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34-059-22200

Well Details

Well ID: 34-059-22200
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Country: United States
State: Ohio
County: Guernsey
Municipality: Madison Township
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name: WINTERSET
License Status: Final Restoration
License Date: 2015-05-29
Spud Date: 1977-10-12
Spud Drilling Contractor:
Final Drill Date: 1977-10-26
Well Total Depth: 5648.00 ft
Configuration: Vertical
Latitude: 40.070000
Longitude: -81.390000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1977-10-12
Completed 1977-10-25
Reached Total Depth 1977-10-26
CO 1982-02-01 1115 CAVENDISH PETRO OF OH INC GeoDate 2/1/82
CO 1996-05-01 3071 KINGSTON OIL CORP GeoDate 2/1/82
APP 2000-05-22 Proposed Formations:CLINTON, Issued Date:5/22/00, Expired Date:5/22/01 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2001-01-12 Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC
Change of Owner 2004-03-03 Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC
APP 2013-03-12 Proposed Formations:CLINTON, Issued Date:3/12/2013, Expired Date:3/12/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
APP 2015-05-29 Proposed Formations:CLINTON, Issued Date:5/29/2015, Expired Date:5/28/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-11-04
Record Last Modified 2016-06-17
Construction Permit Expires 2017-05-28

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5498 5572 23
5498 5572 23
5498 5572 23

