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34-055-21837

Well Details

Well ID: 34-055-21837
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Country: United States
State: Ohio
County: Geauga
Municipality: Newbury Township
Operator Name: ALLIANCE PETROLEUM CORPORATION
Well Pad ID:
Farm/Lease Name: SURCKLA P
License Status: Final Restoration
License Date: 2010-07-30
Spud Date: 2005-09-29
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2005-10-04
Well Total Depth: 4030.00 ft
Configuration: Vertical
Latitude: 41.480000
Longitude: -81.270000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2005-07-18 Proposed Formations:CLINTON, Issued Date:7/18/2005, Expired Date:7/18/2006 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 2005-09-29 RBDMS Rec
Completed 2005-10-04 RBDMS Rec
Reached Total Depth 2005-10-04 RBDMS Rec
Completion Report Received 2006-05-10 RBDMS Rec
APP 2010-07-30 Proposed Formations:CLINTON, Issued Date:7/30/2010, Expired Date:7/29/2012 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2012-06-15 RBDMS Rec
Construction Permit Expires 2012-07-29 RBDMS Rec
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-07-28 3834 3916 80
3834 3916 80
3834 3916 80

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 80000 Gal 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1197273229 2005-10-1 0:00: DD No Violations
-1717459095 2007-1-2 0:00:0 PL No Violations
-2126319946 2007-6-7 0:00:0 PW No Violations
-400059374 2013-7-16 0:00: FR No Violations
-827435874 2006-1-4 0:00:0 DD No Violations
-931054791 2007-6-13 0:00: PL No Violations
0385410254 2013-10-08 Final Restoration No Violations My inspection today found no changes since my last inspection.
0400059374 2013-07-16 Final Restoration No Violations Final Restoration not passed. Well site has large patches of dry-hard soil with no vegetation growing. Tank battery site is still present. Tank batterys dike is still largely intact with the gravel bottom still present. The piping is still present at Tank battery site, with some staining of the gravel. Access road is covered with native vegetation.
0437848965 2015-10-13 Final Restoration No Violations My inspection found the flow line and the tank battery has been removed. The location has been graded, seeded, and strawed. The company still has a sales line riser inside where the tank battery was previously, due to a pipeline right of way on the property. The meter for the pipeline is at the entrance to the location on Pekin Rd. Once vegetation is established on the location, final restoration can be passed.
0820922727 2016-05-31 Final Restoration No Violations My inspection found the flow line and the tank battery has been removed. The location has been graded, seeded, and strawed. The company still has a sales line riser inside where the tank battery was previously, due to a pipeline right of way on the property. The meter for the pipeline is at the entrance to the location on Pekin Rd. Vegetation has been established on the location. Final restoration can be passed.
0827435874 2006-01-04 Drill / Deepen / Reopen No Violations
0902216777 2006-08-24 Drill / Deepen / Reopen No Violations status check
0924008186 2012-06-14 Plug / Plug Back No Violations I was on site today to witness plugging operations. Well had 400 pounds per square inch (psi) pressure on it. Nicks Plugging blew down the well. The well blew down within 5 minutes. During fracturing, this well broke down at 3,800psi and the operator was unable to run sand during the frac job. The operator was going to trip tubing in and spot bottom plug but decided to attempt bull heading bottom plug in. Operator mixed cement and attempted to displace but 20 barrels into the 57.78 barrels of displacement the well locked up. Operator pressured up to 2700psi, and shut down. At 2:18 pm this day, the operator is tripping tubing into the hole to flush cement plug out and spot bottom plug. Operator tripped tubing below the cement and flushed the cement out. Operator will complete tripping tubing into the hole, pack off the well and complete plugging on 06/15/2012.
0931054791 2007-06-13 Preliminary Restoration No Violations On site at the request of the operator. Lease road has been restored and topped with 57s. Drainage has been installed on the east and west side of the lease road. Affected area has been graded, seeded and mulched. Restoration will be passed once vegetation is established.
1144167252 2006-01-13 Drill / Deepen / Reopen No Violations drilling checking for mud on road none found.
1167422728 2006-12-29 Production Wells No Violations On site to check the status of reclamation work. No new work has been completed. Drainage is blocked along the lease road. Lease road is soft and in poor condition. Per operator reclamation will start 01/02/2007. NOV will be issued that day if work is not started.
1179850797 2007-05-22 Preliminary Restoration Violations Noted Lease road has not been restored. Lease road is still bare earth. Lease road is blocking drainage and causing water to accumulate on the adjacent landowners property. Tank battery is not completed. Sink hole to the south of the well head. Tracks from and excavator have not been graded out and area seeded. Edges of affected area have not been blended in. Culvert 100 east of the well head is blocked., larger culvert needs to be installed. Final grading needs completed. Culverts installed and sufficient drainage established. Area seeded. Any debris removed,
1180115674 2007-05-24 Preliminary Restoration No Violations On site with adjacent landowner, Ted and Bruce Close from Alliance Petroleum Corp. Lease road has not been restored. Lease road is blocking drainage and allowing drainage to accumulate on the landowner to the east. Tank battery is not complete, fencing is not up. Sink hole 8X10 south east of the well head is present. Culvert between the well head and tank battery is blocked and not of sufficient size to handle drainage for the area. A pipe line was installed from well #1842 to #1837, affected area from the installation of the pipe line has not been graded and seeded.
1197273229 2005-10-01 Drill / Deepen / Reopen No Violations Company had trouble running 85/8
1444761620 2015-10-09 Final Restoration No Violations I was on location with Bruce Close a supervisor with Alliance Petroleum. The company has hired CES to remove the flow line and the tank battery. The flow line has been removed and the company is in the process off cutting it into sections for removal. I will return on 10/13/2015 to check the status of the work being performed.
1717459095 2007-01-02 Preliminary Restoration No Violations Operator on site installing culvert at the entrance of the road. Operator is continuing to work on reclamation of the site.
1797174307 2013-09-03 Final Restoration No Violations My inspection today found the well to be plugged. The area around the well has spots where vegetation has not been established. There is pieces of pit liner showing up through the soil. The tank battery has had the equipment removed from the location. The stone is still present in the tank battery as well as the flow line and the sales line portions are above ground. I will need a line waiver and lease road waiver before I can pass the final restoration. I spoke with Bruce Close a supervisor with Alliance about the issues. He stated he will have it taken care of this month.
2100370253 2006-01-13 Drill / Deepen / Reopen No Violations checking road for mud NO MUD no violation
2126319946 2007-06-07 Production Wells No Violations Operator is in the process of restoring the lease road. Operator has installed drainage along the east and west side of the lease road. Ruff grading has been completed south end of the lease road. Site still needs to be seeded and graded.
385410254 2013-10-8 0:00: FR No Violations
437848965 2015-10-13 0:00 FR No Violations
820922727 2016-5-31 0:00: FR No Violations
902216777 2006-8-24 0:00: DD No Violations
924008186 2012-6-14 0:00: PB No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1179850797 US-OH-104791 2007-05-22 Failure to restore land surface within 9 mos. (CHANGE) (REPLACE)

For data sources see[5]

References