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34-059-24176

Well Details

Well ID: 34-059-24176
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Country: United States
State: Ohio
County: Guernsey
Municipality: Adams Township
Operator Name: ARTEX OIL COMPANY
Well Pad ID:
Farm/Lease Name: WELLS-CRUM UNIT
License Status: Producing
License Date: 2011-01-07
Spud Date: 2011-04-21
Spud Drilling Contractor: WARREN DRLG
Final Drill Date: 2011-05-15
Well Total Depth: 7350.00 ft
Configuration: Vertical
Latitude: 40.050000
Longitude: -81.670000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-01-07 Proposed Formations:OHIO SHALE THRU KNOX (MAY NOT PRODUCE CLINTON), Issued Date:1/7/2011, Expired Date:1/6/2013 12:00:00 PM, Drilling unit acres:77, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2011-05-15
Completion Report Received 2011-07-14
Construction Permit Expires 2013-01-06
Record Last Modified 2017-10-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2011-10-03 7225 7275 36
7225 7275 36
7225 7275 36

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2011-05-19 ACID 15 11800 Gal 0 Producers Service Corporation

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 ARTEX OIL COMPANY 11303.00 0.00 365
2012 ARTEX OIL COMPANY 18873.00 0.00 366
2013 ARTEX OIL COMPANY 11681.00 79.00 365
2014 ARTEX OIL COMPANY 10204.00 33.00 365
2015 ARTEX OIL COMPANY 8472.00 16.00 365
2016 ARTEX OIL COMPANY 7732.00 27.00 365
2017 ARTEX OIL COMPANY 7110.00 47.00 365
2018 ARTEX OIL COMPANY 6874.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 ARTEX OIL COMPANY Brine 2587 365
2012 ARTEX OIL COMPANY Brine 129 366
2013 ARTEX OIL COMPANY Brine 68 365
2014 ARTEX OIL COMPANY Brine 47 365
2015 ARTEX OIL COMPANY Brine 62 365
2016 ARTEX OIL COMPANY Brine 35 365
2017 ARTEX OIL COMPANY Brine 54 365
2018 ARTEX OIL COMPANY Brine 43 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1196040442 2011-4-7 0:00:0 DD No Violations
-1207253645 2011-4-22 0:00: DD No Violations
-1357178278 2011-5-18 0:00: DD No Violations 1.50
-1826599568 2011-5-6 0:00:0 DD No Violations
-329267992 2011-5-27 0:00: DD No Violations
-70471574 2011-5-10 0:00: DD No Violations
-866902323 2011-5-18 0:00: DD No Violations 1.00
0070471574 2011-05-10 Drill / Deepen / Reopen No Violations Inspection revealed that rig crew was tripping tools from well they twisted off@7230 and they got a hold of fish on first run and once removed from well they will replace broken drill pipe and then go back in well to drill to total depth.
0092460841 2016-09-08 Production Wells No Violations On the day of my inspection I witnessed the production equipment included 2-100 barrel tanks and a compressor unit within an earthen dike. Also present a horizontal separator, a motor valve, a 2 inch salesmeter with a 1 inch orifice and chart recorder. The well was equipped with 8.625 inch casing; 4.5 inch casing, 2.375 inch tubing and a plunger lift system with valves open on the tubing and closed on the casing. Identification was present and production records were current.
0329267992 2011-05-27 Drill / Deepen / Reopen No Violations Inspection revealed that well is equipped with 11 conductor pipe and 8.625 surface casing and 4.5 production casing and 2.375 tubing and 2-100 bbl tanks and separator within dike area.

Note: Horner Excavating was starting to reclaim site on the day of my inspection.

0344733097 2011-04-25 Drill / Deepen / Reopen No Violations Inspection revealed that rotary rig was drilling@3781 still dusting in lime TOL was noted@3496.
0363732111 2013-04-16 Production Wells No Violations On the day of my inspection Reviewed the Divisions production records and found them to be current, there is 8.625 casing with 4.5 production casing and 2 tubing standing from the ground, all the valves are open at the well, there are (3) one hundred barrel production tanks/ compressor setting inside a containment dike, the separator is setting inside a containment dike, the I.D. is posted on the tanks.
0491586832 2011-05-09 Drill / Deepen / Reopen No Violations Stopped by drill rig for update on upcoming casing job they were drilling at 7115 on 9#fluid and Trenton top was noted@6417 with small gas show in top of formation.
0514556378 2011-09-23 Preliminary Restoration No Violations Inspection revealed that drill site has been restored and vegetation has been established.

