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Well ID: 34-073-21543 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hocking | |
Municipality: Falls Township | |
Operator Name: KILBARGER INVESTMENTS INC | |
Well Pad ID: | |
Farm/Lease Name: COSPER WELL SERVICE INC | |
License Status: Active Injection | |
License Date: 1985-02-01 | |
Spud Date: 1972-09-01 | |
Spud Drilling Contractor: CO TOOLS | |
Final Drill Date: 1985-04-23 | |
Well Total Depth: 2607.00 ft | |
Configuration: Vertical | |
Latitude: 39.500000 | |
Longitude: -82.430000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1972-09-01 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
Plugged/Abandoned | 1974-06-22 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
CO | 1985-02-01 | 1068 COSPER WELL/H COSPER GeoDate 2/1/85 |
Conversion to Injector | 1985-02-01 | |
Salt Water Injection Well | 1985-02-01 | Issued Date 2/1/85 Expired Date 7/31/85 Acres 0040000 Tool Type CRF Proposed Formation NEWBURG Proposed Depth 00000 Proposed Drill Depth 00000 |
Storage Well | 1985-02-01 | Issued Date 2/1/85 Expired Date 7/31/85 Acres 0040000 Tool Type CRF Proposed Formation NEWBURG Proposed Depth 00000 Proposed Drill Depth 00000 |
Reached Total Depth | 1985-04-23 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
Annulus Pressure Monitoring Approved | 1985-04-30 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
First Injection | 1985-05-18 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
Construction Permit Expires | 1985-07-31 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
CO | 1994-04-29 | 1675 KILBARGER EDWARD OR ANN GeoDate 2/1/85 |
Last Compliance Report | 2016-05-16 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
Record Last Modified | 2017-10-19 | BASED ON CHIEFS ORDER 2001-21 MAXIMUM PRESSURE IS 310 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-04-28 | 2250 | 2300 | 0 |
2250 | 2300 | 0 | |
2250 | 2300 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 70000 Gal | 0 | 200 SACKS SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1039804720 | 2019-11-21 0:00 | SW | No Violations | 2.00 |
-1133295158 | 2005-10-26 0:00 | SW | No Violations | |
-1139110421 | 2010-3-15 0:00: | SW | No Violations | |
-1199638308 | 2019-7-9 0:00:0 | SW | No Violations | 3.70 |
-126124846 | 2019-7-12 0:00: | SW | No Violations | 8.50 |
-1283405592 | 2019-7-3 0:00:0 | SW | No Violations | 0.80 |
-1297702774 | 2012-3-29 0:00: | SW | No Violations | 1.00 |
-1299757447 | 2018-12-4 0:00: | SW | No Violations | 3.00 |
-1382504724 | 2015-9-14 0:00: | SW | No Violations | 3.00 |
-1384968944 | 2007-10-30 0:00 | SW | No Violations | |
-1395525982 | 2016-8-31 0:00: | SW | No Violations | 2.00 |
-1427204606 | 2018-8-6 0:00:0 | SW | No Violations | 6.70 |
-1459311594 | 2020-4-2 0:00:0 | SW | No Violations | 2.50 |
-1463099775 | 2015-4-1 0:00:0 | SW | No Violations | 2.00 |
-1467766740 | 2012-8-22 0:00: | SW | No Violations | |
-1507168674 | 2011-8-31 0:00: | SW | No Violations | |
-151804385 | 2010-12-28 0:00 | SW | No Violations | 0.50 |
-1535789232 | 2012-2-23 0:00: | SW | No Violations | |
-1548280675 | 2003-5-6 0:00:0 | SW | No Violations | |
-158727039 | 2009-9-2 0:00:0 | SW | No Violations | |
-1638470805 | 2016-3-10 0:00: | SW | No Violations | 3.50 |
-1659275288 | 2018-8-9 0:00:0 | SW | No Violations | 0.80 |
-1661046046 | 2007-2-15 0:00: | SW | No Violations | |
-1691828432 | 2019-3-25 0:00: | SW | No Violations | 4.50 |
-1695129565 | 2012-1-25 0:00: | SW | No Violations | 2.50 |
-1712029995 | 2003-1-29 0:00: | SW | No Violations | |
-1740113642 | 2006-7-12 0:00: | SW | No Violations | |
-1756202985 | 2015-9-17 0:00: | SW | No Violations | 2.00 |
-1769329562 | 2016-5-9 0:00:0 | SW | No Violations | 3.50 |
-1777427458 | 2016-5-3 0:00:0 | SW | No Violations | 1.50 |
-1813940934 | 2003-7-24 0:00: | SW | No Violations | |
-2019634361 | 2014-4-9 0:00:0 | SW | No Violations | 4.00 |
-2060452849 | 2014-5-13 0:00: | SW | No Violations | 1.50 |
-2062700710 | 2013-11-25 0:00 | SW | No Violations | 5.50 |
-2125436276 | 2020-6-2 0:00:0 | SC | No Violations | 3.50 |
-229075245 | 2019-5-20 0:00: | SW | No Violations | 6.00 |
-243623953 | 2019-7-10 0:00: | SW | No Violations | 5.40 |
-28469154 | 2016-9-1 0:00:0 | AM | No Violations | |
-317591014 | 2020-6-29 0:00: | SC | No Violations | 1.00 |
-387228205 | 2005-6-8 0:00:0 | SW | No Violations | |
-404624269 | 2009-3-3 0:00:0 | SW | No Violations | |
-405832014 | 2003-10-27 0:00 | SW | No Violations | |
-426977741 | 2013-9-16 0:00: | SW | No Violations | 2.00 |
-450769040 | 2018-3-5 0:00:0 | SW | No Violations | 1.50 |
-46836104 | 2019-5-8 0:00:0 | SW | No Violations | 5.00 |
-482011221 | 2020-3-11 0:00: | SC | No Violations | 4.00 |
-511992619 | 2015-1-28 0:00: | SW | No Violations | 1.50 |
-516859439 | 2004-1-27 0:00: | SW | No Violations | |
-542593344 | 2008-12-8 0:00: | SW | No Violations | |
-551549115 | 2018-9-13 0:00: | SW | No Violations | 10.30 |
-559281015 | 2012-6-13 0:00: | SW | No Violations | 1.00 |
-633971054 | 2011-3-31 0:00: | SW | No Violations | |
-664010408 | 2004-5-27 0:00: | SW | No Violations | |
-760952749 | 2008-5-21 0:00: | SW | No Violations | |
-770660392 | 2018-8-24 0:00: | SW | No Violations | 8.50 |
-869291426 | 2012-3-29 0:00: | SW | No Violations | |
-890087559 | 2004-4-1 0:00:0 | SW | No Violations | |
-916501293 | 2016-3-15 0:00: | SW | No Violations | 4.00 |
-927315817 | 2007-3-12 0:00: | SW | No Violations | |
-957042327 | 2007-6-20 0:00: | SW | No Violations | |
0000UIC289 | 1987-08-12 | Salt Water Injection Well | No Violations | 1501:9-3-04 (A) |
0000UIC290 | 1987-08-12 | Salt Water Injection Well | No Violations | 1509.072 |
