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Well ID: 34-059-22750 | Loading map...
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Country: United States | |
State: Ohio | |
County: Guernsey | |
Municipality: Adams Township | |
Operator Name: CONSOLIDATED RES OF AMER | |
Well Pad ID: | |
Farm/Lease Name: ACHAUER-LARRICK FARM | |
License Status: Producing | |
License Date: 1980-08-04 | |
Spud Date: 1980-09-16 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-09-20 | |
Well Total Depth: 5036.00 ft | |
Configuration: Vertical | |
Latitude: 40.070000 | |
Longitude: -81.630000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-08-04 | 264 CONSOLIDATED RES OF AMER GeoDate 8/4/80 |
Original Spud | 1980-09-16 | 69.5=ACRES I.P.- A.F. |
Completed | 1980-09-20 | 69.5=ACRES I.P.- A.F. |
Reached Total Depth | 1980-09-20 | 69.5=ACRES I.P.- A.F. |
Record Last Modified | 2019-04-03 | 69.5=ACRES I.P.- A.F. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4861 | 4889 | 6 |
4861 | 4889 | 6 | |
4861 | 4889 | 6 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 65000 Gal | 40000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CONSOLIDATED RES OF AMER | 6410.00 | 0.00 | 0 |
1985 | CONSOLIDATED RES OF AMER | 5412.00 | 0.00 | 365 |
1986 | CONSOLIDATED RES OF AMER | 2798.00 | 139.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CONSOLIDATED RES OF AMER | Brine | 0 | 0 |
1985 | CONSOLIDATED RES OF AMER | Brine | 50 | 365 |
1986 | CONSOLIDATED RES OF AMER | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1263785505 | 2013-12-4 0:00: | PW | No Violations | |
-1485251112 | 2015-2-9 0:00:0 | PW | No Violations | 2.00 |
-625689213 | 2020-6-2 0:00:0 | PW | No Violations | 1.00 |
0001766966 | 2017-01-31 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice - 1348844553, I witnessed that the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing and disconnected domestic gas service with all valves in the closed position. There was a small gas leak around the tubing packing. No production equipment was on site, no identification was present and no change in status since last inspection on 12/22/15. |
0244575935 | 2005-07-18 | Administrative Inspection | No Violations | FOR SHERRY YOUNG. WELL STIL EXISTS, ALL PRODUCING EQUIPMENT PULLED OFF WELL.CONVERSATION WITH LANDOWNERS,STATED WELL HAS BEEN IDLE SINCE 1990. |
0890626462 | 2015-12-22 | Orphan | No Violations | On the day of my inspection following up on NOV-1348844553, I witnessed that the well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing and domestic gas service with all valves in the closed position. There was a small gas leak around the tubing packing. No production equipment was on site, no identification was present and no change in status. |
1263785505 | 2013-12-04 | Production Wells | No Violations | No change in the status of the well prior to my last inspection done on 11/27/2012, I had a conversation with the landowner at that time, he stated to me he wanted to take ownership of the well. |
1277586294 | 2012-11-27 | Production Wells | No Violations | Pryor to the last inspection I received a call from Mr. Larrick informing me that he was going to take ownership of the well in order to get it plugged. |
1332478613 | 2008-02-07 | Production Wells | No Violations | IDLE BUT LANDOWNER WANTS TO TRY TO AQUIRE WELL. |
1348844553 | 2012-09-28 | Production Wells | Violations Noted | On the day of my inspection I found all the valves at the well in the closed position, the packing for the tubing is venting gas, there is no I.D. posted at the well site. |
1409785626 | 2020-4-3 0:00:0 | PW | No Violations | |
1485251112 | 2015-02-09 | Production Wells | No Violations | On the day of my inspection following up on NOV-1348844553, I witnessed that the well was equipped with 8.625 inch casing, 4.5 inch casing, 1.5 inch tubing and domestic gas hookup with valves in the closed position. No production equipment was on site and identification was not present. I met with land owner Mr. Larrick and he stated they now owned the well. I referred to RBMS which it still has Consolidated Resources as the current owner. I referred Mr. Larrick to Columbus to the Surety and Bonding Department for change of ownership. |
1553012365 | 2019-03-19 | Production Wells | No Violations | The purpose of my inspection was a follow up on compliance notice - 1348844553. During my inspection I spoke with the landowner Mrs. Larrick prior to entering the wellsite. Mrs. Larrick stated that she would like to see it plugged because she could smell the gas leaking from the well. The well was equipped with 8.625-inch diameter casing with a casing head, 4.5-inch diameter casing with a tubing head, and 1.5-inch diameter tubing. All valves were in the closed position. A small gas leak was coming from the tubing head packing. Consolidated Resources has not submitted reports of production since the year 1986. |
1766966 | 2017-1-31 0:00: | PW | No Violations | 1.00 |
2024298299 | 2018-02-12 | Production Wells | No Violations | On the day of my inspection following up on Compliance Notice - 1348844553, I witnessed that the well was equipped with 8.625 inch diameter casing, 4.5 inch diameter casing, 1.5 inch diameter tubing and disconnected domestic gas service with all valves in the closed position. There was a small gas leak around the tubing packing. No production equipment was on site, no identification was present and no change in status since last inspection on 1/31/17. |
244575935 | 2005-7-18 0:00: | AM | No Violations | |
890626462 | 2015-12-22 0:00 | OR | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1348844553 | US-OH-110105 | 2012-10-05 | Failure to legibly identify well | |
1348844553 | US-OH-110106 | 2012-10-05 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1348844553 | US-OH-110107 | 2012-10-05 | Defective casing, leaking well |
For data sources see[9]