Note: Will check site in spring too see if any remedial work needs to be preformed.

0746135421 2011-05-11 Drill / Deepen / Reopen No Violations Inspection revealed that drilling rig was drilling@7295 and proposed total depth will be 7350 they should be ready to run production casing in the morning.
0866902323 2011-05-18 Drill / Deepen / Reopen No Violations Accompanied Dave Ball with Josh Garland on inspection. Tubing was being ran during visit.
1196040442 2011-04-07 Drill / Deepen / Reopen No Violations Warren Drilling moving in on site, stopped and checked site for pit construction compliance and received update on possible conductor cement job.
1207253645 2011-04-22 Drill / Deepen / Reopen No Violations Stopped by drill rig for update they were spotting fluid tanks shale shaker and mud pump in preparation for down hole drilling program.
1302559392 2011-04-11 Drill / Deepen / Reopen No Violations Well spudded drilling conductor hole on fluid they except to run 200 of 11.75 conductor pipe, there is a water well approximately 250 due west of drill site.
1302910996 2011-04-15 Drill / Deepen / Reopen No Violations On site to witness testing of BOP Assembly they tested blind ram@1000psi and we monitored pressure for 15 min with no decline then they attempted to test pipe rams and test failed they then proceeded to change out seal rings and retested and test failed again then decision was made to replace entire assembly will resume testing 4/18/11.

Note: Solidified mud pit and closed they are going to bring in steel tank to place cuttings in while drilling down hole.

1305244344 2011-05-12 Drill / Deepen / Reopen No Violations Stopped by drill rig for update they were picking drill string back up to go in hole to remove bridge from well,they tried to log well and tools sat down@4160 operator stated they possibly would be ready to cement casing by tomorrow if all goes well.
1305419616 2011-05-14 Drill / Deepen / Reopen No Violations Inspection revealed that rig crew ran 7340 of 4.5 casing in well and cemented it in place with 160 sacks 50/50 POZ and 150 sacks of Class A Rose Run blend cement plug down@7:50 a.m.
1305756840 2011-05-18 Completion Testing No Violations On site to witness bond log and perforating of casing top of cement@5700 and 36 shots @7225-7275 owner will acidize well tomorrow.
1305928361 2011-05-19 Completion Testing No Violations On site to witness acid job Producers Services pumped 9800 gal of 15%acid and 1000 gal of 28% into perfs and displaced with H2O into formation and let soak for predetermined time and they started to swab it back into 300 bbl tank.
1307232792 2011-06-03 Preliminary Restoration No Violations Restoration work continues at site.
1357178278 2011-05-18 Drill / Deepen / Reopen No Violations Accompanied D. Ball on inspection. Well had been perfed that morning and to be acidized the next day. TD 7350.
1826599568 2011-05-06 Drill / Deepen / Reopen No Violations Stopped by drill site for update they were drilling on 9# mud@6574 should be logging hole later this evening.
1994983109 2011-04-27 Drill / Deepen / Reopen No Violations Stopped by drill rig they were tripping bit@5172 should be back to drilling later today and they plan on coring Utica Shale section of well bore they have a 60 barrel on site and coring will be done on drilling fluid.
2031640025 2011-04-12 Drill / Deepen / Reopen No Violations Stopped by drill rig for update on upcoming conductor job they were drilling on fluid@145 should be running and cementing pipe by late evening.
344733097 2011-4-25 0:00: DD No Violations
363732111 2013-4-16 0:00: PW No Violations
491586832 2011-5-9 0:00:0 DD No Violations
514556378 2011-9-23 0:00: PL No Violations
746135421 2011-5-11 0:00: DD No Violations
92460841 2016-9-8 0:00:0 PW No Violations 0.50
925518250 2020-6-10 0:00: PW No Violations 1.00

For data sources see[9]

References