0000UIC301 | 1986-12-11 | Salt Water Injection Well | No Violations | 1501:9-3-06 |
0000UIC302 | 1986-12-11 | Salt Water Injection Well | No Violations | 1509.22 (A) |
0000UIC303 | 1986-12-11 | Salt Water Injection Well | No Violations | 1509.072(A) |
0000UIC304 | 1986-12-11 | Salt Water Injection Well | No Violations | 1501:9-3-04 (A) |
0000UIC305 | 1986-12-11 | Salt Water Injection Well | No Violations | 1501:9-3-07 (F) |
0000UIC480 | 1988-02-18 | Salt Water Injection Well | No Violations | 1501:9-3-04 (A) |
0000UIC537 | 1988-05-20 | Salt Water Injection Well | No Violations | 1501:9-3-04(A) |
0000UIC910 | 1990-05-08 | Brine Hauler | No Violations | 1509.222-(A-2) LACK OF INSURANCE COMPANY COSPER WELL SERVICE |
000PL16360 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
001269i512 | 2001-11-13 | Salt Water Injection Well | No Violations | No violations. |
001269i697 | 2002-01-16 | Salt Water Injection Well | No Violations | No violations. |
001269i875 | 2002-03-19 | Salt Water Injection Well | No Violations | No violations. |
0026793697 | 2017-03-20 | Brine Hauler | No Violations | Inspected the surface facility and witnessed brine truck unloading on the pad. Reviewed brine hauling log. |
0028469154 | 2016-09-01 | Administrative Inspection | No Violations | Received a voice mail from Larry Howdyshell at 7:01 am. The collar above the packer pulled off. They are working on retrieving the packer. |
0046836104 | 2019-05-08 | Salt Water Injection Well | Violations Noted | Compliance Notice # 1427204606 and # 1541774687 follow up inspection. On site with ODNR DOGRM Geologist Jake Glascock. A new scald area was observed between the tank battery and the unloading pad half round tank, at the base of the steep slope and under the overhead lines from the unloading pad half round tank to the tank battery. Scald GPS N39.50717/W082.43765. A soil sample from the scald was collected. Sample # JG-176. The sample will be sent to the Lab for analysis. The state issued conductivity probe was used in the tank battery and maxed out the conductivity probe by two of the leaking tanks. The oil residue has not been removed from the scald area extending down slope from the tank battery into the containment moat. The scald areas need to be excavated and the contaminated material hauled to an EPA approved landfill for disposal. Grade and establish good vegetative cover on all remediated areas at the facility. Larry Howdyshell was notified of the new scald area at 1:26 pm on 5-8-2019. Contact Inspector Jon Scott at 740-624-4963. |
0053889245 | 2004-12-14 | Salt Water Injection Well | No Violations | No violations. |
005609i210 | 2001-06-04 | Salt Water Injection Well | Violations Noted | An inspection of the well revealed that the well site needs seed and mulch on all bare areas and ID needs rewrote on sticker at tanks and full ID at well head. Need a 1/4 valve on injection side of well, this is a must . |
005609i338 | 2001-08-20 | Salt Water Injection Well | Violations Noted | An inspection of the well revealed that the pressure on both the injection and annulus are the same. Both are on vaccum and well must be shut in until violation has been corrected. Notified Mr. Delmer Harris and Mr. Mike Mc Pete of Kilbargers . Also notified Tom in UIC. |
0078190246 | 2015-06-22 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment area, tanks, injection pressure and annulus pressure. One of the 100 barrel steel tanks showed signs of leaking at the base. I called Larry Howdyshell and Clint Kilbarger about the tank. Larry told me that he was aware of the tank and that it was empty. He told me that they will disconnect the tank on the 24th. Checked brine hauling logs and witnessed brine trucks unloading on the pad. |
01269i1072 | 2002-05-22 | Salt Water Injection Well | No Violations | No violations. |
0151804385 | 2010-12-28 | Salt Water Injection Well | No Violations | An inspection revealed no violations. Run tickets dated 12/28/10 showed: 30 bbl from Hocking Co. Permit 1365; and 80 bbl split load for Perry Co. Permits 3386, 6961, 3422. Snow cover at time of inspection. |
0158727039 | 2009-09-02 | Salt Water Injection Well | No Violations | An inspection revealed that the filter change location above the well has been cleaned up. No violations at this time. |
0200226437 | 2009-12-03 | Salt Water Injection Well | No Violations | No violations were noted at this time. |
0348830415 | 2013-01-15 | Salt Water Injection Well | No Violations | Good Identification on well. Checked the injection pressure and the annulus pressure. Two of the 100 barrel steel tanks show signs of leakage (stained area 1 foot in diameter) on gravel. Leak appears to be coming from the tank drain valve nipple. Tanks were not leaking during inspection. Inspector Andy Thomas will follow up with Kilbarger on the status of the tanks. |
0349627697 | 2012-03-08 | Salt Water Injection Well | No Violations | Checked on a contamination clean-up for inspector Jon Scott. Everything was back in compliance. Contamination had been cleaned up and area had straw on it. Accompanied by inspector Kip Thompson. |
0387228205 | 2005-06-08 | Salt Water Injection Well | No Violations | No violations. |
0404624269 | 2009-03-03 | Salt Water Injection Well | No Violations | An inspection revealed no violations at this time. |
0405832014 | 2003-10-27 | Salt Water Injection Well | No Violations | No violations. |
0426977741 | 2013-09-16 | Salt Water Injection Well | No Violations | UIC inspection, the annulus pressure was 30 PSI, the injection side was on vacuum. No violations noted. |
