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34-041-20334

Well Details

Well ID: 34-041-20334
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Country: United States
State: Ohio
County: Delaware
Municipality: Porter Township
Operator Name: R C POLING CO INC
Well Pad ID:
Farm/Lease Name: LODGE HEIRS # 1
License Status: Producing
License Date: 1985-11-26
Spud Date: 1985-12-20
Spud Drilling Contractor:
Final Drill Date: 1985-12-30
Well Total Depth: 3675.00 ft
Configuration: Vertical
Latitude: 40.340000
Longitude: -82.780000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1985-11-26 Issued Date 11/26/85 Expired Date 11/26/86 Acres 0020000 Tool Type RTF Proposed Formation TREMPEALEAU Proposed Depth 03675 Proposed Drill Depth 03675
Original Spud 1985-12-20 RBDMS Rec
Completed 1985-12-30 RBDMS Rec
Reached Total Depth 1985-12-30 RBDMS Rec
CO 1986-02-03 1381 FISHBURN SERVICES INC GeoDate 11/26/85
Completion Report Received 1986-04-29 RBDMS Rec
Construction Permit Expires 1986-11-26 RBDMS Rec
CO 1994-04-25 236 POLING R C CO INC GeoDate 11/26/85
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2012-01-18 3484 3510 21
3484 3510 21
3484 3510 21

