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34-055-22102

Well Details

Well ID: 34-055-22102
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Country: United States
State: Ohio
County: Geauga
Municipality: Parkman Township
Operator Name: DJR WELL SERVICES INC.
Well Pad ID:
Farm/Lease Name: BYLER UNIT
License Status: Producing
License Date: 2009-08-20
Spud Date: 2009-08-30
Spud Drilling Contractor: ADVENT DRLG
Final Drill Date: 2009-09-04
Well Total Depth: 4245.00 ft
Configuration: Vertical
Latitude: 41.410000
Longitude: -81.020000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2009-08-20 Proposed Formations:CLINTON, Issued Date:8/20/2009, Expired Date:8/20/2010 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2009-09-04
Completion Report Received 2010-03-01
Construction Permit Expires 2010-08-20
Record Last Modified 2017-10-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2010-05-17 3997 4059 33
3997 4059 33
3997 4059 33

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 60150 Gal 32000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 WILKES ENERGY INC 0.00 0.00 0
2010 WILKES ENERGY INC 5157.00 893.00 0
2011 WILKES ENERGY INC 7549.00 1040.00 365
2012 WILKES ENERGY INC 5649.00 655.00 366
2013 WILKES ENERGY INC 4171.00 499.00 365
2014 WILKES ENERGY INC 4097.00 351.00 365
2015 WILKES ENERGY INC 2963.00 481.00 365
2016 WILKES ENERGY INC 2988.00 336.00 365
2017 WILKES ENERGY INC 2167.00 323.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 WILKES ENERGY INC Brine 0 0
2010 WILKES ENERGY INC Brine 527 0
2011 WILKES ENERGY INC Brine 302 365
2012 WILKES ENERGY INC Brine 110 366
2013 WILKES ENERGY INC Brine 86 365
2014 WILKES ENERGY INC Brine 0 365
2015 WILKES ENERGY INC Brine 50 365
2016 WILKES ENERGY INC Brine 50 365
2017 WILKES ENERGY INC Brine 82 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-2076409884 2012-8-9 0:00:0 PW No Violations
-483840533 2009-10-22 0:00 PL No Violations
0483840533 2009-10-22 Preliminary Restoration No Violations Operator is actively reclaiming site. Drainage controls need repaired at the drainage ditch at the road. Called Randy from Wilkes Energy requested drainage controls be repaired.
0643345516 2009-08-31 Drill / Deepen / Reopen No Violations On location for CND job. Job went well 6 BBL return to surface of cement. Cement held at surface.
1254249463 2009-08-31 Drill / Deepen / Reopen No Violations Moving rig on to location. Digging pits, pits were clay. Drainage controls are in place. Pulled water sample from the Byler home, water well is within 100 feet of the well. Wilkes was unable to get a lab to the home before drilling started. Pulled water sample for landowner. Requested that Wilkes Energy improve drainage controls at the road ditch.
2076409884 2012-08-09 Production Wells No Violations My inspection today was due to a water well complaint filed by the Bylers. They are having odor issue with their water well and they can not drink the water. I reviewed the well construction records for the well. The casing and cementing program went as scheduled. Cementing of the casing went as planned. My inspection of the well today found a Plunger lift system well with and automatic shut off installed on it in good repair. The 8.625 casing annulus was open. The tank battery had two 140bbl production tanks and a mechincal separator in it. The tank battery dike was in good repair. Identification sign was posted on the tank battery. Load lines were locked.
643345516 2009-8-31 0:00: DD No Violations

For data sources see[9]

References