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34-067-20135

Well Details

Well ID: 34-067-20135
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Country: United States
State: Ohio
County: Harrison
Municipality: Monroe Township
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name: KILDOW
License Status: Final Restoration
License Date: 2016-04-27
Spud Date: 1972-03-01
Spud Drilling Contractor: FLANIGAN BROS
Final Drill Date: 1972-06-29
Well Total Depth: 5575.00 ft
Configuration: Vertical
Latitude: 40.380000
Longitude: -81.250000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1972-01-06 43 RESOURCE AMERICA INC GeoDate 1/6/72
Original Spud 1972-03-01 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE
Completed 1972-06-29 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE
Reached Total Depth 1972-06-29 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE
Completion Report Received 1972-07-24 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE
Change of Owner 2004-03-12 Operator changed from 43, RESOURCE AMERICA INC to 6867, ATLAS AMERICA INC
Change of Owner 2011-01-27 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
Change of Owner 2011-02-08 Operator changed from 6867, ATLAS AMERICA LLC to 6866, ATLAS NOBLE LLC
APP 2016-04-27 Proposed Formations:CLINTON, Issued Date:4/27/2016, Expired Date:4/27/2018 12:00:00 PM, Drilling unit acres:135.348, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-06-02 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE
Record Last Modified 2017-02-16 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE
Construction Permit Expires 2018-04-27 WELL PLUGGED PER INSPECTION REPORT, STATUS UPDATED, AWAITING FINAL RESTORATION-08/08/2016 ALE

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5401 5405 0
2000-02-07 5391 5448 25
5391 5448 25
5401 5405 0
5391 5448 25
2006-09-11 5444 5448 0
2006-09-11 5411 5424 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2200 Bbl 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC 410.00 561.00 365
1985 RESOURCE AMERICA INC 27.00 486.00 365
1987 RESOURCE AMERICA INC 0.00 710.00 365
1988 RESOURCE AMERICA INC 0.00 400.00 365
1989 RESOURCE AMERICA INC 0.00 527.00 365
1990 RESOURCE AMERICA INC 0.00 463.00 365
1993 RESOURCE AMERICA INC 0.00 400.00 365
1994 RESOURCE AMERICA INC 0.00 307.00 239
1995 RESOURCE AMERICA INC 0.00 485.00 365
1996 RESOURCE AMERICA INC 0.00 340.00 365
1997 RESOURCE AMERICA INC 0.00 430.00 365
1998 RESOURCE AMERICA INC 0.00 375.00 365
1999 RESOURCE AMERICA INC 0.00 453.00 365
2000 RESOURCE AMERICA INC 0.00 234.00 365
2001 RESOURCE AMERICA INC 0.00 282.00 365
2002 RESOURCE AMERICA INC 0.00 464.00 365
2003 RESOURCE AMERICA INC 0.00 303.00 365
2004 CHEVRON APPALACHIA LLC 0.00 275.00 365
2005 CHEVRON APPALACHIA LLC 0.00 288.00 365
2006 CHEVRON APPALACHIA LLC 0.00 207.00 365
2007 CHEVRON APPALACHIA LLC 0.00 224.00 365
2008 CHEVRON APPALACHIA LLC 0.00 292.00 366
2009 CHEVRON APPALACHIA LLC 0.00 223.00 365
2010 ATLAS NOBLE LLC 0.00 69.00 365
2011 CHEVRON APPALACHIA LLC 0.00 142.00 365
2012 ATLAS NOBLE LLC 0.00 363.00 366
2013 ATLAS NOBLE LLC 0.00 358.00 365
2014 ATLAS NOBLE LLC 0.00 273.00 365
2015 ATLAS NOBLE LLC 0.00 0.00 58
2016 ATLAS NOBLE LLC 0.00 0.00 366

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RESOURCE AMERICA INC Brine 0 365
1985 RESOURCE AMERICA INC Brine 192 365
1987 RESOURCE AMERICA INC Brine 0 365
1988 RESOURCE AMERICA INC Brine 0 365
1989 RESOURCE AMERICA INC Brine 0 365
1990 RESOURCE AMERICA INC Brine 74 365
1993 RESOURCE AMERICA INC Brine 0 365
1994 RESOURCE AMERICA INC Brine 0 239
1995 RESOURCE AMERICA INC Brine 0 365
1996 RESOURCE AMERICA INC Brine 0 365
1997 RESOURCE AMERICA INC Brine 0 365
1998 RESOURCE AMERICA INC Brine 130 365
1999 RESOURCE AMERICA INC Brine 36 365
2000 RESOURCE AMERICA INC Brine 0 365
2001 RESOURCE AMERICA INC Brine 0 365
2002 RESOURCE AMERICA INC Brine 32 365
2003 RESOURCE AMERICA INC Brine 0 365
2004 CHEVRON APPALACHIA LLC Brine 30 365
2005 CHEVRON APPALACHIA LLC Brine 0 365
2006 CHEVRON APPALACHIA LLC Brine 0 365
2007 CHEVRON APPALACHIA LLC Brine 0 365
2008 CHEVRON APPALACHIA LLC Brine 0 366
2009 CHEVRON APPALACHIA LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 CHEVRON APPALACHIA LLC Brine 57 365
2012 ATLAS NOBLE LLC Brine 94 366
2013 ATLAS NOBLE LLC Brine 223 365
2014 ATLAS NOBLE LLC Brine 375 365
2015 ATLAS NOBLE LLC Brine 275 58
2016 ATLAS NOBLE LLC Brine 60 366

