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34-067-20403

Well Details

Well ID: 34-067-20403
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Country: United States
State: Ohio
County: Harrison
Municipality: Freeport Township
Operator Name: RHDK OIL & GAS LLC/DBA RED HIL
Well Pad ID:
Farm/Lease Name: MCCONNELL GEORGE
License Status: Final Restoration
License Date: 2014-06-12
Spud Date: 1981-04-28
Spud Drilling Contractor:
Final Drill Date: 1981-05-03
Well Total Depth: 5935.00 ft
Configuration: Vertical
Latitude: 40.200000
Longitude: -81.300000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-11-05 168 RED HILL DEVELOPMENT GeoDate 11/5/80
Oil and Gas 1980-11-05 Issued Date 11/5/80 Expired Date Acres 0083900 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05935 Proposed Drill Depth 05935
Original Spud 1981-04-28
Completed 1981-05-03
Reached Total Depth 1981-05-03
Completion Report Received 1982-08-31
APP 2014-06-12 Proposed Formations:CLINTON, Issued Date:6/12/2014, Expired Date:6/11/2016 12:00:00 PM, Drilling unit acres:83.919, Proposed Well Type:TAAD, Proposed Well Class:
Plugged/Abandoned 2014-12-09
Last Compliance Report 2015-01-05
Construction Permit Expires 2016-06-11
Record Last Modified 2017-02-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5702 5769 6
5702 5769 6
5702 5769 6

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 75600 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RHDK OIL & GAS LLC/DBA RED HIL 2458.00 0.00 0
1985 RHDK OIL & GAS LLC/DBA RED HIL 1621.00 58.00 365
1986 RHDK OIL & GAS LLC/DBA RED HIL 1806.00 0.00 365
1987 RHDK OIL & GAS LLC/DBA RED HIL 1467.00 0.00 365
1988 RHDK OIL & GAS LLC/DBA RED HIL 1346.00 104.00 365
1989 RHDK OIL & GAS LLC/DBA RED HIL 1228.00 0.00 365
1990 RHDK OIL & GAS LLC/DBA RED HIL 1263.00 0.00 365
1991 RHDK OIL & GAS LLC/DBA RED HIL 1062.00 0.00 365
1992 RHDK OIL & GAS LLC/DBA RED HIL 713.00 81.00 365
1993 RHDK OIL & GAS LLC/DBA RED HIL 661.00 0.00 365
1994 RHDK OIL & GAS LLC/DBA RED HIL 657.00 0.00 365
1995 RHDK OIL & GAS LLC/DBA RED HIL 554.00 0.00 365
1996 RHDK OIL & GAS LLC/DBA RED HIL 575.00 0.00 365
1997 RHDK OIL & GAS LLC/DBA RED HIL 711.00 68.00 365
1998 RHDK OIL & GAS LLC/DBA RED HIL 1067.00 0.00 365
1999 RHDK OIL & GAS LLC/DBA RED HIL 276.00 97.00 365
2010 RHDK OIL & GAS LLC/DBA RED HIL 0.00 0.00 365
2011 RHDK OIL & GAS LLC/DBA RED HIL 57.00 0.00 365
2012 RHDK OIL & GAS LLC/DBA RED HIL 8.00 0.00 366
2014 RHDK OIL & GAS LLC/DBA RED HIL 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 0
1985 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1986 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1987 RHDK OIL & GAS LLC/DBA RED HIL Brine 50 365
1988 RHDK OIL & GAS LLC/DBA RED HIL Brine 40 365
1989 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1990 RHDK OIL & GAS LLC/DBA RED HIL Brine 130 365
1991 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1992 RHDK OIL & GAS LLC/DBA RED HIL Brine 25 365
1993 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1994 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1995 RHDK OIL & GAS LLC/DBA RED HIL Brine 48 365
1996 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1997 RHDK OIL & GAS LLC/DBA RED HIL Brine 50 365
1998 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
1999 RHDK OIL & GAS LLC/DBA RED HIL Brine 20 365
2010 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 365
2011 RHDK OIL & GAS LLC/DBA RED HIL Brine 46 365
2012 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 366
2014 RHDK OIL & GAS LLC/DBA RED HIL Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1559629148 2014-12-9 0:00: PB No Violations 2.00
-2093161887 2014-12-5 0:00: PB No Violations 1.50
-830177238 2003-2-10 0:00: PW No Violations
0830177238 2003-02-10 Production Wells No Violations status check
1417620283 2014-12-03 Plug / Plug Back No Violations I arrived today to witness them shoot off the 1-1/2 inch diameter tubing. Appalachian Well service shot off the tubing at 5640 ft. and Nicks Well Plugging pumped 25 sacks of class A cement from 5640 ft. to 5440 ft. .Nicks Well pulled up above 4800 ft. so that Appalachian Well service could shoot the 4-1/12 inch diameter casing with 10 shots spread out over 10 ft. The shot could not get out the bottom of the tubing and after trying to drop through it was decided that the tubing would need to come out. The tubing was tripped out and because it was not in great shape another string will need to be delivered. Appalachian Well then went back down inside the 4-1/2 inch casing and shot the casing at 4800 ft. with 10 shots spread over 10 ft. Tubing will not be on site until morning so the plugging operation is shut down until the tubing can arrive.
1435837709 2015-07-01 Final Restoration No Violations Location has met the 1509.072B requirements.
1559629148 2014-12-09 Plug / Plug Back No Violations On the date of inspection I accompanied ODNR Inspector Mark Moreland to witness the top two plugs set into the well. Refer to Mark Morelands report for further details.
2093161887 2014-12-05 Plug / Plug Back No Violations I am on site today to see if Nicks Well Plugging Service can rip the 4-1/2 inch diameter casing. H2S gas has rotted the top of the casing off at the well head. It may be apart down the hole in more than one area. They are trying to rip the casing without picking up to pull stretch due to the lack of integrity. After they get the casing ripped they will pull it all out of the hole and go back in with 2-3/8 inch diameter tubing. The remaining plugs will be set using tubing.

For data sources see[9]

References