0432493261 | 2018-03-01 | Salt Water Injection Well | Violations Noted | The Division received annual report form 204. Review of the form 204 revealed an exceedance of the maximum allowable injection pressure. The injection pressure shall be reduced and the auto shut down switch shall be adjusted to the maximum allowable injection pressure. A follow-up inspection will be conducted. |
0450769040 | 2018-03-05 | Salt Water Injection Well | No Violations | The salt water injection well was written up for 1501: 9-3-07 (D) exceeding maximum allowable injection pressure. The injection tubing was on vacuum and the annulus had 10 psi. The containment dike was free of fluids. This satisfies the compliance notice issued on 3.1.2018. |
0474636307 | 2012-08-22 | Salt Water Injection Well | No Violations | Assisted Inspector Jon Scott with sampling water from the tank battery. |
0511992619 | 2015-01-28 | Salt Water Injection Well | No Violations | UIC inspection. The injection is on vacuum, the annulus has pressure, but the pressure was to low to read. I have contacted Kilbarger to have a mini test performed. |
0516859439 | 2004-01-27 | Salt Water Injection Well | No Violations | No violations. |
0542593344 | 2008-12-08 | Salt Water Injection Well | No Violations | An inspection revealed no violations at this time. |
0551549115 | 2018-09-13 | Salt Water Injection Well | No Violations | Compliance Notice # 1427204606 follow up inspection. Collect soil samples from the containment area and take the samples to the ODNR-DOGRM Lab. |
0559281015 | 2012-06-13 | Salt Water Injection Well | No Violations | Drain from unloading pad was piped into a 100 barrel tank in the dike. Vegetation was well established where spill occurred near filter housing. Tank underneath filter housing had been recently pumped out. |
0595755828 | 2016-08-29 | Salt Water Injection Well | Violations Noted | Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. The injection tubing and annulus both had vacuum. The annulus must be tested. Contact Inspector Jon Scott at 740-624-4963 to schedule the test. |
0612977728 | 2012-08-20 | Salt Water Injection Well | No Violations | Well and tank battery in compliance. |
0628501973 | 2009-06-02 | Salt Water Injection Well | No Violations | An inspection of the SWIW and related storage tanks was conducted with Mr. Jeff Fry. During the inspection, it was noted that old oil approximately 3 x 5 exists around the catch tank/filter change location above the well head. Contacted Mr. Mike McPeek with Kilbarger by telephone on 6/2/2009 @ 1:59 pm and recommended that they be more cautious changing filters and to cleanup area. No violations at this time. |
0633971054 | 2011-03-31 | Salt Water Injection Well | No Violations | 14- 100bbl steel tanks manifold together with in an earthen dike. 2 open top steel vaults, 2- 200 bbl steel horizontal tanks contained with in a dike, located next to unloading pad. |
0664010408 | 2004-05-27 | Salt Water Injection Well | No Violations | No vioaltions |
0664518521 | 2013-07-03 | Salt Water Injection Well | No Violations | Injection well inspection, the annulus pressure was 310 PSI, the injection side is on vacuum. No violation noted. |
0738737287 | 2016-09-01 | Administrative Inspection | No Violations | Received a phone call from Larry Howdyshell at 12:01 pm. Larry stated that the packer released and fell down the well casing. They are currently working on retrieving the packer. Larry asked for well records. He was referred to the UIC section geologist. |
0760952749 | 2008-05-21 | Salt Water Injection Well | No Violations | No violations |
0770660392 | 2018-08-24 | Salt Water Injection Well | No Violations | Compliance Notice # 1427204606 follow up inspection. Kilbarger service rig on well running new Parmaco tension packer with shear pins (40000 lbs. shear) and 2003.35 feet of used tubing. Packer set at 2003.35 feet with 28,000 lbs. tension. Annulus was filled with water and inhibitor and tested at 330 psi, at 5 minutes 330 psi, at 15 psi 328 psi. |
0778227111 | 2014-03-11 | Salt Water Injection Well | No Violations | UIC inspection, the injection pressure was 0 PSI, the annulus pressure was 5 PSI. No violations noted. |
0810256088 | 2008-09-22 | Salt Water Injection Well | No Violations | A follow-up inspection revealed that pressure has been placed on the annulus. |
0869291426 | 2012-03-29 | Salt Water Injection Well | Violations Noted | Mixed fresh water and green dye and poured down the unloading pad drain. The water came out of the hillside. A 2inch rusted steel line was broken off. The unloading pad drain is not connected to a tank or vault. I called Jim Kilbarger and told him to correct this issue. He said that he will take care of it. I told him that the drain from the unloading pad must go to a tank or water tight vault for storage. |
0882079066 | 2019-04-29 | Salt Water Injection Well | Violations Noted | Our records indicate that the Division has not received the Salt Water Injection Well Annual Report (Form 204) that was due on April 15th for 2018, Please submit the Form 204 to the Division by 5/29/2019. |
0890087559 | 2004-04-01 | Salt Water Injection Well | No Violations | No violations. |
0916501293 | 2016-03-15 | Salt Water Injection Well | No Violations | Compliance Notice # 1638470805 follow up inspection. The annulus pressure is zero. The injection tubing fittings have not been replaced. Approximately half of the contaminated area has the straw replaced. I meet with Larry Howdyshell and Jim Kilbarger on site to discuss the compliance notice. We discussed the need to replace the 1/4 fitting on the injection tubing. We also discussed the need to test the annulus and monitor the annulus pressure. We reviewed the areas that need to be remediated. We also discussed future upgrades to the facility and the need to submit plans to the UIC section for approval prior to any changes to the facility. |
