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Well ID: 34-077-20258 | Loading map...
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Country: United States | |
State: Ohio | |
County: Huron | |
Municipality: Wakeman Township | |
Operator Name: FRANKLIN GAS & OIL CO LLC | |
Well Pad ID: | |
Farm/Lease Name: CONRY UNIT | |
License Status: Final Restoration | |
License Date: 2018-02-27 | |
Spud Date: 2003-05-14 | |
Spud Drilling Contractor: CAPSTAR DRILLING | |
Final Drill Date: 2003-05-21 | |
Well Total Depth: 3940.00 ft | |
Configuration: Vertical | |
Latitude: 41.250000 | |
Longitude: -82.420000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2003-04-29 | 65 FRANKLIN GAS & OIL CO LLC Proposed Formation NEWBURG THRU TREMPEALEAU Issued Date 4/29/2003 Expired Date 4/28/2004 6:00:00 AM |
Inspector Comments Cement Job | 2003-05-14 | Conductor casing drilled on air, cemented in place. Surface casing drilled on air till ~900 feet.Cement Ticket Notes Inspector Reporting BENKO THOMAS |
Original Spud | 2003-05-14 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Completed | 2003-05-21 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Reached Total Depth | 2003-05-21 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Completion Report Received | 2003-09-25 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
APP | 2018-02-27 | Proposed Formations:TREMPEALEAU, Issued Date:2/27/2018, Expired Date:2/27/2020 12:00:00 PM, Drilling unit acres:30.89, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-07-11 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Record Last Modified | 2019-05-10 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
Construction Permit Expires | 2020-02-27 | RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2003-11-06 | 3822 | 3828 | 18 |
3822 | 3828 | 18 | |
3822 | 3828 | 18 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 300 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | FRANKLIN GAS & OIL CO LLC | 4368.00 | 297.00 | 0 |
2004 | FRANKLIN GAS & OIL CO LLC | 2698.00 | 1703.00 | 1320 |
2005 | FRANKLIN GAS & OIL CO LLC | 617.00 | 946.00 | 365 |
2006 | FRANKLIN GAS & OIL CO LLC | 904.00 | 840.00 | 365 |
2007 | FRANKLIN GAS & OIL CO LLC | 988.00 | 644.00 | 365 |
2008 | FRANKLIN GAS & OIL CO LLC | 908.00 | 472.00 | 365 |
2009 | FRANKLIN GAS & OIL CO LLC | 633.00 | 347.00 | 365 |
2010 | FRANKLIN GAS & OIL CO LLC | 243.00 | 325.00 | 365 |
2011 | FRANKLIN GAS & OIL CO LLC | 91.00 | 335.00 | 365 |
2012 | FRANKLIN GAS & OIL CO LLC | 126.00 | 331.00 | 366 |
2013 | FRANKLIN GAS & OIL CO LLC | 74.00 | 276.00 | 365 |
2014 | FRANKLIN GAS & OIL CO LLC | 90.00 | 163.00 | 365 |
2015 | FRANKLIN GAS & OIL CO LLC | 68.00 | 112.00 | 365 |
2016 | FRANKLIN GAS & OIL CO LLC | 139.00 | 0.00 | 365 |
2017 | FRANKLIN GAS & OIL CO LLC | 18.00 | 105.00 | 365 |
2018 | FRANKLIN GAS & OIL CO LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2003 | FRANKLIN GAS & OIL CO LLC | Brine | 345 | |
2004 | FRANKLIN GAS & OIL CO LLC | Brine | 1320 | |
2005 | FRANKLIN GAS & OIL CO LLC | Brine | 330 | 365 |
2006 | FRANKLIN GAS & OIL CO LLC | Brine | 920 | 365 |
2007 | FRANKLIN GAS & OIL CO LLC | Brine | 2210 | 365 |
2008 | FRANKLIN GAS & OIL CO LLC | Brine | 942 | 365 |
2009 | FRANKLIN GAS & OIL CO LLC | Brine | 1032 | 365 |
2010 | FRANKLIN GAS & OIL CO LLC | Brine | 842 | 365 |
2011 | FRANKLIN GAS & OIL CO LLC | Brine | 112 | 365 |
2012 | FRANKLIN GAS & OIL CO LLC | Brine | 180 | 366 |
2013 | FRANKLIN GAS & OIL CO LLC | Brine | 0 | 365 |
2014 | FRANKLIN GAS & OIL CO LLC | Brine | 712 | 365 |
2015 | FRANKLIN GAS & OIL CO LLC | Brine | 566 | 365 |
2016 | FRANKLIN GAS & OIL CO LLC | Brine | 367 | 365 |
2017 | FRANKLIN GAS & OIL CO LLC | Brine | 0 | 365 |
2018 | FRANKLIN GAS & OIL CO LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1381498993 | 2018-5-14 0:00: | PW | No Violations | |
-1617304139 | 2003-5-19 0:00: | PB | No Violations | |
-1773640795 | 2015-9-14 0:00: | PW | No Violations | |
