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Well ID: 34-067-20518 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Freeport Township | |
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL | |
Well Pad ID: | |
Farm/Lease Name: CLAY W | |
License Status: Final Restoration | |
License Date: 2017-08-23 | |
Spud Date: 1982-02-28 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1982-03-02 | |
Well Total Depth: 6160.00 ft | |
Configuration: Vertical | |
Latitude: 40.210000 | |
Longitude: -81.250000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-02-18 | Issued Date 2/18/82 Expired Date 8/17/82 Acres 0050700 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06160 Proposed Drill Depth 06160 |
Original Spud | 1982-02-25 | |
Completed | 1982-03-02 | |
Reached Total Depth | 1982-03-02 | |
CO | 1982-04-19 | 168 RED HILL DEVELOPMENT GeoDate 2/18/82 |
Completion Report Received | 1984-01-30 | |
APP | 2014-08-12 | Proposed Formations:ORISKANY, Issued Date:8/12/2014, Expired Date:8/11/2016 12:00:00 PM, Drilling unit acres:50.75, Proposed Well Type:OG, Proposed Well Class:ESPW |
APP | 2017-08-23 | Proposed Formations:CLINTON, Issued Date:8/23/2017, Expired Date:8/23/2019 12:00:00 PM, Drilling unit acres:50.75, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-03-01 | |
Record Last Modified | 2018-11-29 | |
Construction Permit Expires | 2019-08-23 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5958 | 6052 | 1 |
5958 | 6052 | 1 | |
5958 | 6052 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 16500 Gal | 0 | FRAC: FOAM |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1101905512 | 2016-7-28 0:00: | PW | No Violations | 1.00 |
-1607633603 | 2018-2-28 0:00: | PB | No Violations | 3.00 |
0989667477 | 2018-09-19 | Final Restoration | No Violations | On the day of my inspection I found this well has been plugged. Area is graded and vegetated. Roadway remains. Plugging report in RBDMS. Landowner waiver emailed to me. Site meets requirements for final restoration. |
1101905512 | 2016-07-28 | Production Wells | No Violations | On the day of my inspection, I witnessed this is a plunger- lift system well, using 2 inch diameter production tubing placed inside 4.5 inch diameter production casing. The plunger is being operated by a motor valve. Production equipment for this well includes a 100 bbl. production tank, a horizontal separator and a 2 inch diameter meter run; all placed inside an earth dike that measures approximately 30*40 feet at an average height of 4 foot. Proper identification was in place on the tank battery at the time of my inspection. RBDM records indicate the well is in producing order. I was unable to record the coordinate, due to my GPS dying prior to my arrival. |
1519937486 | 2018-03-01 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Kimbles service rig had ran 1.9 inch diameter tubing to a depth of 4280. Petroset is onsite to plug the well out. Cement is Class A with 2% cacl, 1.36 yield, and 14.6 pounds per gallon. First plug set was a 50 sack Big Lime plug from 4280-4080, displaced with 11 barrels of brine. Second plug set was a 50 sack surface casing plug from 1516-1316, displaced with 3.5 barrels of freshwater. Appalachian set a wire line bridge plug at 1300 feet. Final plug set was from 400 to surface. 165 sacks of cement pumped with returns to surface. |
1607633603 | 2018-02-28 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed Petroset pump a 30 sack bottom plug. Kimbles service rig ran 1.9 inch diameter tubing to 5890 feet. Perforations from 5958-6052 feet. Loggers total depth of hole is 6160 feet. This bottom plug is a 300 foot isolation plug. Plug location should be 5890-5600. Class A cement with 2% CaCl and a yield of 1.36. 14.6 pounds per gallon. Displaced with 14 barrels of fresh water. |
989667477 | 2018-9-19 0:00: | FR | No Violations | 1.00 |
For data sources see[9]