0927315817 | 2007-03-12 | Salt Water Injection Well | No Violations | The company, Kilbarger Investments, is pulling tubing and packer out of the well. |
0957042327 | 2007-06-20 | Salt Water Injection Well | No Violations | A follow-up inspection revealed that the well is in-compliance. |
0968352752 | 2007-03-12 | Surface Facility Construction | No Violations | Company is pulling tubing and packer out of the well. |
0981865674 | 2019-01-15 | Salt Water Injection Well | No Violations | Compliance Notice # 1427204606 and 1541774687 follow up inspection. Collect soil sample from beside the half round steel tank with the filter housing on top at GPS N39.50782/W082.43742. And a Control sample at GPS N39.50787/W082.43794. Samples to be taken to Lab. |
0983318169 | 2008-09-16 | Salt Water Injection Well | No Violations | An inspection revealed no pressure on the annulus. The company was contacted by telephone and informed of the inspection results. |
0987662428 | 2011-12-15 | Salt Water Injection Well | No Violations | Accompanied Jon Scott on inspection. |
1028745012 | 2020-5-28 0:00: | SC | No Violations | 5.50 |
1071168668 | 2003-12-09 | Salt Water Injection Well | No Violations | No violations. |
1083414513 | 2008-02-21 | Salt Water Injection Well | No Violations | An inspection revealed that pressure has been placed on the annulus. |
1092925288 | 2004-08-19 | Salt Water Injection Well | No Violations | No violations. NEW LAT & LONG |
1113221954 | 2005-04-06 | Salt Water Injection Well | No Violations | No violations. |
1113388492 | 2014-10-22 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment area, tanks, injection pressure and annulus pressure. Identification posted on the well. |
1114928871 | 2012-03-29 | Salt Water Injection Well | No Violations | FOLLOW UP TO NOV # 1989879742 FOLLOW UP TO NOV # -869291426 Mixed fresh water and green dye and poured down the unloading pad drain. The water came out of the hillside. A 2inch rusted steel line was broken off. The unloading pad drain is not connected to a tank or vault. I called Jim Kilbarger and told him to correct this issue. He said that he will take care of it. I told him that the drain from the unloading pad must go to a tank or water tight vault for storage. |
1133295158 | 2005-10-26 | Salt Water Injection Well | No Violations | No violations |
1139110421 | 2010-03-15 | Salt Water Injection Well | No Violations | An inspection revealed no violations at this time. |
1168627885 | 2007-01-10 | Salt Water Injection Well | Violations Noted | An inspection conducted on 1/10/2007 revealed that the injection and annulus side of the well did not have pressure. Also noted was that a 1/4 valve would be needed on the injection side of the well, a fitting was leaking at a storage facility and new identification would be needed at the storage tank and the well head. |
1203357498 | 2016-11-14 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. Identification posted at the well. |
1218998161 | 2019-01-10 | Salt Water Injection Well | No Violations | Compliance Notice # 1427204606 and # 1541774687 follow up inspection. Inspected the unloading pad, half round tank at unloading pad, containment area, tanks, half round tank with filter housing( located between the tanks and the well), Injection pressure and annulus pressure. An additional 100 barrel steel tank is seeping brine. The tank was marked with orange marking tape. The half round tank with the filter housing has over flowed brine. Fluid was observed under the half round tank. The fluid was tested with High Range Quantab The Quantab maxed out exceeding 6620 ppm Cl. The area down slope of the tanks had fresh straw covering oil residue and oil absorbing material. Nick Vecchiarelli was notified by phone about the leaking 100 barrel tank, and the release at the half round tank. |
1232285113 | 2007-05-24 | Salt Water Injection Well | No Violations | A follow-up inspection revealed non-compliance. |
1235625814 | 2003-06-19 | Salt Water Injection Well | No Violations | No violations. |
1243047128 | 2011-12-15 | Salt Water Injection Well | No Violations | Accompanied by Andy Thomas MRI. 100 bbl tank has ran over and leaked small amount brine in dike. The half tank under the filter housing has leaked and needs emptied. Andy has contacted the company. |
1269i1072 | 2002-5-22 0:00: | SW | No Violations | |
1269i11851 | 2001-03-27 | Salt Water Injection Well | No Violations | In - complaince |
1269i11851144 | 2001-3-27 0:00: | SW | No Violations | |
1269i30509 | 2001-02-14 | Salt Water Injection Well | No Violations | AN INSPECTION OF THE WELL REVEALED THAT THERE IS NO WAY OF TESTING THE INJECTION PRESSURE ON THE WELL , THERE IS NO 1/4 VALVE TO HOOK GAUGE TOO. ALSOREQUEST THAT ON NEXT MONTHLY TEST THAT THE COMPANY NOTIFY THE INSPECTOR OF THE TEST IS HE CAN WITNESS THE TEST. |
1269i3050925 | 2001-2-14 0:00: | SW | No Violations | |
1269i512 | 2001-11-13 0:00 | SW | No Violations | |
1269i697 | 2002-1-16 0:00: | SW | No Violations | |
1269i875 | 2002-3-19 0:00: | SW | No Violations | |
1289319692 | 2004-02-26 | Salt Water Injection Well | No Violations | No violations. |
1297702774 | 2012-03-29 | Salt Water Injection Well | No Violations | Accompanied Inspector Jon Scott on inspection. We poured dye in the drain on the unloading pad, and discovered that it drained out on the side of the hill. |
