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34-077-20258

Well Details

Well ID: 34-077-20258
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Country: United States
State: Ohio
County: Huron
Municipality: Wakeman Township
Operator Name: FRANKLIN GAS & OIL CO LLC
Well Pad ID:
Farm/Lease Name: CONRY UNIT
License Status: Final Restoration
License Date: 2018-02-27
Spud Date: 2003-05-14
Spud Drilling Contractor: CAPSTAR DRILLING
Final Drill Date: 2003-05-21
Well Total Depth: 3940.00 ft
Configuration: Vertical
Latitude: 41.250000
Longitude: -82.420000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2003-04-29 65 FRANKLIN GAS & OIL CO LLC Proposed Formation NEWBURG THRU TREMPEALEAU Issued Date 4/29/2003 Expired Date 4/28/2004 6:00:00 AM
Inspector Comments Cement Job 2003-05-14 Conductor casing drilled on air, cemented in place. Surface casing drilled on air till ~900 feet.Cement Ticket Notes Inspector Reporting BENKO THOMAS
Original Spud 2003-05-14 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.
Completed 2003-05-21 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.
Reached Total Depth 2003-05-21 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.
Completion Report Received 2003-09-25 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.
APP 2018-02-27 Proposed Formations:TREMPEALEAU, Issued Date:2/27/2018, Expired Date:2/27/2020 12:00:00 PM, Drilling unit acres:30.89, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-07-11 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.
Record Last Modified 2019-05-10 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.
Construction Permit Expires 2020-02-27 RBDMS Rec. UPDATE LOCATION PER DOGRM SURVEYOR 4/16/2018 ALE.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2003-11-06 3822 3828 18
3822 3828 18
3822 3828 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 300 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2003 FRANKLIN GAS & OIL CO LLC 4368.00 297.00 0
2004 FRANKLIN GAS & OIL CO LLC 2698.00 1703.00 1320
2005 FRANKLIN GAS & OIL CO LLC 617.00 946.00 365
2006 FRANKLIN GAS & OIL CO LLC 904.00 840.00 365
2007 FRANKLIN GAS & OIL CO LLC 988.00 644.00 365
2008 FRANKLIN GAS & OIL CO LLC 908.00 472.00 365
2009 FRANKLIN GAS & OIL CO LLC 633.00 347.00 365
2010 FRANKLIN GAS & OIL CO LLC 243.00 325.00 365
2011 FRANKLIN GAS & OIL CO LLC 91.00 335.00 365
2012 FRANKLIN GAS & OIL CO LLC 126.00 331.00 366
2013 FRANKLIN GAS & OIL CO LLC 74.00 276.00 365
2014 FRANKLIN GAS & OIL CO LLC 90.00 163.00 365
2015 FRANKLIN GAS & OIL CO LLC 68.00 112.00 365
2016 FRANKLIN GAS & OIL CO LLC 139.00 0.00 365
2017 FRANKLIN GAS & OIL CO LLC 18.00 105.00 365
2018 FRANKLIN GAS & OIL CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2003 FRANKLIN GAS & OIL CO LLC Brine 345
2004 FRANKLIN GAS & OIL CO LLC Brine 1320
2005 FRANKLIN GAS & OIL CO LLC Brine 330 365
2006 FRANKLIN GAS & OIL CO LLC Brine 920 365
2007 FRANKLIN GAS & OIL CO LLC Brine 2210 365
2008 FRANKLIN GAS & OIL CO LLC Brine 942 365
2009 FRANKLIN GAS & OIL CO LLC Brine 1032 365
2010 FRANKLIN GAS & OIL CO LLC Brine 842 365
2011 FRANKLIN GAS & OIL CO LLC Brine 112 365
2012 FRANKLIN GAS & OIL CO LLC Brine 180 366
2013 FRANKLIN GAS & OIL CO LLC Brine 0 365
2014 FRANKLIN GAS & OIL CO LLC Brine 712 365
2015 FRANKLIN GAS & OIL CO LLC Brine 566 365
2016 FRANKLIN GAS & OIL CO LLC Brine 367 365
2017 FRANKLIN GAS & OIL CO LLC Brine 0 365
2018 FRANKLIN GAS & OIL CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1381498993 2018-5-14 0:00: PW No Violations
-1617304139 2003-5-19 0:00: PB No Violations
-1773640795 2015-9-14 0:00: PW No Violations
-2016236994 2018-7-3 0:00:0 PB No Violations
-2033054618 2003-5-19 0:00: DD No Violations
-271663038 2006-3-21 0:00: PW No Violations
-381491621 2015-9-14 0:00: PW No Violations
-66454406 2003-5-14 0:00: DD No Violations
-821832448 2003-5-15 0:00: DD No Violations
0066454406 2003-05-14 Drill / Deepen / Reopen No Violations Inspect Site. Drill rig and equipment is being mobbed onto site. Conductor casing will be set later today.
0271663038 2006-03-21 Production Wells No Violations Inspect tank and wells. Site ok.
0343322462 2018-05-10 Production Wells No Violations Received a call at 13:32 on from the owner of this well about a possible oil spill from the well. I arrived at 15:06 and on arrival there was a slight amount of oil on the roadway and because of the location of the oil I asked the owner of the well to report the oil spill. An earthen dike was constructed around the wellhead and it was determined that approximately two barrels of oil were lost while the contractor was pulling tubing from the well. The well was still blowing natural gas and it was finally shut in at approximately 17:00. A vacuum truck was used to remove all the free oil inside and outside of the dike area and there was no observed oil in the Waters of Ohio.
0381491621 2015-09-14 Production Wells No Violations Identification is posted and no violations observed at the present time.
0441741446 2005-01-26 Production Wells No Violations Inspect well. Site ok.
0638291460 2003-09-18 Production Wells No Violations Site inspection. Well in production. Two 210 bbl tanks and one 100 bbl tank. ID Posted. Preliminary restoration passed.
0754383336 2004-02-10 Preliminary Restoration No Violations Preliminary restoration ok. Pump jack. 1-210 bbl tank, 1-100 bbl tank.
0821832448 2003-05-15 Drill / Deepen / Reopen No Violations Drill new well. At 434 feet.
1063887755 2003-09-08 Production Wells No Violations Well inspection. Well in production. 100 bbl Tank and 210 bbl tank. Pits closed. Rough graded. Rabbit well.