-2016236994 | 2018-7-3 0:00:0 | PB | No Violations | |
-2033054618 | 2003-5-19 0:00: | DD | No Violations | |
-271663038 | 2006-3-21 0:00: | PW | No Violations | |
-381491621 | 2015-9-14 0:00: | PW | No Violations | |
-66454406 | 2003-5-14 0:00: | DD | No Violations | |
-821832448 | 2003-5-15 0:00: | DD | No Violations | |
0066454406 | 2003-05-14 | Drill / Deepen / Reopen | No Violations | Inspect Site. Drill rig and equipment is being mobbed onto site. Conductor casing will be set later today. |
0271663038 | 2006-03-21 | Production Wells | No Violations | Inspect tank and wells. Site ok. |
0343322462 | 2018-05-10 | Production Wells | No Violations | Received a call at 13:32 on from the owner of this well about a possible oil spill from the well. I arrived at 15:06 and on arrival there was a slight amount of oil on the roadway and because of the location of the oil I asked the owner of the well to report the oil spill. An earthen dike was constructed around the wellhead and it was determined that approximately two barrels of oil were lost while the contractor was pulling tubing from the well. The well was still blowing natural gas and it was finally shut in at approximately 17:00. A vacuum truck was used to remove all the free oil inside and outside of the dike area and there was no observed oil in the Waters of Ohio. |
0381491621 | 2015-09-14 | Production Wells | No Violations | Identification is posted and no violations observed at the present time. |
0441741446 | 2005-01-26 | Production Wells | No Violations | Inspect well. Site ok. |
0638291460 | 2003-09-18 | Production Wells | No Violations | Site inspection. Well in production. Two 210 bbl tanks and one 100 bbl tank. ID Posted. Preliminary restoration passed. |
0754383336 | 2004-02-10 | Preliminary Restoration | No Violations | Preliminary restoration ok. Pump jack. 1-210 bbl tank, 1-100 bbl tank. |
0821832448 | 2003-05-15 | Drill / Deepen / Reopen | No Violations | Drill new well. At 434 feet. |
1063887755 | 2003-09-08 | Production Wells | No Violations | Well inspection. Well in production. 100 bbl Tank and 210 bbl tank. Pits closed. Rough graded. Rabbit well. |
1090473041 | 2018-05-09 | Plug / Plug Back | No Violations | Service rig is currently on wellhead. Rods have been pulled from well and stacked on steel stands at well. Identification is posted at site. Operator is going to pull tubing and set bottom plug before moving off site. |
1101308164 | 2003-05-19 | Drill / Deepen / Reopen | No Violations | Drilling At 1130 feet. Target 1200 for surface casing. Sour gas encountered at 900 feet and extreme amount of light blue/green colored water. Collected sample of water, > 1% NaCl. |
1266739142 | 2018-03-06 | Production Wells | No Violations | Inspected well and tank battery. Pump jack is not operable at the present time. Received plugging permit to plug wel in the near future. Identification is posted. |
1359985310 | 2003-05-28 | Drill / Deepen / Reopen | No Violations | Update GPS reading. Well has been drilled. |
1381498993 | 2018-05-14 | Production Wells | No Violations | Follow-up from oil spill from 5/10/2018. Owner has removed tall grass from area and has installed absorbent booms across the road ditch and also in the lake across the road from this well. There is no observed oil at either boom location and the owner has increased the height of the dike. There is still a small amount of oil inside of the dike and no observed oil outside of dike area. Owner will continue the operation of cleaning up the site. |
1511211503 | 2004-01-29 | Production Wells | No Violations | Franklin was in process of swab well. |
1525274620 | 2018-05-02 | Plug / Plug Back | No Violations | Service rig on site currently removing rods from well. Will be pulling rods and tubing from this well and will move service rig to another well before plugging. |