1299757447 | 2018-12-04 | Salt Water Injection Well | No Violations | Compliance Notices # 1427204606 and 1541774687 follow up inspection. The facility access road gate was closed and locked. The contaminated material at the well site where the injection tubing was stacked has been removed from the location. The oil soaked absorbent material has been removed from between the 100 barrel tanks. Straw has been placed on the area between the 100 barrel tanks. The containment area down slope of the 100 barrel tanks has not had the oil residue removed and this area has fresh straw placed on top of the area. Down slope of the half round steel tank at the unloading pad has had the oil contaminated soil removed and fresh straw placed on top of the remediated area. High range Quantabs were used to test the water between the 100 barrel tanks. The Quantab had 4.8 on the strip which is 1037 ppm CL. Identification was posted at the well. The containment area has 8 inches of fluid in it. |
1319306838 | 2012-11-27 | Salt Water Injection Well | No Violations | No violations were noted at the time of inspection. Tank battery and well are in compliance. |
1327543793 | 2018-08-14 | Salt Water Injection Well | No Violations | Compliance Notice # 1427204606 follow up inspection. Absorbent material has been placed on the oil around the 100 barrel tanks that overflowed and also on the area down slope of the 100 barrel tanks. The injection tubing and packer are stacked on the well site. The well casing has a 4.5 inch plug installed. Accompanied by UIC Geologist. |
1330543337 | 2012-01-25 | Salt Water Injection Well | No Violations | Talked to Delmer Harris about the half tank with filter housing on top needs to be emptied and used filters need to be disposed of. |
1342327358 | 2005-03-03 | Salt Water Injection Well | No Violations | No violations. |
137723017 | 2019-7-8 0:00:0 | SW | No Violations | 0.30 |
1382504724 | 2015-09-14 | Salt Water Injection Well | Violations Noted | Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. The 100 barrel steel tank that is connected to the unloading pad drain has a 2 leaking valve, with a 2 area of contamination below the valve. Multiple areas covered with straw and devoid of vegetation were observed down slope of the open top half tank at the unloading pad. Closer inspection revealed oil stained soil below the straw. I called Larry Howdyshell and told him to repair or replace the leaking 2 valve and to remove all contaminated soil and take it to an EPA approved landfill. |
1384968944 | 2007-10-30 | Salt Water Injection Well | No Violations | No violations were noted. |
1395525982 | 2016-08-31 | Salt Water Injection Well | No Violations | Compliance Notice # 595755828 follow up inspection. The annulus is not holding water. Every time the annulus is filled up the water level drops at a steady rate. A service rig is being scheduled to work on the well. The injection line valve is shut off. |
1412182321 | 2014-10-01 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment dike, tanks, injection line, annulus pressure and injection pressure. Witnessed Kilbarger truck (UIC # 46) unloading on the pad and a MartinDill truck (UIC # 344) unloading on the pad. Reviewed the brine hauling logs of both trucks. |
1417985171 | 2013-01-15 | Salt Water Injection Well | No Violations | I accompanied Inspector Jon Scott on this inspection. We inspected the tank battery first. There are two steel nipples that exhibit signs of leakage. They were not leaking at the time of inspection, but I will follow-up with the company about them so that they will be aware of it. Pressures were gauged at the well head, and it is in compliance. |
1427204606 | 2018-08-06 | Salt Water Injection Well | Violations Noted | Received notification of a brine release in the containment dike, from ODNR-DOGRM MRI Thompson 8-6-18 at 8:44 am. A 100 barrel steel tank was over flowed and caused oil and brine to flow into the containment area. Contaminated soil had been removed prior to my arrival. The containment area is 141 feet by 6 feet. 3 Field tests of the soil revealed( 1) 4057 ppm Cl. (2) greater than 6620 ppm Cl. (3) greater than 6620 ppm Cl. The injection pressure and annulus pressure were checked during the inspection. The annulus and injection tubing were on vacuum. Larry Howdyshell was on site. I told Larry to test the annulus and to remove all contaminated material from the containment area and to haul it to an EPA approved landfill. The injection tubing is to be shut in until a successful mechanical integrity test can be performed. |
1458652781 | 2016-03-21 | Salt Water Injection Well | No Violations | Compliance notice # 1638470805 Follow up inspection. The 1/4 injection tubing fitting has been replaced with a new 1/4 needle valve. The annulus had slight vacuum then zero pressure. The injection tubing had zero pressure. The contaminated soil has not been removed. New straw was placed over the contaminated area. One of the 100 barrel steel tanks appears to have a small leak at the bottom. Tank bottom edge is wet and rust has flaked off. Gravel is stained. |
1459791098 | 2016-04-04 | Salt Water Injection Well | No Violations | Compliance notice # 1638470805 follow up inspection. Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. The contamination down slope from the unloading pad has not been remediated. Contaminated soil was observed under fresh straw in multiple locations. I contacted Larry Howdyshell about the remaining contaminated material. We discussed that the contaminated material must be disposed of at an EPA approved landfill and that disposal documentation needs to be provided to the UIC Section. |
