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Well ID: 34-067-21210 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Moorefield Township | |
Operator Name: GULFPORT ENERGY CORPORATION | |
Well Pad ID: US-OH-001015 | |
Farm/Lease Name: PUSKARICH | |
License Status: Final Restoration | |
License Date: 2014-06-13 | |
Spud Date: 2014-07-11 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: 7870.00 ft | |
Configuration: Horizontal | |
Latitude: 40.200000 | |
Longitude: -81.160000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2013-06-17 | Proposed Formations:TRENTON, Issued Date:6/17/2013, Expired Date:6/17/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2014-06-13 | Proposed Formations:UTICA/POINT PLEASANT, Issued Date:6/13/2014, Expired Date:6/12/2016 12:00:00 PM, Drilling unit acres:354.4, Proposed Well Type:OG, Proposed Well Class:POOL |
Plugged/Abandoned | 2014-09-02 | LOST HOLE |
Construction Permit Expires | 2016-06-12 | LOST HOLE |
Record Last Modified | 2017-10-23 | LOST HOLE |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1161267781 | 2014-8-4 0:00:0 | DD | No Violations | |
-1684437113 | 2014-9-2 0:00:0 | PB | No Violations | |
-1783509341 | 2014-8-29 0:00: | DD | No Violations | |
-2122160744 | 2014-9-2 0:00:0 | PB | No Violations | 1.50 |
0706766982 | 2015-08-14 | Final Restoration | No Violations | This well has been plugged to surface on 9/02/2014 and Nick Berelsman called to advise that the permit number is now attached to the top of the well casing. It has been cut off below ground level and the tin horn has been pulled and filled to surface. Meets requirements for restoration final. |
1161267781 | 2014-08-04 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found Sidewinder Rig # 60. attempting to recover 450 feet of drill pipe and the drill assembly. The tool joint broke when completing the drilling process. |
1405129720 | 2014-07-11 | Casing String Witnessed | No Violations | Upon arrival on location I found Sidewinder Rig 60 installing 13 3/8 inch diameter casing to the depth of 320 feet CalFrac will cement to surface. It was determined that Gulfport was not following the casing program approved by the permitting section. After discussions with the Divison Management, it was determined that Gulfports proposed casing program met all well construction requirements and approval was granted to continue with installation of the 13 3/8 inch casing. Gulfport is to contact the permitting section on Monday July 14, 2014 for a revised drilling permit. |
1406036315 | 2014-07-22 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found Sidewinder Rig # 60 drilling ahead to the depth of 7304 feet, of 8 1/2 inch diameter hole. They have encountered some lost circulation problems. They are preparing to mix more lost circulation material in there drilling mud. |
1406554180 | 2014-07-28 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found Sidewinder Rig # 60 at a depth of 15002 feet and a 8 1/2 inch hole. The rig will TD today at a depth of 15330 feet and will set casing at a depth od 15316 feet. |
1407382425 | 2014-08-06 | Plug / Plug Back | No Violations | On the day of my inspection I found Sidewinder Rig 60 preparing to plug back across the clinton formation. A 450 foot drill pipe and drill assembly was lost in the hole at 6686 feet. Several attempts were make to retrieve the tools, the attempts were unsuccessful. It was decided to plug back across the clinton formation. The bottom of the plug was set at 6692 feet. A 600 foot plug was set to seal across the formation and to use as kickoff point to drill around the drill assembly, and reenter the existing well bore. |
1408449791 | 2014-08-18 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found Sidewinder Rig # 60 has successfully reentered the original wellbore, at 7153 feet and drilled ahead to 7155 feet. They were tripping out of the hole and going to trip back into the hole with a 8 1/2 inch tricone bit, and clean out the wellbore to the original total depth. |
1409369261 | 2014-08-26 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found the Sidewinder Rig 60 was attempting to retrieve drill pipe and bit that was left in wellbore, total pipe left in the wellbore was 3705 feet. |
1409509760 | 2014-08-31 | Plug / Plug Back | No Violations | On the day of my inspection I found Sidewinder Rig 60 preparing to run a inflatable packer. It is a Baker Hughes PIP 7 inch outside diameter to 13 1/4 inch outside diameter. It was set at 7885 feet deep. A washout or other diameter difference would not let us to set packer at 7880 feet. It could be set at 7885 feet. Plug #1 set at 7860 feet to 7360 feet. Circulation was established and cement was pumped. |
1684437113 | 2014-09-02 | Plug / Plug Back | No Violations | On the day of my inspection Gulfport continued to plug and abandon the well. 2 3/8 tubing was run to the depth of 300 feet to cement the top section to the surface. Circulation was established and cement was pumped into the wellbore and brought to the surface. Tubing was laid down and the well was topped off. |
1783509341 | 2014-08-29 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I was accompanied by District Supervisor Brent Bear. We found that Sidewinder Rig 60 was preparing to plug and abandon the well. A cement bond log was run. I left location and will return when they are ready to set a inflatable packer. Upon returning to location Sidewinder Rig 60 was running the inflatable packer to the depth of 7880 feet. An attempt to set the packer failed, pushing the packer down the hole to J off of it. Then will run back in the well with a different packer. |
1915519082 | 2014-08-28 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found that Sidewinder Rig 60 was continuing to attempt to retrieve drill pipe and bit. It was determined that they had grabbed on the fish and was pulling the pipe out of the wellbore. |
2093910010 | 2016-12-02 | Production Wells | No Violations | I am on site today to perform a routine status check of the well bore and the well location. On the day of my inspection I witnessed the lease load was in good repair, however slight erosion was noticed at the beginning of the lease road and the gates for the location were locked. After inspecting the well bore I discovered no high annular pressures and that the well was in producing order. With the inspection I did not discover any indications of pollution or contamination. |
2122160744 | 2014-09-02 | Plug / Plug Back | No Violations | On the date of inspection I accompanied ODNR Inspector Randy Akins to witness the top plug of the well. Refer to Randy Akins report for further details. |
706766982 | 2015-8-14 0:00: | FR | No Violations | 1.50 |
For data sources see[3]