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 84000 Gal 86000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 CAVENDISH PETRO OF OH INC 3278.00 0.00 0
1985 CAVENDISH PETRO OF OH INC 3265.00 0.00 365
1986 CAVENDISH PETRO OF OH INC 1353.00 0.00 0
1987 CAVENDISH PETRO OF OH INC 667.00 0.00 0
1988 CAVENDISH PETRO OF OH INC 717.00 0.00 365
1989 CAVENDISH PETRO OF OH INC 634.00 0.00 365
1993 KINGSTON OIL CORP 1024.00 0.00 116
1994 KINGSTON OIL CORP 438.00 0.00 261
1995 KINGSTON OIL CORP 0.00 0.00 350
1996 KINGSTON OIL CORP 1243.00 0.00 261
1997 KINGSTON OIL CORP 1084.00 0.00 350
1998 KINGSTON OIL CORP 871.00 0.00 290
1999 KINGSTON OIL CORP 379.00 0.00 0
2000 KINGSTON OIL CORP 884.00 0.00 0
2001 CHEVRON APPALACHIA LLC 442.00 0.00 365
2002 CHEVRON APPALACHIA LLC 617.00 0.00 365
2003 ATLAS NOBLE LLC 436.00 0.00 365
2004 ATLAS NOBLE LLC 128.00 0.00 365
2005 ATLAS NOBLE LLC 24.00 19.00 365
2006 ATLAS NOBLE LLC 0.00 0.00 365
2007 ATLAS NOBLE LLC 0.00 0.00 365
2008 ATLAS NOBLE LLC 0.00 0.00 366
2009 ATLAS NOBLE LLC 0.00 0.00 365
2010 ATLAS NOBLE LLC 0.00 0.00 365
2011 ATLAS NOBLE LLC 0.00 0.00 0
2012 ATLAS NOBLE LLC 0.00 0.00 0
2013 ATLAS NOBLE LLC 0.00 0.00 0
2014 ATLAS NOBLE LLC 0.00 0.00 0
2015 ATLAS NOBLE LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 CAVENDISH PETRO OF OH INC Brine 0 0
1985 CAVENDISH PETRO OF OH INC Brine 45 365
1986 CAVENDISH PETRO OF OH INC Brine 0 0
1987 CAVENDISH PETRO OF OH INC Brine 0 0
1988 CAVENDISH PETRO OF OH INC Brine 0 365
1989 CAVENDISH PETRO OF OH INC Brine 0 365
1993 KINGSTON OIL CORP Brine 15 116
1994 KINGSTON OIL CORP Brine 0 261
1995 KINGSTON OIL CORP Brine 0 350
1996 KINGSTON OIL CORP Brine 70 261
1997 KINGSTON OIL CORP Brine 0 350
1998 KINGSTON OIL CORP Brine 0 290
1999 KINGSTON OIL CORP Brine 144
2000 KINGSTON OIL CORP Brine 0
2001 CHEVRON APPALACHIA LLC Brine 0 365
2002 CHEVRON APPALACHIA LLC Brine 0 365
2003 ATLAS NOBLE LLC Brine 0 365
2004 ATLAS NOBLE LLC Brine 0 365
2005 ATLAS NOBLE LLC Brine 25 365
2006 ATLAS NOBLE LLC Brine 0 365
2007 ATLAS NOBLE LLC Brine 0 365
2008 ATLAS NOBLE LLC Brine 0 366
2009 ATLAS NOBLE LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 ATLAS NOBLE LLC Brine 0
2012 ATLAS NOBLE LLC Brine 0 0
2013 ATLAS NOBLE LLC Brine 0 0
2014 ATLAS NOBLE LLC Brine 0 0
2015 ATLAS NOBLE LLC Brine 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1082313110 2005-5-6 0:00:0 PW No Violations
-1135431680 2016-3-31 0:00: PB No Violations 1.00
-172585299 2015-11-4 0:00: PB No Violations 3.00
-1899401177 2015-11-3 0:00: PB No Violations 3.00
-59591240 2015-1-21 0:00: PW No Violations 2.00
0059591240 2015-01-21 Production Wells No Violations On the day of my inspection following up on NOV-1358208032, I witnessed that the well was equipped with 8.625 inch casing; 4.5 inch casing, 2.375 inch tubing and a plunger lift system with all valves in the closed position. Production equipment included a 210bbl tank and a horizontal separator within an earthen dike. Identification was present with production records not meeting the States minimum. I placed call to Atlas Noble Supervisor Pat Ervin and advised him that the current plug permit expires in March.
0106058344 2003-06-24 Production Wells No Violations STATUS CHECK
0167614005 2016-05-05 Plug / Plug Back No Violations On the day of my inspection I witnessed the grade has been restored since the last inspection. Location needs to be seeded and mulched for erosion control.
0172585299 2015-11-04 Plug / Plug Back No Violations On the day of my inspection I witnessed Nicks Well Plugging trip inside the 4.5 inch casing unable to get down to the Big Lime. NWP successfully got telegraph and ripped 4.5 inch casing at 3543 feet. NWP pulled 1 joint of casing and pumped a 75 sack 250 foot Class A isolation plug from 3501 feet to 3251 feet. Cement was displaced with 51.7bbls of water. NWP will trip up to the Berea and ODNR inspector Austin Gutridge will complete plugging.
0236969984 2005-10-06 Production Wells No Violations STATUS CHECK
0370674825 2007-09-05 Production Wells No Violations STATUS CHECK
0874892908 2015-12-17 Plug / Plug Back No Violations On the day of my inspection checking the status of reclamation, I witnessed the site has been roughed in and the pits closed with production equipment and debris still present. I placed call to Atlas and requested an update on when production equipment would be removed and the dike reclaimed.
106058344 2003-6-24 0:00: PW No Violations
1082313110 2005-05-06 Production Wells No Violations STATUS CHECK
1135431680 2016-03-31 Plug / Plug Back No Violations On the day of my inspection I witnessed final restoration was not completed with erosion developing on the access road, several low spots on the location with no erosion control present. Production equipment has been removed with the dike being restored. I contacted Atlas Noble and requested an update for completion of restoration as it is due on 5/4/16.
1358208032 2013-01-14 Production Wells Violations Noted Pryor to my inspection I received a complaint E-mail on an idle well in Madison twp, in Guernsey Co. On the day of my inspection I spoke with the land owner, he told me the well has not been in production for several years, I reviewed the divisions production records there has been no recorded production since the year of 2007. My inspection at the well site reveals there is four inch well casing with two inch tubing and a gate valve that is closed standing from the ground, there is also two inch production line leading from the well with a ball valve that is closed, there is no I.D. posted at the well site. The well is in violation of / 9-9-02 General safety/ 9-9-05(A) Failure to legibly identify well/ 1509.11 Statement of production, these are requirements to meet the divisions standards failure to comply will result in forfeiture of bond.
1382634499 2013-10-24 Production Wells No Violations On the day of my inspection, I found no change in the status of the well since my last inspection done on 01/14/2013, the permit to plug was issued on 03/12/2013 and expires on 03/12/2015.
1446664186 2015-11-04 Plug / Plug Back No Violations My inspection today was on cementing the Big lime, Berea, Bottom of Surface, and Surface plug. Nicks Well Plugging was on location with their water truck, cement truck, pump truck, and service rig. I witnessed NWP pull the 4.5 inch casing up to the Big Lime and cement from 3543 ft. to 3293 ft. Then they pulled up to 1288 ft. and set the Berea plug from 1288 ft. to 1088 ft. at the bottom of the 8.625 inch surface casing they set a cement plug from 590 ft. to 390 ft. NWP pulled up to 200 ft. and set a surface plug from 200 ft. to surface. Plugs were cemented through 4.5 inch casing with Class A cement.
1465907090 2016-06-14 Final Restoration No Violations On the day of my inspection I witnessed the erosion control is in place and the site meeting ORC 1509.072B.
167614005 2016-5-5 0:00:0 PB No Violations 1.00
1750701736 2015-11-05 Administrative Inspection No Violations NOV-1358208032 is resolved as well is now plugged.
1899401177 2015-11-03 Plug / Plug Back No Violations On the day of my inspection I witnessed Appalachian Well Survey tag bottom of tubing at 5475 feet and shoot the bottom of the tubing off at 5465 feet. Nicks Well Plugging was on site and pumped a 30 sack 200 foot class A bottom plug from 5465 feet to 5065 feet. Cement was displaced with 19.6bbls of water. NWP will trip tubing from well and rip 4.5 inch casing with completion of plugging tomorrow.
236969984 2005-10-6 0:00: PW No Violations
370674825 2007-9-5 0:00:0 PW No Violations
874892908 2015-12-17 0:00 PB No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1358208032 US-OH-110373 2013-02-27 General Safety
1358208032 US-OH-110374 2013-02-27 Failure to legibly identify well

For data sources see[9]

References