1463099775 | 2015-04-01 | Salt Water Injection Well | No Violations | UIC inspection. The injection side is on vacuum. The annulus pressure was 350 PSI. The tank that is used for catching fluid during filter changes has been pumped down. No violations noted. |
1467766740 | 2012-08-22 | Salt Water Injection Well | No Violations | Random brine sample taken today and sent to ODNR Lab. Sample taken from brine line feeding into steel tank (gravity feed). Accompanied by Andy Thomas MRI 2. |
1472833770 | 2016-09-02 | Salt Water Injection Well | No Violations | Kilbarger has removed the packer from the well. The old packer was leaking. They purchased a new packer. The packer is a Parmaco 2.375, 8 round by 4.5 tension packer. The model number is 160901. The packer was set at 1828. They used 2.375 upset tubing to set the packer. The packer was not set. It will be set on 9-6-2016. |
1473186461 | 2016-09-06 | Salt Water Injection Well | No Violations | Compliance Notice # 595755828 Follow up inspection. Kilbarger service rig set a new Parmaco packer with shear pins at 1828 feet with 12,000 lbs tension. The injection tubing is used 2 3/8 inch 8 round. The annulus was filled with 125 gallons fresh water and 1 gallon inhibitor. The annulus capacity is 19.74 barrels. The fluid level was at approximately 300 feet prior to setting the packer. The packer was pressured up to 530 psi for 15 minutes with a loss of 5 psi. End pressure was 525. The injection tubing was on vacuum during the test. |
1476721330 | 2020-6-22 0:00: | SC | No Violations | 11.40 |
1495722630 | 2017-05-25 | Salt Water Injection Well | No Violations | Salt water injection well inspection. The well had 0 psi on the injection tubing and 31 psi on the annulus. No violations noted. |
1507168674 | 2011-08-31 | Salt Water Injection Well | No Violations | Good identification. |
1526568692 | 2018-05-15 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. Identification posted. |
1535789232 | 2012-02-23 | Salt Water Injection Well | No Violations | Grass bellow half tank with filter housing on top was bent over and had an oil residue on the ground 26 feet by 3 foot area. I called Jim Kilbarger and told him to clean up the site. Jim told me that he will have Delmer take care of it. Delmer called me and said that his guys spilled some fluid while changing a filter and that they are going to finish cleaning it up. |
1541774687 | 2018-11-08 | Salt Water Injection Well | Violations Noted | Compliance Notice # 1427204606 follow up inspection. Accompanied by UIC Supervisor. The half round tank at the unloading pad has over flowed. The contaminated area down slope of the half round tank has fresh straw on top of oil / brine contamination. Oil was observed on the ground between the 100 barrel tanks. At the well head, where the injection tubing was stacked the soil is contaminated with oil and inhibitor. Contaminated soil must be removed and taken to an EPA approved landfill. |
1548280675 | 2003-05-06 | Salt Water Injection Well | No Violations | No violations at this time. |
1563830875 | 2018-08-07 | Salt Water Injection Well | No Violations | Compliance Notice # 1427204606 follow up inspection. Kilbarger service rig is on well. Released packer and pull up 2 feet. Set packer at 1826 feet and attempt to fill annulus. Unable to fill annulus. Injection tubing is shut in with valve. The contaminated material in the containment area has been removed. The current plan for the well is to pull the tubing and packer on 8-8-18. |
1574700359 | 2010-06-24 | Salt Water Injection Well | No Violations | No violations were noted. |
1580407636 | 2020-1-28 0:00: | SW | No Violations | 8.00 |
1606263257 | 2004-09-24 | Salt Water Injection Well | No Violations | No violations. |
1619496732 | 2019-7-2 0:00:0 | SW | No Violations | 1.40 |
1621459616 | 2015-11-25 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. Annulus had slight vacuum then zero pressure. Gravity feed injection line from facility to well had zero pressure. Witnessed brine trucks unloading on the pad. |
1638470805 | 2016-03-10 | Salt Water Injection Well | Violations Noted | Inspected the unloading pad, tanks, filter skid, and annulus pressure. The half tank at the unloading pad has overflowed and oil has flowed down slope toward the tanks. Straw has been placed over the contaminated areas. All contaminated soil and material needs to be removed and taken to an EPA approved landfill. The 1/4 injection fitting on the well is too corroded to install gauge. Repair or replace 1/4 fitting to allow installation of gauge. Annulus had vacuum then zero psi. Annulus must be tested. Call inspector prior to testing the annulus. |
1650717930 | 2007-04-20 | Salt Water Injection Well | Violations Noted | An inspection revealed that a fitting will be needed on the annulus side of the well. |
1651852555 | 2006-10-06 | Salt Water Injection Well | No Violations | A inspection was conducted at the facility owned by Kilbarger Investments Inc. No violations were noted during the inspection. |
1659275288 | 2018-08-09 | Salt Water Injection Well | No Violations | I inspected this well to determine if Kilbarger had been successful in pulling the tubing and packer from this well. The tubing and packer were removed from the well but the packer was destroyed in the process of pulling the packer out. Kilbarger will be required to run a bond log before setting the new packer to determine where the top of cement is. |
1661046046 | 2007-02-15 | Salt Water Injection Well | No Violations | A follow-up inspection revealed that service rig has not moved onto this well to perform work. |
