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Well ID: 34-059-24038 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Adams Township | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: BARNES UNIT | |
License Status: Final Restoration | |
License Date: 2017-05-16 | |
Spud Date: 2006-10-26 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: 2006-11-09 | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.070000 | |
Longitude: -81.640000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2006-10-16 | Proposed Formations:ROSE RUN (MAY NOT PRODUCE CLINTON), Issued Date:10/16/2006, Expired Date:10/16/2007 6:00:00 AM, Drilling unit acres:105.16, Proposed Well Type:OG, Proposed Well Class:EDPW |
Correction to Well | 2006-10-27 | CORRECTION TO FOOTAGE, SHOULD BE "1130'NL & 345'EL OF SEC. 2". |
Completed | 2006-11-09 | UPDATED COORDINATES PER DOGRM SURVEYOR ALE 12/13/17. |
Reached Total Depth | 2006-11-09 | UPDATED COORDINATES PER DOGRM SURVEYOR ALE 12/13/17. |
Correction to Well | 2007-01-19 | CORRECTION TO FOOTAGE,SHOULD BE 1130'NL & 345'EL OF SEC. 2 |
Completion Report Received | 2007-04-02 | UPDATED COORDINATES PER DOGRM SURVEYOR ALE 12/13/17. |
APP | 2017-05-16 | Proposed Formations:BEEKMANTOWN, Issued Date:5/16/2017, Expired Date:5/16/2019 12:00:00 PM, Drilling unit acres:105.16, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2017-06-15 | UPDATED COORDINATES PER DOGRM SURVEYOR ALE 12/13/17. |
Record Last Modified | 2017-12-13 | UPDATED COORDINATES PER DOGRM SURVEYOR ALE 12/13/17. |
Construction Permit Expires | 2019-05-16 | UPDATED COORDINATES PER DOGRM SURVEYOR ALE 12/13/17. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2007-07-17 | 6883 | 7047 | 63 |
6883 | 7047 | 63 | |
6883 | 7047 | 63 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 8400 Gal | 0 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | ARTEX OIL COMPANY | 0.00 | 0.00 | 365 |
2007 | ARTEX OIL COMPANY | 7494.00 | 109.00 | 365 |
2008 | ARTEX OIL COMPANY | 1055.00 | 0.00 | 365 |
2009 | ARTEX OIL COMPANY | 505.00 | 0.00 | 365 |
2010 | ARTEX OIL COMPANY | 185.00 | 0.00 | 365 |
2011 | ARTEX OIL COMPANY | 162.00 | 0.00 | 365 |
2012 | ARTEX OIL COMPANY | 46.00 | 0.00 | 366 |
2013 | ARTEX OIL COMPANY | 0.00 | 0.00 | 365 |
2014 | ARTEX OIL COMPANY | 8.00 | 0.00 | 365 |
2015 | ARTEX OIL COMPANY | 54.00 | 0.00 | 365 |
2016 | ARTEX OIL COMPANY | 153.00 | 0.00 | 365 |
2017 | ARTEX OIL COMPANY | 63.00 | 52.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2006 | ARTEX OIL COMPANY | Brine | 900 | 365 |
2007 | ARTEX OIL COMPANY | Brine | 109 | 365 |
2008 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2009 | ARTEX OIL COMPANY | Brine | 76 | 365 |
2010 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2011 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2012 | ARTEX OIL COMPANY | Brine | 0 | 366 |
2013 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2014 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2015 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2016 | ARTEX OIL COMPANY | Brine | 0 | 365 |
2017 | ARTEX OIL COMPANY | Brine | 179 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-57124150 | 2007-7-5 0:00:0 | PL | No Violations | |
0057124150 | 2007-07-05 | Preliminary Restoration | No Violations | PRELIMENARY RESTORATION |
0272671731 | 2017-07-20 | Final Restoration | No Violations | On the day of my inspection I witnessed the access road was gated and locked. The site passed final restoration according to ORC 1509.072B. |
1052807964 | 2006-10-31 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING.WAIT ON BOP. HAD TO RE-BUILD BLADDER. |
1161955301 | 2006-10-26 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING. MOVING ON RIGGING UP. |
1162827948 | 2006-11-06 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING, WILL TD HOLE TODAY. GOOD FLARE IN BEEKMANTOWN. WILL RUN PRODUCTION STRING. |
1367263408 | 2017-06-12 | Production Wells | No Violations | |
1497438379 | 2017-06-14 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed the Bishop Well Service (BWS) had tripped 2.375 inch diameter tubing to the depth of 7019. Formation Cementing Inc. was onsite and gained circulation and pumped a 30 sack 400 foot Class A Beekmantown Dolomite plug from 7019 feet to 6619 feet. Cement was displaced with 25.6 barrels of brine water. BWS tripped 2.375 inch diameter tubing from the wellbore. BWS then tripped inside the 4.5 inch diameter casing, gained telegraph at 6090 feet and successfully ripped casing at 6050 feet. BWS worked pipe to ensure it was free and will pull 1 joint of casing tomorrow morning and complete plugging. |
1497527511 | 2017-06-15 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed the Bishop Well Service (BWS) had laid down 1 joint of 4.5 inch diameter casing. Casing was tallied leaving it set at 6008 feet. Formation Cementing Inc. was onsite and gained circulation and pumped a 50 sack 200 foot Class A Trenton Limestone isolation plug from 6008 feet to 5808 feet. Cement was displaced with 92.3 barrels of brine water. BWS tripped 29 joints of 4.5 inch diameter casing leaving it set at 4785 feet. Formation Cementing Inc. pumped a 60 sack 240 foot Class A Clinton plug from 4785 feet to 4545 feet. Cement was displaced with 72.2 barrels of brine water. BWS tripped 35 joints of 4.5 inch diameter casing leaving it set at 3308 feet. Formation Cementing Inc. pumped a 38 sack 150 foot Class A Big Lime plug from 3308 feet to 3158 feet. Cement was displaced with 50.2 barrels of brine water. BWS tripped 47 joints of 4.5 inch diameter casing leaving it set at 1325 feet. Formation Cementing Inc. gained circulation and pumped a 51 sack 200 foot Class A Bottom of the surface plug from 1325 feet to 1125 feet. Cement was displaced with 17.8 barrels of fresh water. BWS tripped 27 joints of 4.5 inch diameter casing and fluid level was at 150 feet. BWS tripped remaining casing from wellbore and Formation Cementing Inc. pumped a 47 sack 150 foot Class A Surface plug from 150 feet to surface circulating cement to surface. Instructed operator to cut casing off 30 inches below grade and install metal plate identifying well and reclaim according to ORC 1509.072B. |
1998775901 | 2006-10-27 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING. WILL SPUD TODAY.MOUSE HOLE AND CONDUCTOR WILL BE CUT ON FLUID. |
272671731 | 2017-7-20 0:00: | FR | No Violations | 1.00 |
For data sources see[9]