that the area has a history of the cement falling to 40 to 60 feet. I told Dugan to let the cement set overnight, and top it off with sack cement. They agreed to top it off the following day after the casing pressure test. |
| 1476285903 | 2016-10-12 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I met Guy Dugan at the site to witness the pressure test and the casing being topped off with sack cement. Cemenco pumped into the casing and brought the pressure up to 300 psi. The pressure bled off to 150 psi. within 5 minutes. Dugan Drilling tightened the cement head down on the casing and Cemenco tried to bleed all of the air out of the system. They pressured up on the casing again and the test failed again. I spoke with Guy Dugan and requested that he have a bond log run on the surface casing cement job. |
| 1476452675 | 2016-10-14 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found that Dugan Drilling was not working at the drill site. The cement head had been removed and the 8.625 inch casing was open. The fluid had fallen out of sight. I dropped a small rock and estimated the fluid to be down 150 feet. I also dropped a pebble down the annulus and estimated the cement to be down 100 feet. I called Guy Dugan and he said they were still waiting on Jet Wireline to run the bond log. |
| 1476715428 | 2016-10-17 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Jet Wireline Service was on site to run a bond log on the surface casing cement job. The log showed the cement top at 42 feet. Dugan had 25 bags of sack cement to top the annulus off. |
| 205606116 | 2016-9-22 0:00: | DD | No Violations | |
| 2125466930 | 2016-12-01 | Drill / Deepen / Reopen | No Violations | Drilling operations are on going with the clean out of this well. The rig is setting idle during this inspection. |
| 562846521 | 2016-11-25 0:00 | DD | No Violations | |
| 572713695 | 2016-10-7 0:00: | DD | No Violations | |
| 618346500 | 2016-12-8 0:00: | DD | No Violations | |
| 625453828 | 2016-11-4 0:00: | DD | No Violations | |
| 681191052 | 2016-9-29 0:00: | DD | No Violations | |
| 842622887 | 2016-11-10 0:00 | DD | No Violations |
For data sources see[8]