1691828432 | 2019-03-25 | Salt Water Injection Well | No Violations | Compliance notice # 1427204606 and 1541774687 follow up inspection. Oil reside has not been removed from the spill sites. The oil has absorbent material placed on top and covered with straw. Larry Howdyshell was on site and was told to remove the contaminated material from down slope of the half round tank at the unloading pad and down slope from the 100 barrel tank battery. The unloading pad drain was observed leaking at the 2 inch valve on the down slope side before the tank connection. Green dye was placed in the unloading pad drain and was observed leaking out and flowing down slope into the tank battery. Witnessed multiple brine trucks unloading during the inspection. Brine hauling logs were reviewed. |
1692728832 | 2003-03-04 | Salt Water Injection Well | No Violations | No violations at this time. |
1695129565 | 2012-01-25 | Salt Water Injection Well | No Violations | I accompanied inspector Jon Scott on this inspection. |
1708126321 | 2020-6-25 0:00: | SC | No Violations | 6.50 |
1712029995 | 2003-01-29 | Salt Water Injection Well | No Violations | No violations at this time. |
1740113642 | 2006-07-12 | Salt Water Injection Well | No Violations | No violations were noted during this inspection. |
1746598009 | 2007-03-16 | Salt Water Injection Well | No Violations | On 3/16/2007, Kilbarger Investments ran new tubing and packer into the well. A new R4 Haliburton packer was set a 1798.15 feet. A pressure test was performed on annulus between longstring and tubing. The well passed the required test. |
1752199643 | 2015-03-24 | Salt Water Injection Well | No Violations | UIC inspection, the gauge that is plugging the annulus side of the casing cannot be removed. The half tank used to catch fluid wile the filters are changed need pumped out. I contacted Larry Howdyshell who is responsible for the maintenance of the facility. Larry said the gauge would be removed and the tank pumped out by 3/27/15. |
1756202985 | 2015-09-17 | Salt Water Injection Well | No Violations | Contaminated soil has been removed below the 100 barrel steel tank valve. The valve leak has been repaired. Material has been removed from below the half tank. All contaminated material has been taken to an EPA approved landfill. |
1769329562 | 2016-05-09 | Salt Water Injection Well | No Violations | Compliance Notice # 1638470805 follow up inspection. Mechanical integrity test. Tested annulus at 325 psi for 15 minutes with no loss in pressure. |
1777427458 | 2016-05-03 | Salt Water Injection Well | No Violations | Compliance notice # 1638470805 follow up inspection with UIC Supervisor. Inspected the unloading pad, containment area, tanks, injection line, injection pressure and annulus pressure. Annulus had vacuum then zero pressure. Vegetative growth has started to establish on 3/4 of the remediated area. Some oil residue was observed under a layer of straw, on the slope between the unloading pad and the 100 barrel tanks. |
1805403672 | 2019-6-26 0:00: | SW | No Violations | 5.00 |
1813940934 | 2003-07-24 | Salt Water Injection Well | No Violations | No violations. |
1888218904 | 2010-09-27 | Salt Water Injection Well | No Violations | An inspection revealed no violations. Note: The gauge utilized for this inspection will require calibration. |
1890583420 | 2020-6-9 0:00:0 | SC | No Violations | 0.50 |
1911791636 | 2020-5-12 0:00: | SC | No Violations | 2.50 |
1929956501 | 2008-02-11 | Salt Water Injection Well | No Violations | An inspection revealed that there was no pressure on the annulus side of the well. Kilbarger was contacted by telephone and informed of the inspection results. Kilbarger states that they will place pressure on the annulus by the end of the week. |
1989879742 | 2012-03-29 | Salt Water Injection Well | No Violations | FOLLOW UP TO NOV # -869291426 Mixed fresh water and green dye and poured down the unloading pad drain. The water came out of the hillside. A 2inch rusted steel line was broken off. The unloading pad drain is not connected to a tank or vault. I called Jim Kilbarger and told him to correct this issue. He said that he will take care of it. I told him that the drain from the unloading pad must go to a tank or water tight vault for storage. |
1993822673 | 2012-02-23 | Salt Water Injection Well | No Violations | FOLLOW UP TO NOV # -1535789232 Grass below half tank with filter housing on top was bent over and had an oil residue on the ground 26 feet by 3 foot area. I called Jim Kilbarger and told him to clean up the site. Jim told me that he will have Delmer take care of it. Delmer called me and said that his guys spilled some fluid while changing a filter and that they are going to finish cleaning it up. |
200226437 | 2009-12-3 0:00: | SW | No Violations | |
2019634361 | 2014-04-09 | Salt Water Injection Well | No Violations | Inspected the unloading pad, containment dike, tanks, injection line, annulus pressure and injection pressure. Met with Tony Kilbarger on site to discuss upgrading the surface facility. We discussed the containment options. Tony said that he will work on designing a new facility and submit the plans to the UIC section. |
2041855167 | 2018-01-18 | Salt Water Injection Well | No Violations | The salt water injection well injection tubing was on vacuum and the annulus had 0 psi. I have contacted well tender Larry Howdyshell to add pressure to the annulus. |
2060452849 | 2014-05-13 | Salt Water Injection Well | No Violations | Inspected the unloading pad, tanks, containment dike, injection line, injection pressure, and annulus pressure. |
