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34-073-21924

Well Details

Well ID: 34-073-21924
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Country: United States
State: Ohio
County: Hocking
Municipality: Green Township
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name: POSTON RALPH
License Status: Final Restoration
License Date: 2007-03-20
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1976-11-17
Well Total Depth: 2860.00 ft
Configuration: Vertical
Latitude: 39.500000
Longitude: -82.340000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-09-27 263 GENERAL ELEC CO GeoDate 9/27/76
Completed 1976-11-17
Reached Total Depth 1976-11-17
CO 1996-12-02 5387 OH OIL GATHERING CORP IV GeoDate 9/27/76
Change of Owner 2001-08-23 Operator changed from 5387, OH OIL GATHERING CORP IV to 6295, KNOX ENERGY INC.
Plugged/Abandoned 2007-03-15
APP 2007-03-20 Proposed Formations:CLINTON, Issued Date:3/20/2007, Expired Date:3/19/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2008-03-19
Record Last Modified 2013-03-14

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1600 Bbl 20000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 GE CONSUMER & INDUSTRIAL 847.00 295.00 0
1985 GE CONSUMER & INDUSTRIAL 600.00 261.00 0
1986 GE CONSUMER & INDUSTRIAL 1187.00 277.00 365
1987 GE CONSUMER & INDUSTRIAL 1242.00 325.00 365
1988 GE CONSUMER & INDUSTRIAL 764.00 116.00 365
1989 GE CONSUMER & INDUSTRIAL 1386.00 61.00 365
1990 GE CONSUMER & INDUSTRIAL 2438.00 40.00 365
1991 GE CONSUMER & INDUSTRIAL 1821.00 49.00 365
1992 GE CONSUMER & INDUSTRIAL 1465.00 103.00 365
1993 GE CONSUMER & INDUSTRIAL 811.00 25.00 365
1994 GE CONSUMER & INDUSTRIAL 241.00 44.00 260
1995 GE CONSUMER & INDUSTRIAL 148.00 86.00 260
1996 GE CONSUMER & INDUSTRIAL 189.00 31.00 200
2001 KNOX ENERGY INC. 0.00 0.00 365
2002 KNOX ENERGY INC. 0.00 0.00 365
2003 KNOX ENERGY INC. 0.00 0.00 365
2004 KNOX ENERGY INC. 0.00 5.00 222
2005 KNOX ENERGY INC. 0.00 0.00 0
2006 KNOX ENERGY INC. 0.00 21.00 365
2007 KNOX ENERGY INC. 0.00 0.00 75

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 GE CONSUMER & INDUSTRIAL Brine 0 0
1985 GE CONSUMER & INDUSTRIAL Brine 1523 0
1986 GE CONSUMER & INDUSTRIAL Brine 1385 365
1987 GE CONSUMER & INDUSTRIAL Brine 1803 365
1988 GE CONSUMER & INDUSTRIAL Brine 1317 365
1989 GE CONSUMER & INDUSTRIAL Brine 1178 365
1990 GE CONSUMER & INDUSTRIAL Brine 997 365
1991 GE CONSUMER & INDUSTRIAL Brine 1013 365
1992 GE CONSUMER & INDUSTRIAL Brine 0 365
1993 GE CONSUMER & INDUSTRIAL Brine 129 365
1994 GE CONSUMER & INDUSTRIAL Brine 78 260
1995 GE CONSUMER & INDUSTRIAL Brine 51 260
1996 GE CONSUMER & INDUSTRIAL Brine 37 200
2001 KNOX ENERGY INC. Brine 0 365
2002 KNOX ENERGY INC. Brine 0 365
2003 KNOX ENERGY INC. Brine 0 365
2004 KNOX ENERGY INC. Brine 0 222
2005 KNOX ENERGY INC. Brine 0 0
2006 KNOX ENERGY INC. Brine 0 365
2007 KNOX ENERGY INC. Brine 0 75

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1397485574 2008-8-6 0:00:0 FR No Violations
-1629657937 2008-5-30 0:00: FR No Violations
-1677929060 2008-4-21 0:00: FR No Violations
-53224104 2007-3-15 0:00: PB No Violations
0053224104 2007-03-15 Plug / Plug Back No Violations Company set pre-cast plug and washed in clay to the surface.
1324995994 2007-03-13 Plug / Plug Back No Violations Company washed in 500 feet of clay for bottom hole plug.
1361505287 2007-09-04 Final Restoration Violations Noted An inspection revealed that the final restoration does not meet requirements. Plastic and steel lines observed along the lease road and around plugged and abandoned well location. Also, noted was (2) 210bbl tanks will need to be removed.
1397485574 2008-08-06 Final Restoration No Violations A follow-up inspection revealed that the FR meets requirements.
1629657937 2008-05-30 Final Restoration No Violations A follow-up inspection revealed non-compliance.
1677929060 2008-04-21 Final Restoration No Violations A follow-up inspection revealed that the company is working towards resolving FR.
1971004760 2007-11-19 Final Restoration No Violations A follow-up inspection revealed non-compliance.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1361505287 US-OH-110505 2007-09-06 Failure to remove production equip. within 6 mos. REPLACE

For data sources see[8]

References