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34-055-20568

Well Details

Well ID: 34-055-20568
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Country: United States
State: Ohio
County: Geauga
Municipality: Huntsburg Township
Operator Name: PETROX, INC
Well Pad ID:
Farm/Lease Name: RAY T UNIT
License Status: Producing
License Date: 1983-09-02
Spud Date: 1983-10-23
Spud Drilling Contractor: SHERMAN DRLG
Final Drill Date: 1983-10-27
Well Total Depth: 3980.00 ft
Configuration: Vertical
Latitude: 41.570000
Longitude: -81.040000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1983-09-02 213 LOMAK OPERATING CO GeoDate 9/2/83
Oil and Gas 1983-09-02 Issued Date 9/2/83 Expired Date Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth Proposed Drill Depth
Original Spud 1983-10-23 IP. OIL = 1/2 BBL.
Completed 1983-10-27 IP. OIL = 1/2 BBL.
Reached Total Depth 1983-10-27 IP. OIL = 1/2 BBL.
Completion Report Received 1983-12-06 IP. OIL = 1/2 BBL.
Construction Permit Expires 1984-02-29 IP. OIL = 1/2 BBL.
Change of Owner 2000-06-27 Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC
Change of Owner 2005-01-21 Operator changed from 2026, SUMMIT PETROLEUM INC to 1966, PETROX, INC
Change of Owner 2005-01-21 Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 2026, SUMMIT PETROLEUM INC
Record Last Modified 2017-02-15 IP. OIL = 1/2 BBL.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3748 3842 0
3748 3842 0
2006-09-11 3749 3794 49
3749 3794 49
3748 3842 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 60000 Gal 50000 FRAC: WATER, SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 RANGE OPERATING COMPANY 25975.00 91.00 0
1985 RANGE OPERATING COMPANY 20239.00 126.00 365
1986 RANGE OPERATING COMPANY 10049.00 0.00 365
1987 RANGE OPERATING COMPANY 12041.00 110.00 365
1988 RANGE OPERATING COMPANY 8108.00 0.00 366
1989 RANGE OPERATING COMPANY 6139.00 88.00 365
1990 RANGE OPERATING COMPANY 4614.00 0.00 365
1991 RANGE OPERATING COMPANY 3502.00 0.00 365
1992 RANGE OPERATING COMPANY 2362.00 75.00 366
1993 RANGE OPERATING COMPANY 2398.00 0.00 365
1994 RANGE OPERATING COMPANY 2522.00 0.00 365
1995 RANGE OPERATING COMPANY 2182.00 99.00 365
1996 RANGE OPERATING COMPANY 1656.00 0.00 365
1997 RANGE OPERATING COMPANY 1354.00 0.00 365
1998 RANGE OPERATING COMPANY 1743.00 37.00 274
1999 RANGE RESOURCES-APPALACHIA LLC 522.00 0.00 92
2000 RANGE RESOURCES-APPALACHIA LLC 1331.00 0.00 365
2001 RANGE RESOURCES-APPALACHIA LLC 1444.00 0.00 335
2002 RANGE RESOURCES-APPALACHIA LLC 1588.00 0.00 334
2003 RANGE RESOURCES-APPALACHIA LLC 1254.00 0.00 303
2005 PETROX, INC 943.00 0.00 365
2006 PETROX, INC 1715.00 0.00 365
2007 PETROX, INC 1037.00 0.00 365
2008 PETROX, INC 844.00 64.00 308
2009 PETROX, INC 578.00 0.00 365
2010 PETROX, INC 924.00 0.00 365
2011 PETROX, INC 1092.00 0.00 365
2012 PETROX, INC 1241.00 56.00 366
2013 PETROX, INC 1160.00 0.00 365
2014 PETROX, INC 617.00 49.00 365
2015 PETROX, INC 0.00 0.00 0
2016 PETROX, INC 0.00 0.00 0
2017 PETROX, INC 0.00 0.00 0
2018 PETROX, INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 RANGE OPERATING COMPANY Brine 0 0
1985 RANGE OPERATING COMPANY Brine 365 365
1986 RANGE OPERATING COMPANY Brine 365 365
1987 RANGE OPERATING COMPANY Brine 240 365
1988 RANGE OPERATING COMPANY Brine 280 366
1989 RANGE OPERATING COMPANY Brine 140 365
1990 RANGE OPERATING COMPANY Brine 210 365
1991 RANGE OPERATING COMPANY Brine 68 365
1992 RANGE OPERATING COMPANY Brine 70 366
1993 RANGE OPERATING COMPANY Brine 246 365
1994 RANGE OPERATING COMPANY Brine 145 365
1995 RANGE OPERATING COMPANY Brine 75 365
1996 RANGE OPERATING COMPANY Brine 145 365
1997 RANGE OPERATING COMPANY Brine 0 365
1998 RANGE OPERATING COMPANY Brine 274
1999 RANGE OPERATING COMPANY Brine 59 273
2000 RANGE RESOURCES-APPALACHIA LLC Brine 0 365
2001 RANGE RESOURCES-APPALACHIA LLC Brine 25 335
2002 RANGE RESOURCES-APPALACHIA LLC Brine 25 334
2003 RANGE RESOURCES-APPALACHIA LLC Brine 0 303
2005 PETROX, INC Brine 0 365
2006 PETROX, INC Brine 53 365
2007 PETROX, INC Brine 365
2008 PETROX, INC Brine 22 308
2009 PETROX, INC Brine 68 365
2010 PETROX, INC Brine 51 365
2011 PETROX, INC Brine 30 365
2012 PETROX, INC Brine 21 366
2013 PETROX, INC Brine 102 365
2014 PETROX, INC Brine 29 365
2015 PETROX, INC Brine 0 0
2016 PETROX, INC Brine 0 0
2017 PETROX, INC Brine 0 0
2018 PETROX, INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-191961880 2015-2-3 0:00:0 PW No Violations
-2032001087 2014-6-9 0:00:0 PW No Violations
0191961880 2015-02-03 Production Wells No Violations My inspection found the well to be equipped with a plunger lift unit. The well and tank battery are in good repair and are surrounded by a chain link fence. The tank battery consists of a 100 BBL production tank and a mechanical separator. The proper identification is on the tank battery. The lease road is in stable condition.
1402318875 2014-06-06 Production Wells No Violations I was called to the location by Geauga Emergency Services Ken Folsom for a flow line leak and about 20 gallons of oil on the ground. My inspection found the flow line had two holes in it. One in the tank battery where the flow line riser comes out of the ground and the other in a dried up creek bed where the flow line was run above ground. The landowner had previously lined the creek bed by his road culverts with cement to prevent erosion. The oil was laying on top of the cement. The company had absorbed the majority of the oil with absorbent mats and peat-sorb. The company was to return in the morning to clean up the rest of the contaminated areas. The lines are scheduled to be repaired on Monday the 9th of June.
1716335626 2013-03-01 Production Wells No Violations My inspection found the well to be equipped with a plunger lift unit. The wellhead was surrounded by a chain link fence. The tank battery is surrounded by a chain link fence and a sufficient dike. The tank battery consists of a 100 bbl production tank and a mechanical separator. The identification is on the tank battery. The lease road is in stable condition.
2032001087 2014-06-09 Production Wells No Violations My inspection today found the area contaminated by oil in the creek bed had been cleaned up. The hole in the flow line was temporarily repaired by a pipe clamp. The flow line riser in the tank battery was not repaired and there was still peat-sorb spread around the area. Petrox has Scott Miller Construction scheduled to make the repairs and clean up the rest of the tank battery.

For data sources see[9]

References