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 1500 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1994 R C POLING CO INC 26002.00 998.00 365
1995 R C POLING CO INC 5378.00 1339.00 365
1996 R C POLING CO INC 779.00 2025.00 365
1997 R C POLING CO INC 40.00 2000.00 365
1998 R C POLING CO INC 116.00 2609.00 365
2001 R C POLING CO INC 0.00 2074.00 365
2002 R C POLING CO INC 0.00 1875.00 365
2003 R C POLING CO INC 0.00 1675.00 365
2004 R C POLING CO INC 0.00 1921.00 365
2005 R C POLING CO INC 0.00 1401.00 365
2006 R C POLING CO INC 0.00 1437.00 365
2007 R C POLING CO INC 0.00 1379.00 365
2008 R C POLING CO INC 0.00 1226.00 365
2009 R C POLING CO INC 0.00 1199.00 365
2010 R C POLING CO INC 0.00 853.00 365
2011 R C POLING CO INC 0.00 866.00 365
2012 R C POLING CO INC 0.00 1209.00 366
2013 R C POLING CO INC 0.00 1020.00 365
2014 R C POLING CO INC 0.00 1032.00 365
2015 R C POLING CO INC 0.00 1052.00 365
2016 R C POLING CO INC 0.00 854.00 365
2017 R C POLING CO INC 0.00 341.00 365
2018 R C POLING CO INC 0.00 1195.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1994 R C POLING CO INC Brine 0 365
1995 R C POLING CO INC Brine 125 365
1996 R C POLING CO INC Brine 111 365
1997 R C POLING CO INC Brine 30 365
1998 R C POLING CO INC Brine 163 365
2001 R C POLING CO INC Brine 30 365
2002 R C POLING CO INC Brine 0 365
2003 R C POLING CO INC Brine 0 365
2004 R C POLING CO INC Brine 0 365
2005 R C POLING CO INC Brine 0 365
2006 R C POLING CO INC Brine 65 365
2007 R C POLING CO INC Brine 80 365
2008 R C POLING CO INC Brine 20 365
2009 R C POLING CO INC Brine 30 365
2010 R C POLING CO INC Brine 30 365
2011 R C POLING CO INC Brine 15 365
2012 R C POLING CO INC Brine 40 366
2013 R C POLING CO INC Brine 15 365
2014 R C POLING CO INC Brine 35 365
2015 R C POLING CO INC Brine 15 365
2016 R C POLING CO INC Brine 91 365
2017 R C POLING CO INC Brine 15 365
2018 R C POLING CO INC Brine 45 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1130705092 2014-1-28 0:00: PW No Violations
-1281142997 2017-8-9 0:00:0 PW No Violations
-1389517115 2017-8-15 0:00: PW No Violations
-1737616781 2017-7-25 0:00: PW No Violations
-1761875482 2020-6-26 0:00: PW No Violations
-2024340057 2017-9-20 0:00: PW No Violations
-263095237 2017-7-28 0:00: PW No Violations
-530164339 2014-1-28 0:00: PW No Violations
-670737353 2017-7-17 0:00: PW No Violations
-901711476 2017-12-19 0:00 PW No Violations
0214345543 2015-07-17 Production Wells Violations Noted Inspected the Lodge Heirs #1 (#334) as part of a standard production well status check. Inspect well, storage and identification. Status: residual oil on the ground around the well head is excessive. Contacted operator for clean up.
0263095237 2017-07-28 Production Wells No Violations Check location for remediation status. No activity.
0530164339 2014-01-28 Production Wells No Violations Location Information. ENTRANCE: Lat. 40.34616 Long. -82.78344 / WELL HEAD: Lat. 40.34570 Long. -82.78374 / CENTER-OF-STORAGE: Lat. 40.34600 Long. -82.78323.
0590443131 2004-12-08 Production Wells Violations Noted
0670737353 2017-07-17 Production Wells Violations Noted Inspected the Lodge Heirs #1 (#334) as part of a standard production well status check. Inspect well, storage and identification. Status: violation (1501:9-1-07), crude oil released from stuffing box leak has saturated the gravel at the wellhead, approximate affected area (19L x 3W) perpendicular to the pump jack. Contacted the operator by phone to remove and replace gravel.
0901711476 2017-12-19 Production Wells No Violations The operator has placed the well back into production. Status: ok. The well was pumping at the time of inspection.
0902051078 2013-04-18 Production Wells No Violations Inspect pump jack, well, storage and identification. Status: ok.
0924473577 2018-11-19 Production Wells No Violations Inspected the Lodge Heirs #1 (#334) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection.
1130705092 2014-01-28 Production Wells No Violations Inspected the Lodge Heirs #1 (#334) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1165241324 2006-12-04 Production Wells Violations Noted Well has pump jack and is capable. Single 210 Bbl. Storage. Has Fishburn ID. Called Dick Poling at 740/743-2531 9:05am. Request his ID be put up and call me when completed.
1166040762 2006-12-12 Production Wells No Violations Dick Poling called 12-08-06_ID posted as requested. NOV resolved.
1252622409 2017-11-20 Production Wells No Violations The well is currently out-of-service as the rods and tubing are pulled and stacked next to the well. No service rig on the well.
1281142997 2017-08-09 Production Wells No Violations Check well for remediation, none started. Contacted operator for reminder.
1347306252 2012-09-10 Production Wells No Violations Inspected the Lodge Heirs #1 (#334) as a standard productive well status check. The well is pumping by a black Churchill electric powered pump jack. A fresh layer of gravel has been spread over the well pad. The storage consists of one brown tank (#37298) set in a recessed stone lined dike. The well identification is clearly marked at the storage. There is some confusion on the ownership of the well as either Fishburn Producing or R.C. Poling. Status OK.
1389517115 2017-08-15 Production Wells No Violations Compliance notice follow-up. No work completed: contacted operator.
1440425396 2015-08-20 Production Wells No Violations The operator has not remediated the oil around the well pad. Status: contacted the operator.
1440591392 2015-08-25 Production Wells No Violations The operator has spread saw dust around the well pad and shut the well in for repairs (stuffing box rubbers) as part of the initial remediation. The operator plans to remove the stained gravel and soil and reset the pumping unit. Status: will continue to monitor the remediation and repair.
1627403537 2012-12-06 Production Wells No Violations Check well and storage. Site is in production, clean, and identified.
1737616781 2017-07-25 Production Wells No Violations The operator has not begun clean-up work.
1991412460 2015-09-21 Production Wells No Violations The residual oil on around the well pad has been remediated and the well has been placed back into production. This clears the previous compliance notice. Status: ok.
2024340057 2017-09-20 Production Wells No Violations The operator is on the well for workover (rods and tubing pulled). The contamination around the wellhead has been removed and replaced with fresh gravel. This clears the previous violation #670737353.
214345543 2015-7-17 0:00: PW No Violations
590443131 2004-12-8 0:00: PW No Violations
902051078 2013-4-18 0:00: PW No Violations
924473577 2018-11-19 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0214345543 US-OH-122016 2015-10-02 Well operation causing pollution and contamination
0590443131 US-OH-126640 2004-12-08 Failure to legibly identify well
0670737353 US-OH-127589 2017-08-30 9-1-07 Well operation causing pollution and contamination
1165241324 US-OH-104386 2006-12-04 Failure to legibly identify well

For data sources see[9]

References