1090473041 2018-05-09 Plug / Plug Back No Violations Service rig is currently on wellhead. Rods have been pulled from well and stacked on steel stands at well. Identification is posted at site. Operator is going to pull tubing and set bottom plug before moving off site.
1101308164 2003-05-19 Drill / Deepen / Reopen No Violations Drilling At 1130 feet. Target 1200 for surface casing. Sour gas encountered at 900 feet and extreme amount of light blue/green colored water. Collected sample of water, > 1% NaCl.
1266739142 2018-03-06 Production Wells No Violations Inspected well and tank battery. Pump jack is not operable at the present time. Received plugging permit to plug wel in the near future. Identification is posted.
1359985310 2003-05-28 Drill / Deepen / Reopen No Violations Update GPS reading. Well has been drilled.
1381498993 2018-05-14 Production Wells No Violations Follow-up from oil spill from 5/10/2018. Owner has removed tall grass from area and has installed absorbent booms across the road ditch and also in the lake across the road from this well. There is no observed oil at either boom location and the owner has increased the height of the dike. There is still a small amount of oil inside of the dike and no observed oil outside of dike area. Owner will continue the operation of cleaning up the site.
1511211503 2004-01-29 Production Wells No Violations Franklin was in process of swab well.
1525274620 2018-05-02 Plug / Plug Back No Violations Service rig on site currently removing rods from well. Will be pulling rods and tubing from this well and will move service rig to another well before plugging.
1526994054 2018-05-11 Production Wells No Violations Follow-up from oil spill from 5/10/2018. Inspected area around wellhead and found small amount of oil within dike area that was constructed after the spill. Two small areas of oil was located outside of the dike and the oil was cleaned up while I was on location. Grass was asked to be removed because of oily substance on leaves. No oil was observed in the Waters of Ohio.
1526994783 2018-05-18 Production Wells No Violations Follow-up from oil spill from 5/10/2018. Inspected the absorbent booms in road ditch and in the neighbors lake and observed no sign of oil. One puddle of oil was observed outside of the dike area and an absorbent pad was used to remove the oil.
1529074992 2018-06-15 Production Wells No Violations Inspected wellsite after release of oil and brine. Oil and brine have been removed after the accidental release. Well was reconnected to the pipeline after the release but has now been disconnected because of lack of pressure. Operator is going to continue plugging the well in the near future.
1531414272 2018-07-12 Plug / Plug Back No Violations Inspected the level of the cement in the well after plugging activities. Cement level was observed at approximately 2 feet below the surface and the operator is going to cut off the casing below that level and install a steel plate with the wells API number.
1531488206 2018-07-11 Plug / Plug Back No Violations Witnessed the plugging of this well. Installed a cement plug in the area that the 4.5 inch production casing was ripped. Installed a bottom of the surface casing plug and also one at the surface. Cement was witnessed at the surface.
1532517683 2018-07-03 Plug / Plug Back No Violations Witness Petroset Cementing Services Inc. who set a 30 sack bottom cement plug by the bullhead method. The cement was weighed at 14.5 pounds per gallon.
1538678312 2018-10-04 Final Restoration No Violations Checked status of wellsite after well was plugged. Final restoration is not approved at the present time. Steel storage tanks are on site and dike area will need to be leveled and seeded. Contacted operator and he will be providing a landowner waiver in order to allow the flow line to be left.
1542822028 2018-11-21 Final Restoration No Violations Final restoration is not approved. Storage tanks and production equipment have been removed . Dike area will need to have limestone removed and leveled out. Operator has indicated that a landowner waiver will be needed in order to leave the flowline
1550059211 2003-05-21 Drill / Deepen / Reopen No Violations Well was completed today. Mobe to next location on Thursday.
1558626899 2009-12-17 Production Wells No Violations Inspect well. Site ok.
1564587414 2019-7-31 0:00: FR No Violations
1617304139 2003-05-19 Plug / Plug Back No Violations Oversee the installation of the Surface casing. 400 lb of grout, 100 lb of cotton seed. Mix cement 360 sks. No basket was placed on 8 surface casing. 1500 hrs plug down. Total depth 1200 feet.
1773640795 2015-09-14 Production Wells No Violations Identification is posted. Well site consist of a pump jack with a natural gas powered motor and one 210 BBL and one 100 BBL tank with separator. No violations observed at the present time.
1799175803 2017-01-06 Production Wells No Violations No V belts are currently between natural gas engine and pump jack. Identification is posted.
2016236994 2018-07-03 Plug / Plug Back No Violations Bullhead a 30 sack cement plug with cotton seed hulls. Measured the cement weight at 14.5 pounds per gallon.
2033054618 2003-05-19 Drill / Deepen / Reopen No Violations Borehole at 3665 feet. Core bedrock later in day.
343322462 2018-5-10 0:00: PW No Violations
441741446 2005-1-26 0:00: PW No Violations
475714360 2019-12-24 0:00 FR No Violations 0.50
638291460 2003-9-18 0:00: PW No Violations
754383336 2004-2-10 0:00: PL No Violations

For data sources see[9]

References