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| Well ID: 34-059-24049 | Loading map...
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| Country: United States | |
| State: Ohio | |
| County: Guernsey | |
| Municipality: Knox Township | |
| Operator Name: GENESIS RESOURCES LLC | |
| Well Pad ID: | |
| Farm/Lease Name: TRESL/BIRD UNIT | |
| License Status: Producing | |
| License Date: 2007-01-22 | |
| Spud Date: 2007-02-28 | |
| Spud Drilling Contractor: KILBARGER DRLG | |
| Final Drill Date: 2007-03-25 | |
| Well Total Depth: 5281.00 ft | |
| Configuration: Directional | |
| Latitude: 40.080000 | |
| Longitude: -81.690000 |
For data sources see[1]
| Well Status | Well Status Date | Comment |
|---|---|---|
| APP | 2007-01-22 | Proposed Formations:KNOX, Issued Date:1/22/2007, Expired Date:1/22/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL |
| Completed | 2007-03-25 | LOST 2 DOWNHOLE MOTORS IN HOLE ALONG WITH JARS. ATTEMPTED TO FISH, BUT COULD NOT GET ONTO ANY OF THESE ITEMS. PLUGGED BACK TO CLINTON. |
| Plugged Back | 2007-03-25 | LOST 2 DOWNHOLE MOTORS IN HOLE ALONG WITH JARS. ATTEMPTED TO FISH, BUT COULD NOT GET ONTO ANY OF THESE ITEMS. PLUGGED BACK TO CLINTON. |
| Reached Total Depth | 2007-03-25 | LOST 2 DOWNHOLE MOTORS IN HOLE ALONG WITH JARS. ATTEMPTED TO FISH, BUT COULD NOT GET ONTO ANY OF THESE ITEMS. PLUGGED BACK TO CLINTON. |
| Completion Report Received | 2007-11-05 | LOST 2 DOWNHOLE MOTORS IN HOLE ALONG WITH JARS. ATTEMPTED TO FISH, BUT COULD NOT GET ONTO ANY OF THESE ITEMS. PLUGGED BACK TO CLINTON. |
| Construction Permit Expires | 2008-01-22 | LOST 2 DOWNHOLE MOTORS IN HOLE ALONG WITH JARS. ATTEMPTED TO FISH, BUT COULD NOT GET ONTO ANY OF THESE ITEMS. PLUGGED BACK TO CLINTON. |
| Change of Owner | 2015-07-10 | Operator changed from 6288, ALLIANCE PETROLEUM CORPORATION to 9086, GENESIS RESOURCES LLC |
| Record Last Modified | 2017-02-15 | LOST 2 DOWNHOLE MOTORS IN HOLE ALONG WITH JARS. ATTEMPTED TO FISH, BUT COULD NOT GET ONTO ANY OF THESE ITEMS. PLUGGED BACK TO CLINTON. |
For data sources see[2]
| Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
|---|---|---|---|
| 2008-02-07 | 4674 | 4722 | 57 |
| 4674 | 4722 | 57 | |
| 4674 | 4722 | 57 |
For data sources see[3]
| Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
|---|---|---|---|---|---|---|
| H2O | 0 | 84000 Gal | 40000 |
For data sources see[4]
| Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2007 | ALLIANCE PETROLEUM CORPORATION | 3513.00 | 0.00 | 159 |
| 2008 | ALLIANCE PETROLEUM CORPORATION | 11681.00 | 0.00 | 365 |
| 2009 | ALLIANCE PETROLEUM CORPORATION | 5582.00 | 93.00 | 365 |
| 2010 | ALLIANCE PETROLEUM CORPORATION | 3061.00 | 85.00 | 365 |
| 2011 | ALLIANCE PETROLEUM CORPORATION | 2087.00 | 14.00 | 365 |
| 2012 | ALLIANCE PETROLEUM CORPORATION | 1726.00 | 18.00 | 366 |
| 2013 | ALLIANCE PETROLEUM CORPORATION | 1249.00 | 13.00 | 365 |
| 2014 | ALLIANCE PETROLEUM CORPORATION | 1268.00 | 0.00 | 365 |
| 2015 | GENESIS RESOURCES LLC | 291.00 | 0.00 | 184 |
| 2016 | GENESIS RESOURCES LLC | 883.00 | 0.00 | 320 |
| 2017 | GENESIS RESOURCES LLC | 781.00 | 0.00 | 365 |
| Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
|---|---|---|---|---|
