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34-067-21031

Well Details

Well ID: 34-067-21031
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Country: United States
State: Ohio
County: Harrison
Municipality: Green Township
Operator Name: COAL GAS TRANSPORTATION LLC
Well Pad ID:
Farm/Lease Name: CBM OHIO
License Status: Plugged and Abandoned
License Date: 2015-12-07
Spud Date: 2007-10-12
Spud Drilling Contractor: G & L DRILLING
Final Drill Date: 2007-10-15
Well Total Depth: 520.00 ft
Configuration: Vertical
Latitude: 40.290000
Longitude: -80.940000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-09-19 Proposed Formations:LOWER FREEPORT 6A COAL, Issued Date:9/19/2007, Expired Date:9/18/2008 6:00:00 AM, Drilling unit acres:1, Proposed Well Type:CM, Proposed Well Class:POOL
Completed 2007-10-15 GMM CHANGED TO PA STATUS PER PLUG REPORT
Reached Total Depth 2007-10-15 GMM CHANGED TO PA STATUS PER PLUG REPORT
Completion Report Received 2008-02-05 GMM CHANGED TO PA STATUS PER PLUG REPORT
Change of Owner 2008-12-29 Operator changed from 5319, LAHD ENERGY INC to 8454, COAL GAS TRANSPORTATION LLC
APP 2015-12-07 Proposed Formations:LOWER FREEPORT 6A COAL SEAM, Issued Date:12/7/2015, Expired Date:12/6/2017 12:00:00 PM, Drilling unit acres:1, Proposed Well Type:CM, Proposed Well Class:
Plugged/Abandoned 2016-03-28 GMM CHANGED TO PA STATUS PER PLUG REPORT
Construction Permit Expires 2017-12-06 GMM CHANGED TO PA STATUS PER PLUG REPORT
Record Last Modified 2019-06-05 GMM CHANGED TO PA STATUS PER PLUG REPORT

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0 NOT PERFED OR TREATED

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 COAL GAS TRANSPORTATION LLC 0.00 0.00 31
2009 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2010 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2011 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2012 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2013 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2014 COAL GAS TRANSPORTATION LLC 0.00 0.00 0
2015 COAL GAS TRANSPORTATION LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 COAL GAS TRANSPORTATION LLC Brine 0 31
2009 COAL GAS TRANSPORTATION LLC Brine 0 0
2010 COAL GAS TRANSPORTATION LLC Brine 0 0
2011 COAL GAS TRANSPORTATION LLC Brine 0 0
2012 COAL GAS TRANSPORTATION LLC Brine 0 0
2013 COAL GAS TRANSPORTATION LLC Brine 0 0
2014 COAL GAS TRANSPORTATION LLC Brine 0 0
2015 COAL GAS TRANSPORTATION LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1225260294 2019-9-10 0:00: FR No Violations 1.00
-1623657258 2016-3-15 0:00: PB No Violations 1.00
-16544163 2008-1-29 0:00: PW No Violations 0.50
-2122900246 2018-2-8 0:00:0 FR No Violations 1.00
-523569905 2016-7-13 0:00: FR No Violations 0.50
-92913078 2017-4-26 0:00: FR No Violations 1.00
0016544163 2008-01-29 Production Wells No Violations Inspection revealed no violations at this time. Note: Coal Bed Methane well.
0092913078 2017-04-26 Final Restoration No Violations On the day of my inspection I was unable to locate a well at the given coordinates. Previous inspection reports indicate well was plugged in march 2016 and has a plugging report in RBDMS. A building remains onsite with 2 horizontal seperators and a meter inside. Final restoration cannot be approved until remaining equipment is removed and area is then vegetated.
0499314264 2013-07-29 Preliminary Restoration No Violations Everything passed according to 1509.072A.
0523569905 2016-07-13 Final Restoration No Violations On the day of my inspection the final restoration could not be passed due to the location still needs to be graded.
0535791964 2016-03-29 Plug / Plug Back No Violations I arrived on site accompanied by inspector Mark Moreland and witnessed that the cement (from the plug job performed on the previous day) had settled 10 feet below ground level. I then called Mark Clark to inform him that the hole would need to be filled back to surface before cutting the 7 inch diameter surface casing. Mark stated he planned to accomplish that task tomorrow. I will be back on site to witness the cutting of the surface casing.
1253854974 2007-10-22 Drill / Deepen / Reopen No Violations Inspection revealed that the drilling pits have been closed and the location has been final graded . No violations at this time.
1459510786 2016-03-28 Plug / Plug Back No Violations The rig ran 1-1/2 tubing and tagged the mechanical bridge plug set at 395. They pulled up to the first collat at 385. Cemenco Services cemented the well with 72 sacks of Class A cement. Good cement was returned to the surface. It dropped back ~ 10 when they pulled the tubing. Rigged down and movwed off.
1525463276 2020-10-5 0:00: PW No Violations 1.00
1623657258 2016-03-15 Plug / Plug Back No Violations I am on site accompanied by Inspector Mark Moreland to check on the static test of the well bore. A bridge plug was place inside the 7 inch diameter casing the previous day, in preparation for plugging the well bore. After the bridge plug was set the hole was then filled with fresh water to test the integrity of the bridge plug. On the day of my inspection I found that the bridge plug held indicating that the well could then be filled to surface with cement.
1751963887 2016-03-30 Plug / Plug Back No Violations
1958767890 2019-7-1 0:00:0 FR No Violations 1.00
2122900246 2018-02-08 Final Restoration No Violations On the day of my inspection I am performing a follow up to Chiefs Order 2017-414 issued on 10-31-17 for liability insurance. This well has been plugged but equipment remains on site and a final restoration cannot be passed. A building remains that was used to house compressors. All associated lines remain along with a meter box.
499314264 2013-7-29 0:00: PL No Violations 1.00
510624956 2020-5-8 0:00:0 PW No Violations 1.00
535791964 2016-3-29 0:00: PB No Violations 2.00

For data sources see[8]

References