2062700710 | 2013-11-25 | Salt Water Injection Well | No Violations | Inspected unloading pad, tanks, containment dike, injection line, injection pressure, and annulus pressure. The unloading pad drain line was not draining into the 100 barrel steel tank. The 2 steel line was observed to be on top of the tank and not into the hatch where it usually is located. 1 gallon of water and marking dye was poured down the unloading pad drain. The dye was observed flowing across the top of the 100 barrel tank and onto the ground. I discussed the problem with a Kilbarger water truck driver on site. The water truck driver moved the 2 line back into the hatch. Three scald areas were observed between the half round tank with the filter housing and the well. 1st 9 by 6, 2nd 6 by 2, 3rd 3by2. I contacted Delmer Harris and he said that the injection line was damaged by a mower and the line has been repaired. I told Delmer to continue to remediate the scald areas and get vegetative growth established. I observed a clean up effort in the dike. Soil had been dug up and new material placed around one of the 100 barrel tanks. I asked Delmer about this. He confirmed that one of the tanks overflowed. We also discussed their plans to replace a couple of tanks with- in the containment dike. I witnessed two Kilbarger brine truck loads being unloaded. Both were produced water from their production wells. |
26793697 | 2017-3-20 0:00: | BH | No Violations | 3.00 |
348830415 | 2013-1-15 0:00: | SW | No Violations | 1.50 |
349627697 | 2012-3-8 0:00:0 | SW | No Violations | 1.50 |
432493261 | 2018-3-1 0:00:0 | SW | No Violations | |
474636307 | 2012-8-22 0:00: | SW | No Violations | 4.00 |
53889245 | 2004-12-14 0:00 | SW | No Violations | |
5609i210 | 2001-6-4 0:00:0 | SW | No Violations | |
5609i338 | 2001-8-20 0:00: | SW | No Violations | |
595755828 | 2016-8-29 0:00: | SW | No Violations | 3.50 |
612977728 | 2012-8-20 0:00: | SW | No Violations | 1.50 |
628501973 | 2009-6-2 0:00:0 | SW | No Violations | |
664518521 | 2013-7-3 0:00:0 | SW | No Violations | 2.00 |
738737287 | 2016-9-1 0:00:0 | AM | No Violations | |
778227111 | 2014-3-11 0:00: | SW | No Violations | 2.00 |
78190246 | 2015-6-22 0:00: | SW | No Violations | 2.50 |
810256088 | 2008-9-22 0:00: | SW | No Violations | |
882079066 | 2019-4-29 0:00: | SW | No Violations | |
94901027 | 2020-3-5 0:00:0 | SW | No Violations | |
968352752 | 2007-3-12 0:00: | SC | No Violations | |
981865674 | 2019-1-15 0:00: | SW | No Violations | 4.30 |
983318169 | 2008-9-16 0:00: | SW | No Violations | |
987662428 | 2011-12-15 0:00 | SW | No Violations | 1.00 |
iTOMK00011 | 2001-02-15 | Salt Water Injection Well | No Violations | 1051:9-3-05(A)(3) AND 1501:9-3-07 (E) |
iTOMK000114 | 2001-2-15 0:00: | SW | No Violations | |
iTOMK00013 | 2001-06-04 | Salt Water Injection Well | No Violations | 1509.23;1509.072(A); 1501:9-9-05 (A)(10)- ID AND 1/4 VALVE AND RESTORATION |
iTOMK000139 | 2001-6-4 0:00:0 | SW | No Violations | |
PL16360 | PL | No Violations | ||
UIC289 | 1987-8-12 0:00: | SW | No Violations | |
UIC290 | 1987-8-12 0:00: | SW | No Violations | |
UIC301 | 1986-12-11 0:00 | SW | No Violations | |
UIC302 | 1986-12-11 0:00 | SW | No Violations | |
UIC303 | 1986-12-11 0:00 | SW | No Violations | |
UIC304 | 1986-12-11 0:00 | SW | No Violations | |
UIC305 | 1986-12-11 0:00 | SW | No Violations | |
UIC480 | 1988-2-18 0:00: | SW | No Violations | |
UIC537 | 1988-5-20 0:00: | SW | No Violations | |
UIC910 | 1990-5-8 0:00:0 | BH | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0046836104 | US-OH-125078 | 2019-05-09 | 9-3-04(A) | Pollution/Contamination |
0046836104 | US-OH-125079 | 2019-05-09 | 9-3-05(A)6 | Contamination at surface facility (permit after 6-1-82) |
005609i210 | US-OH-126233 | 2001-06-04 | Failure to restore land surface within 9 mos. (CHANGE) (REPLACE) | |
005609i210 | US-OH-126234 | 2001-06-04 | Failure to legibly identify well | |
005609i210 | US-OH-126235 | 2001-06-04 | Violation of injection tubing/fitting requirements | |
005609i338 | US-OH-126299 | 2001-08-20 | Failure to monitor annulus pressure | |
0432493261 | US-OH-124631 | 2018-03-27 | 9-3-07(D) | Exceeding maximum allowable injection pressure |
0595755828 | US-OH-126715 | 2016-09-21 | Failure to monitor annulus pressure | |
0595755828 | US-OH-126716 | 2016-09-21 | Mechanical failure/contamination | |
0869291426 | US-OH-129893 | 2012-04-04 | Pits not liquid tight/Improper construction or use | |
0882079066 | US-OH-130036 | 2019-05-09 | Failure to file salt water injection annual report | |
1168627885 | US-OH-104468 | 2007-01-12 | Failure to legibly identify well | |
1168627885 | US-OH-104469 | 2007-01-12 | Violation of injection tubing/fitting requirements | |
1168627885 | US-OH-104470 | 2007-01-12 | Contamination at surface facility (permit after 6-1-82) | |
1168627885 | US-OH-104471 | 2007-01-12 | Failure to monitor pressures/volumes | |
1168627885 | US-OH-104472 | 2007-01-12 | Failure to monitor annulus pressure | |
1382504724 | US-OH-111369 | 2015-10-08 | Pollution/Contamination | |
1427204606 | US-OH-112460 | 2018-08-13 | 9-3-05(A)6 | Contamination at surface facility (permit after 6-1-82) |
1427204606 | US-OH-112461 | 2018-08-13 | 9-3-07(F) | Failure to monitor annulus pressure |
1541774687 | US-OH-114915 | 2018-11-16 | 9-3-04(A) | Pollution/Contamination |
1541774687 | US-OH-114916 | 2018-11-16 | 9-3-05(A)6 | Contamination at surface facility (permit after 6-1-82) |
1541774687 | US-OH-114917 | 2018-11-16 | 9-3-08(B) | Tanks not liquid tight/Improper burial |
1638470805 | US-OH-116114 | 2016-05-25 | Pollution/Contamination | |
1638470805 | US-OH-116115 | 2016-05-25 | Violation of injection tubing/fitting requirements | |
1638470805 | US-OH-116116 | 2016-05-25 | Failure to monitor annulus pressure | |
1650717930 | US-OH-116281 | 2007-05-07 | Violation of injection tubing/fitting requirements |
For data sources see[5]