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| Well ID: 34-083-20463 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Knox | |
| Municipality: Jackson Township | |
| Operator Name: DUGAN OIL AND GAS LLC | |
| Well Pad ID: | |
| Farm/Lease Name: DUGAN GUY E & LINDA | |
| License Status: Producing | |
| License Date: 2012-08-16 | |
| Spud Date: 2013-09-24 | |
| Spud Drilling Contractor: CO TOOLS | |
| Final Drill Date: 1948-08-31 | |
| Well Total Depth: 2958.00 ft | |
| Configuration: Vertical | |
| Latitude: 40.280000 | |
| Longitude: -82.250000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| Original Spud | 1948-08-05 | DD 1948, P# 463 REPLACES P# 447 |
| Completed | 1948-08-31 | DD 1948, P# 463 REPLACES P# 447 |
| Reached Total Depth | 1948-08-31 | DD 1948, P# 463 REPLACES P# 447 |
| APP | 2012-08-16 | Proposed Formations:CLINTON, Issued Date:8/16/2012, Expired Date:8/16/2014 12:00:00 PM, Drilling unit acres:104.5, Proposed Well Type:OG, Proposed Well Class:POOL |
| Completion Report Received | 2014-06-05 | DD 1948, P# 463 REPLACES P# 447 |
| Construction Permit Expires | 2014-08-16 | DD 1948, P# 463 REPLACES P# 447 |
| Correction to Well | 2015-01-30 | CHANGE IN LEASE NAME. |
| Change of Owner | 2016-04-27 | Operator changed from 882, DUGAN GUY E to 9292, DUGAN OIL AND GAS LLC |
| Record Last Modified | 2019-06-11 | DD 1948, P# 463 REPLACES P# 447 |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2014-01-22 | 2744 | 2986 | 0 |
| 2744 | 2986 | 0 | |
| 2744 | 2986 | 0 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| 2013-11-21 | H2O | 0 | 27500 Gal | 0 | Producers Service Corporation |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2014 | DUGAN OIL AND GAS LLC | 0.00 | 220.00 | 0 |
| 2015 | DUGAN OIL AND GAS LLC | 0.00 | 346.00 | 312 |
| 2016 | DUGAN OIL AND GAS LLC | 0.00 | 608.00 | 365 |
| 2017 | DUGAN OIL AND GAS LLC | 0.00 | 868.00 | 260 |
| 2018 | DUGAN OIL AND GAS LLC | 0.00 | 939.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2014 | DUGAN OIL AND GAS LLC | Brine | 0 | 0 |
| 2015 | DUGAN OIL AND GAS LLC | Brine | 0 | 312 |
| 2016 | DUGAN OIL AND GAS LLC | Brine | 0 | 365 |
| 2017 | DUGAN OIL AND GAS LLC | Brine | 0 | 260 |
| 2018 | DUGAN OIL AND GAS LLC | Brine | 0 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1010354897 | 2013-9-19 0:00: | DD | No Violations | |
| -1879215670 | 2015-11-17 0:00 | PL | No Violations | |
| -743723350 | 2013-10-11 0:00 | DD | No Violations | |
| 0743723350 | 2013-10-11 | Drill / Deepen / Reopen | No Violations | Witnessed the running surface casing today. |
| 1010354897 | 2013-09-19 | Drill / Deepen / Reopen | No Violations | Rig is on location setting up preparing to reopen the hole. No violations. |
| 1382879080 | 2013-10-12 | Drill / Deepen / Reopen | No Violations | Witnessed the cementing of surface casing today. |
| 1385143064 | 2013-11-21 | Drill / Deepen / Reopen | No Violations | During the fracking of this well today the well began to circulate pushing water and hole cuttings 6 feet into the air at the well head. Fracking of the well was stopped at that point when sand was just beginning to be introduced into the line. There were hole cuttings approximately 1/4 inch deep on the rig floor that had washed up. After breaking off the frack valve the hole went on vacuum. The hole was bailed and only resulted in about four bailers full of fluid. A swedge with a 2 inch shut off valve was screwed into the 4 1/2 production and pressured began to build up on the it and held. The evidence here point to a vertical up hole frack, Being that the production casing is maintaining pressure therefore eliminating the possibility of a possible hole in the casing. Mr. Guy Dugan the operator wants to run an electric plug in the casing to check for a possible hole. |
| 1879215670 | 2015-11-17 | Preliminary Restoration | No Violations | This well is a producing well the area has been reclaimed, all drilling equipment has been removed and, vegetation is established and is being used to graze livestock as pasture. |
For data sources see[9]