| 2007 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 159 |
| 2008 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 365 |
| 2009 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 365 |
| 2010 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 365 |
| 2011 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 365 |
| 2012 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 366 |
| 2013 | ALLIANCE PETROLEUM CORPORATION | Brine | 80 | 365 |
| 2014 | ALLIANCE PETROLEUM CORPORATION | Brine | 0 | 365 |
| 2015 | GENESIS RESOURCES LLC | Brine | 0 | 184 |
| 2016 | GENESIS RESOURCES LLC | Brine | 126 | 320 |
| 2017 | GENESIS RESOURCES LLC | Brine | 0 | 365 |
| Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
|---|---|---|---|---|
| -1244908964 | 2007-3-1 0:00:0 | DD | No Violations | |
| -1468903446 | 2007-3-2 0:00:0 | DD | No Violations | |
| -1596336517 | 2007-10-4 0:00: | PL | No Violations | |
| -1863508095 | 2007-3-20 0:00: | DD | No Violations | |
| -1934288563 | 2007-3-5 0:00:0 | CT | No Violations | |
| -834157761 | 2017-6-20 0:00: | PW | No Violations | 0.50 |
| 0834157761 | 2017-06-20 | Production Wells | No Violations | On the day of my inspection I witnessed the production equipment included a 100 barrel tank, a 37 barrel polymer tank, a vertical separator, a drip, a 2 inch salesmeter with a .625 inch orifice and chart recorder. The well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 2.375 inch diameter tubing and a plunger lift system with valves open on the tubing and valves open on the casing supplying the motor valve. Well identification was present and production records were current through 2015. |
| 1173401529 | 2007-03-08 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING#1, AT 6019 READY TO KICK BIT. TRIP OUT FOR BIT AND CHECK DRILL PIPE .GO BACK IN AND TD HOLE. |
| 1174400419 | 2007-03-19 | Drill / Deepen / Reopen | No Violations | KILBARGER RIG#1. DOWNHOLE MOTOR HUNG IN HOLE AT 6216. BAKER TOOLS ON RIG TRYING TO JAR MOTOR LOOSE. PULLING 200,000#S. PIPE PARTED AT 5215. TO GO BACK IN HOLE WITH FISH TO GET COLLERS(4). TRY TO RETRIEVE MOTOR. |
| 1174996570 | 2007-03-26 | Production Wells | No Violations | KILBARGER DRILLING#1. RUNNING 4.5. CEMENT 4.5 |
| 1244908964 | 2007-03-01 | Drill / Deepen / Reopen | No Violations | KILBARGER DRILLING #1. DRILLING SURFACE SURFACE HOLE. AT 770. GOOD CIRCULATION. |
| 1468903446 | 2007-03-02 | Drill / Deepen / Reopen | No Violations | SET SURFACE CASING. KILBARGER#1. UNIVERSAL CEMENT. |
| 1596336517 | 2007-10-04 | Preliminary Restoration | No Violations | PRELIMINARY RESTORATION |
| 1816709556 | 2007-03-22 | Drill / Deepen / Reopen | No Violations | KILBARGER RIG#1. APPALACHIAN WELL SURVEYS, SHOOT PIPE OFF AT 6000 BELOW JARS, IF SUCCESSFUL, THEY WILL ATTEMPT TO WASHOVER PIPE AND GET BACK ON TO DOWN HOLE MOTOR AND TRY TO RETRIEVE MOTOR. |
| 1863508095 | 2007-03-20 | Drill / Deepen / Reopen | No Violations | KILBARGER RIG#8. LAYING DOWN DRILL PIPE. ONE ROW AND A HALF ON RACK. |
| 1934288563 | 2007-03-05 | Completion Testing | No Violations | KILBARGER#1. DRILLING AT 4446 |
| 342209044 | 2020-8-26 0:00: | PW | No Violations | 1.00 |
For data sources see[9]