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Well ID: 34-067-20857 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Londonderry Township | |
Operator Name: BIG SKY ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: BARDALL | |
License Status: Producing | |
License Date: 1988-07-08 | |
Spud Date: 1988-10-15 | |
Spud Drilling Contractor: ENTERPRISE DRLG | |
Final Drill Date: 1988-10-22 | |
Well Total Depth: 6067.00 ft | |
Configuration: Vertical | |
Latitude: 40.170000 | |
Longitude: -81.300000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1988-07-08 | 213 LOMAK OPERATING CO GeoDate 7/8/88 |
Oil and Gas | 1988-07-08 | Issued Date 7/8/88 Expired Date 7/8/89 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 06067 Proposed Drill Depth 06067 |
Original Spud | 1988-10-15 | |
Completed | 1988-10-22 | |
Reached Total Depth | 1988-10-22 | |
Completion Report Received | 1988-12-23 | |
Construction Permit Expires | 1989-07-08 | |
CO | 1992-07-15 | 3847 HALL & HORNING SERV INC GeoDate 7/8/88 |
Change of Owner | 2010-02-24 | Operator changed from 3847, HALL & HORNING SERV INC to 1333, BIG SKY ENERGY INC |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5773 | 5960 | 0 |
5773 | 5960 | 0 | |
2006-09-11 | 5816 | 5902 | 41 |
5816 | 5902 | 41 | |
5773 | 5960 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 95200 Gal | 80000 | FRAC:GELLED WATER/SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1990 | RANGE OPERATING COMPANY | 6655.00 | 88.00 | 153 |
1991 | RANGE OPERATING COMPANY | 10718.00 | 97.00 | 365 |
1992 | RANGE OPERATING COMPANY | 4389.00 | 86.00 | 182 |
1993 | TEMPLE OIL & GAS CO | 8353.00 | 95.00 | 365 |
1994 | HALL & HORNING SERV INC | 6797.00 | 94.00 | 365 |
1995 | HALL & HORNING SERV INC | 6761.00 | 0.00 | 365 |
1996 | HALL & HORNING SERV INC | 5814.00 | 74.00 | 366 |
1997 | HALL & HORNING SERV INC | 5684.00 | 85.00 | 365 |
1998 | HALL & HORNING SERV INC | 4706.00 | 0.00 | 365 |
1999 | HALL & HORNING SERV INC | 4202.00 | 82.00 | 365 |
2000 | HALL & HORNING SERV INC | 3980.00 | 0.00 | 365 |
2001 | HALL & HORNING SERV INC | 3081.00 | 0.00 | 365 |
2002 | HALL & HORNING SERV INC | 2664.00 | 0.00 | 365 |
2003 | HALL & HORNING SERV INC | 2277.00 | 0.00 | 365 |
2004 | HALL & HORNING SERV INC | 2672.00 | 0.00 | 365 |
2005 | HALL & HORNING SERV INC | 2157.00 | 0.00 | 365 |
2006 | HALL & HORNING SERV INC | 1841.00 | 0.00 | 365 |
2007 | HALL & HORNING SERV INC | 1437.00 | 0.00 | 365 |
2008 | HALL & HORNING SERV INC | 1419.00 | 0.00 | 366 |
2009 | HALL & HORNING SERV INC | 922.00 | 0.00 | 365 |
2011 | BIG SKY ENERGY INC | 1651.00 | 0.00 | 365 |
2012 | BIG SKY ENERGY INC | 2401.00 | 0.00 | 366 |
2013 | BIG SKY ENERGY INC | 1162.00 | 0.00 | 365 |
2014 | BIG SKY ENERGY INC | 1528.00 | 0.00 | 365 |
2016 | BIG SKY ENERGY INC | 9.00 | 0.00 | 28 |
2017 | BIG SKY ENERGY INC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1162460718 | 2018-7-26 0:00: | PW | No Violations | 2.00 |
-123528797 | 2016-4-14 0:00: | PW | No Violations | 2.50 |
-1321605896 | 2018-8-21 0:00: | PW | No Violations | 1.00 |
-1726763810 | 2016-9-21 0:00: | PW | No Violations | 3.00 |
-1978004199 | 2018-6-18 0:00: | PW | No Violations | 1.00 |
-574956652 | 2006-4-18 0:00: | PW | No Violations | 1.00 |
-871575278 | 2019-8-7 0:00:0 | PW | No Violations | 1.00 |
0123528797 | 2016-04-14 | Production Wells | No Violations | On the day of my inspection accompanied by inspector Mark Moreland, I witnessed that the tank battery consisted of a 210bbl tank, 50bbl brine tank, a horizontal separator and sales meter with a chart that dated back to the year 2015. The line pressure and the differential pressure on the chart are at zero psi. This indicates that the well is not in production. The well was equipped with 4.5 inch diameter production casing, 1.5 inch diameter production tubing and a plunger lift system. A patch was placed on the 1.5 inch diameter production tubing directly above the slips on the well head and gas could be heard coming from the patch at the time of my inspection. |
0574956652 | 2006-04-18 | Production Wells | No Violations | Routine inspection revealed no violations at this time . The tank battery consists of one 210 bbl oil storage tank and one plastic brine storage tank . The SPCC dike meets the requirements . Note: Had to walk into the wellsite because there was a gate across the lease road . |
1045781965 | 2020-4-15 0:00: | PW | No Violations | 1.00 |
1162460718 | 2018-07-26 | Production Wells | No Violations | Follow up to Compliance notice 1528999605 for well leaking gas. Well also has a landowner complaint for leaking gas #5434. On the day of my inspection this plunger lift well is equipped with 4.5 inch diameter casing, 1.5 inch diameter tubing and a motor valve. An audible gas leak can be heard and well appears to be leaking gas at the packing or the 1.5 inch tubing. There is a band clamp on tubing. Gas did not register on Tango or Ventis units. Valve on casing is partially open to regulators, and tubing valve is open. Motor valve is closed. Production equipment includes a 210 barrel steel tank, a 42 barrel poly tank, horizontal seperator, and a meter box with a 1 inch diameter sales line orfice. Meter box has an old chart and does not appear to be in production. |
1287830908 | 2020-8-17 0:00: | PW | No Violations | 1.00 |