1526994054 | 2018-05-11 | Production Wells | No Violations | Follow-up from oil spill from 5/10/2018. Inspected area around wellhead and found small amount of oil within dike area that was constructed after the spill. Two small areas of oil was located outside of the dike and the oil was cleaned up while I was on location. Grass was asked to be removed because of oily substance on leaves. No oil was observed in the Waters of Ohio. |
1526994783 | 2018-05-18 | Production Wells | No Violations | Follow-up from oil spill from 5/10/2018. Inspected the absorbent booms in road ditch and in the neighbors lake and observed no sign of oil. One puddle of oil was observed outside of the dike area and an absorbent pad was used to remove the oil. |
1529074992 | 2018-06-15 | Production Wells | No Violations | Inspected wellsite after release of oil and brine. Oil and brine have been removed after the accidental release. Well was reconnected to the pipeline after the release but has now been disconnected because of lack of pressure. Operator is going to continue plugging the well in the near future. |
1531414272 | 2018-07-12 | Plug / Plug Back | No Violations | Inspected the level of the cement in the well after plugging activities. Cement level was observed at approximately 2 feet below the surface and the operator is going to cut off the casing below that level and install a steel plate with the wells API number. |
1531488206 | 2018-07-11 | Plug / Plug Back | No Violations | Witnessed the plugging of this well. Installed a cement plug in the area that the 4.5 inch production casing was ripped. Installed a bottom of the surface casing plug and also one at the surface. Cement was witnessed at the surface. |
1532517683 | 2018-07-03 | Plug / Plug Back | No Violations | Witness Petroset Cementing Services Inc. who set a 30 sack bottom cement plug by the bullhead method. The cement was weighed at 14.5 pounds per gallon. |
1538678312 | 2018-10-04 | Final Restoration | No Violations | Checked status of wellsite after well was plugged. Final restoration is not approved at the present time. Steel storage tanks are on site and dike area will need to be leveled and seeded. Contacted operator and he will be providing a landowner waiver in order to allow the flow line to be left. |
1542822028 | 2018-11-21 | Final Restoration | No Violations | Final restoration is not approved. Storage tanks and production equipment have been removed . Dike area will need to have limestone removed and leveled out. Operator has indicated that a landowner waiver will be needed in order to leave the flowline |
1550059211 | 2003-05-21 | Drill / Deepen / Reopen | No Violations | Well was completed today. Mobe to next location on Thursday. |
1558626899 | 2009-12-17 | Production Wells | No Violations | Inspect well. Site ok. |
1564587414 | 2019-7-31 0:00: | FR | No Violations | |
1617304139 | 2003-05-19 | Plug / Plug Back | No Violations | Oversee the installation of the Surface casing. 400 lb of grout, 100 lb of cotton seed. Mix cement 360 sks. No basket was placed on 8 surface casing. 1500 hrs plug down. Total depth 1200 feet. |
1773640795 | 2015-09-14 | Production Wells | No Violations | Identification is posted. Well site consist of a pump jack with a natural gas powered motor and one 210 BBL and one 100 BBL tank with separator. No violations observed at the present time. |
1799175803 | 2017-01-06 | Production Wells | No Violations | No V belts are currently between natural gas engine and pump jack. Identification is posted. |
2016236994 | 2018-07-03 | Plug / Plug Back | No Violations | Bullhead a 30 sack cement plug with cotton seed hulls. Measured the cement weight at 14.5 pounds per gallon. |
2033054618 | 2003-05-19 | Drill / Deepen / Reopen | No Violations | Borehole at 3665 feet. Core bedrock later in day. |
343322462 | 2018-5-10 0:00: | PW | No Violations | |
441741446 | 2005-1-26 0:00: | PW | No Violations | |
475714360 | 2019-12-24 0:00 | FR | No Violations | 0.50 |
638291460 | 2003-9-18 0:00: | PW | No Violations | |
754383336 | 2004-2-10 0:00: | PL | No Violations |
For data sources see[9]