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1593327318 2016-5-18 0:00: PW No Violations 2.00
-1914921737 2016-7-8 0:00:0 FR No Violations 1.00
-2083781482 2015-4-7 0:00:0 PW No Violations 0.50
-820446621 2016-5-31 0:00: PW No Violations 1.00
-935582158 2016-5-23 0:00: PW No Violations 1.00
0008663027 2016-05-31 Plug / Plug Back No Violations On the day of my inspection Mark Moreland, I witnessed Nicks Well plugging service has arrived on site and rigged up over top the well bore in preparation to plug the well. Specialized Safety Services has H2S monitoring equipment set up around the perimeter of the well. Before starting the service we attended a safety meeting exampling what the work conditions were and where to go in case of an emergency. We also went over the plugging operation and were the plugs will be set. After the meeting I spoke to the company man from Nicks Well Plugging Service, who informed me that he was going to attempt to set the bottom plug today. Later in the day the well conditions prevented Nicks from being able to set the bottom plug. I will be back on site tomorrow to witness the setting of the bottom plug.
0257295122 2016-06-02 Plug / Plug Back No Violations I am on site today accompanied by inspector Mark Moreland to witness the plugging of the well bore. On the day of my inspection, Appalachian Well Services was on site to set perforations inside the 4.5 inch diameter production casing. Appalachian set 10 shots at a depth of 4550 feet, Nicks Well Plugging Service then ran the 2.375 inch diameter tubing to where the perforations where located to set a 200 foot plug from 4550 to 4350 feet to cover up the H2S producing zone. After the plug was set Nicks pulled tubing up to a depth of 3885 and Appalachian shot 10 perforations at 3935. After the perforations, Nicks then ran the tubing back to 3935 and set a 200 foot plug from 3935 to 3735. After the plug was set Nicks pulled the tubing out and ripped the 4.5 inch diameter production casing at a depth of 1243 feet. Production casing was then pulled out of the hole and tubing was ran back to set the next 200 foot plug from 1195-995. After the plug was set tubing was then pulled to 200 feet and cement was then circulated to surface. During the duration of the Job Specialized Safety Services was monitoring the site for H2S and no signs or indications were discovered.
0416685445 2016-06-09 Plug / Plug Back No Violations On the day of my inspection accompanied my inspector Mark Moreland, I witnessed that the well site still needs to be graded.
0820446621 2016-05-31 Production Wells No Violations Atlas Noble is moving trucks in today to steam clean the production tanks and remove them in preparation of the plugging of this well. Nicks Well Plugging is moving trucks on site today and should be ready to plug Wednesday.
0935582158 2016-05-23 Production Wells No Violations Atlas has equipment on site today to steam clean the production tanks and remove them from the site.
1465558300 2016-06-01 Plug / Plug Back No Violations Continue plugging this morning with Nicks Well Plugging setting the bottom plug thru 1 1/2 inch diameter tubing. The plan for today is to set this bottom plug and pull out all of the 1 1/2 tubing to steam clean it so that Appalachian Well Service can drop out the bottom of it to shoot perf holes in the 4 1/2 inch casing. After the tubing has been steamed Nicks will run back in to 4500 ft. and wait until Thursday morning when the shooters are scheduled at 7:00 AM See plug report for more detail on depth of plugs - I returned later in the day and Nicks was waiting for the tubing to get done and then would run it in to 4500 ft.
1477492664 2016-06-01 Plug / Plug Back No Violations I am on site today accompanied by inspector Mark Moreland to witness plugging of the well bore. On the day of my inspection, Nicks Well Plugging Service set the bottom plug through the 2.375 inch diameter production tubing from a depth of 5400 feet to 5200 feet. After the plug was set Nicks then pulled out all the production out of the hole. After the production tubing was pulled, Sutton Pump and Supply then steam cleaned the tubing. The tubing was steamed cleaned to insure that the wireline service company could get the perforation gun down hole. After the tubing was steamed it was ran back to a depth of 4500 feet. The plug job will continue tomorrow, when Appalachian Well Services arrives on site to set perforations. During the duration of the Job Specialized Safety Services was monitoring the site for H2S and no signs or indications were discovered.
1593327318 2016-05-18 Production Wells No Violations I am on site today accompanied by inspector Mark Moreland, were I witnessed the well is utilizing a pump jack for means of production consisting of 8.625 inch diameter surface casing, 4.5 inch diameter production casing, and 2 3/8 inch diameter production tubing. The production tubing valve and production casing valves where in the closed position at the time on my inspection. Production equipment consisted of a 100 bbl. production tank, a 50 bbl. steel brine tank and a horizontal separator with a two inch diameter meter run. All production equipment was placed inside an earthen dike that measured approximately 30*40 feet at an average height of 3 foot. By the well head and the tank battery were wind socks and signs indicating warnings of poisonous gas, however I witnessed no signs of gases at the time of my inspection.
1788578804 2016-05-31 Plug / Plug Back No Violations Arrive on site today to set the bottom plug with Nicks Well Plugging. Nicks Well is pulling the rods and clearing the tubing so that the tubing can be used to set the bottom plug. Before the bottom plug could be set the well kicked off with a gas kick and plugging was cancelled today, until it could subside before placing the bottom plug.
1914921737 2016-07-08 Final Restoration No Violations This well has been plugged, the area graded and seeded with vegetation established. This site meets the requirements for the final restoration to be passed.
2083781482 2015-04-07 Production Wells No Violations On the date of inspection I found that production equipment includes a 100bbl tank and a 50bbl tank within an earthen dike. The well is equipped with a pumping unit, rods, 2.375 inch tubing, 4.5 inch casing, and 8.625 inch casing. Tubing and casing valves are in open position and production records are current through 2014. I did not detect H2S at the well.
257295122 2016-6-2 0:00:0 PB No Violations 12.00
416685445 2016-6-9 0:00:0 PB No Violations 1.00
8663027 2016-5-31 0:00: PB No Violations 5.00

For data sources see[9]

References