1321605896 | 2018-08-21 | Production Wells | No Violations | Follow up to Compliance notice 1528999605 for well leaking gas. Well also has a landowner complaint for leaking gas #5434. On the day of my inspection this plunger lift well is equipped with 4.5 inch diameter casing, 1.5 inch diameter tubing and a motor valve. An audible gas leak can be heard and well appears to be leaking gas at the packing or the 1.5 inch tubing. There is a band clamp on tubing. No H2S registered on Tango unit. Valve on casing is partially open to regulators, and tubing valve is open. Motor valve is closed. Production equipment includes a 210 barrel steel tank, a 42 barrel poly tank, horizontal seperator, and a meter box with a 1 inch diameter sales line orfice. Meter box has an old chart and does not appear to be in production. Enforcement section is currently reviewing case. |
1392048989 | 2014-02-10 | Production Wells | No Violations | On the day of my inspection the ground was snow covered and I witnessed that the tank battery consisted of a 210bbl tank, 50bbl brine tank, a horizontal separator, a sales meter with a 1 inch orifice, all valves open, and a leak was found on the sales line with a current chart dated 2/4/14. The lease road was washed out and gated. The well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system logically controlled with the valve open on the tubing and the flow line. |
1528999605 | 2018-06-14 | Production Wells | Violations Noted | On the day of my inspection I am following up on complaint 5434. Landowner originally complained about the well not producing and it is leaking gas. Emergency Operations Jason Blocker accompanied me during this inspection. This plunger lift well is equipped with 4.5 inch diameter casing, 1.5 inch diameter tubing and a motor valve. An audible gas leak can be heard and well appears to be leaking gas at the packing or the 1.5 inch tubing. There is a band clamp on tubing. Gas did not register on Tango or Ventis units. Valve on casing is partially open to regulators, and tubing valve is open. Production equipment includes a 210 barrel steel tank, a 42 barrel poly tank, horizontal seperator, and a meter box with a 1 inch diameter sales line orfice. Meter box has an old chart and does not appear to be in production. Well should be shut in due to the Temporary Restraining Order issued by Trumbull County Court of Common Pleas, Chiefs Order 2015-535, Chiefs Order #2016-105, Chiefs Order 2016-172, and Chiefs Order 2014-43. |
1530024181 | 2018-06-26 | Production Wells | No Violations | On the day of my inspection I found the well still leaking gas from the tubing or packing. Follow up to my last inspection to verify that the motor valve is closed on the well. Inspection revealed that the motor valve is currently closed and well is not in production. |
1565026001 | 2019-8-7 0:00:0 | PW | No Violations | 0.50 |
1573047745 | 2019-10-22 0:00 | PW | No Violations | 1.00 |
1726763810 | 2016-09-21 | Production Wells | No Violations | On the day of my inspection following up on complaint number 5434 which was a complaint by landowners Rick and Judy Luyster who were concerned about the well not being in production and not providing domestic gas. Rick and Judy stated that they would just like to see the well plugged. Prior to my inspection I met with Rick and Judy. They informed me that the gas to the house was shut off years ago when the gas turned sour and declared unsafe for domestic use. With the conduction of my inspection I witnessed the tank battery consisted of a 210bbl tank, 50bbl brine tank, a horizontal separator and sales meter with a chart that dated back to the year 2015. The line pressure and the differential pressure on the chart are at zero psi. This indicates that the well is not in production. The well was equipped with 4.5 inch diameter production casing, 1.5 inch diameter production tubing and a plunger lift system. A patch was placed on the 1.5 inch diameter production tubing directly above the slips on the well head and gas could be heard coming from the patch at the time of my inspection. I informed Rick I would speak to my supervisor about the well and see what can be done to help resolve the issues they are facing. |
1800935146 | 2014-04-28 | Production Wells | No Violations
-43, I witnessed that the production equipment included a 210bbl tank, 50bbl brine tank, a horizontal separator, a 2 inch sales meter with a 1 inch orifice and chart recorder with all valves open on the sales line. The well was equipped with 4.5 inch casing, 1.5 inch tubing, a plunger lift system logically controlled with the valve open on the tubing and the flow line. Identification is present and production records are current through 2012. | |
1978004199 | 2018-06-18 | Production Wells | No Violations | On the day of my inspection I was accompanied by Inspector Pat Shrieve. We viewed the well and production equipment. Valves on well and seperator are open, need to return and check whether motor valve is open. 210 barrel steel tank is estimated to be half full. Call was placed to Big Sky on 6/20/18 and I asked if he could get the leak fixed. He said that he is not allowed to operate the wells but would try and get someone to fix it. |
2025302182 | 2018-06-18 | Production Wells | No Violations
-working logic box at the well. The tank site consists of [1]210-barrel steel tank, [1] 1100-gallon plastic tank and a horizontal separator. The valves are open and are sweating down- stream from the 1- inch orifice plate. The chart has not been changed in some time and the wind- up clock may not be working in the chart meter. The production equipment is enclosed within an earthen impoundment. The identification is not legible but is posted on the tank. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1528999605 | US-OH-114655 | 2018-06-26 | Well insufficiently equipped to prevent escape of oil and gas |
For data sources see[9]