If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-035-61237 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":41.49,"lon":-81.77,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: HISTORIC OWNER | |
Well Pad ID: | |
Farm/Lease Name: MICHAEL & MILLIE KRESEVICH | |
License Status: Final Restoration | |
License Date: | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 41.490000 | |
Longitude: -81.770000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Changed to Orphan Well Ready | 2008-01-01 | Changed Well To Orphan Ready |
Oil and Gas | 2008-01-31 | IDLE ORPHAN WELL. WELL INSPECTED BY NORBURT LOWDER ON 5/10/2000. WELL FOUND IN BACKYARD WITH CONCRETE PLUG 12 INCH DIAMETER WITH 3 INCH PIPE COMING OUT. WELL WAS GASSING. WELL INSPECTED AGAIN IN 2002. NO CHANGE. |
Plugged/Abandoned | 2018-06-07 | IDLE ORPHAN WELL. WELL INSPECTED BY NORBURT LOWDER ON 5/10/2000. WELL FOUND IN BACKYARD WITH CONCRETE PLUG 12 INCH DIAMETER WITH 3 INCH PIPE COMING OUT. WELL WAS GASSING. WELL INSPECTED AGAIN IN 2002. NO CHANGE. I/O Case No. 2008 01 003. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
Record Last Modified | 2019-06-05 | IDLE ORPHAN WELL. WELL INSPECTED BY NORBURT LOWDER ON 5/10/2000. WELL FOUND IN BACKYARD WITH CONCRETE PLUG 12 INCH DIAMETER WITH 3 INCH PIPE COMING OUT. WELL WAS GASSING. WELL INSPECTED AGAIN IN 2002. NO CHANGE. I/O Case No. 2008 01 003. UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 06/20/17 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-103267024 | 2018-5-24 0:00: | PB | No Violations | |
-1415819342 | 2018-5-22 0:00: | PB | No Violations | |
-1502946678 | 2018-6-7 0:00:0 | PB | No Violations | |
-156048388 | 2018-6-5 0:00:0 | PB | No Violations | |
-1792194191 | 2018-5-29 0:00: | PB | No Violations | |
-1793051379 | 2016-11-3 0:00: | OR | No Violations | |
-1936462261 | 2018-5-23 0:00: | PB | No Violations | |
-2116141340 | 2018-5-18 0:00: | PB | No Violations | |
-413036508 | 2017-6-1 0:00:0 | OR | No Violations | |
-980294123 | 2018-5-21 0:00: | PB | No Violations | |
0103267024 | 2018-05-24 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew has tripped in one collar, bit sub and a 7 7/8 inch bit into the wellbore before tagging an obstruction at 37 feet. Gel has been mixed up for the drill out. The location was secured for the holiday weekend and drill out will commence on the 29th. |
0114651983 | 2018-05-17 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew is currently moving two steel tanks, a pump, and the service rig onto the location in preparation to plug the well. |
0156048388 | 2018-06-05 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The drill string was hung in the wellbore when the crew tried to remove the drill string. After multiple attempts the rig operator was able to free the drill string and remove it from the well. Engineers Kris Roser and Jason Jones stopped out for a site visit. After discussion with the Engineer, Doug Gonzalez, and Orphan Well Manager Gene Chini it was determined that due the well conditions we will plug it at the 1205 ft point. |
0413036508 | 2017-06-01 | Orphan | No Violations | On location to meet with landowner and ascertain their desire as to location of vent line after well is plugged. Determination has been made and information relayed to engineer. |
0620100490 | 2015-07-22 | Orphan | No Violations | I inspected this reported well location as an Orphan Well Program status check. The residents were not home at the time of my inspection. During my site reconnaissance I observed a vent stack comprised of an 8-inch diameter PVC riser located in the back yard, within the footprint of a childrens play area. The riser terminates 15 feet from grade. The well is inferred to be located coincident with the riser. No gas odors or meter readings were observed at the time of my inspection. Subsequent discussions with the landwoners indicate they have observed increased amount of gas odors over the last couple of years. |
0692484941 | 2018-06-06 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew was able to run the 2 3/8 inch tubing into the well to 1205 ft. Petroset is on location to set the first 500 ft cement plug. Petroset rigged up and broke circulation and pumped 130 sacks of Class A Cement that mudscaled at 15.6 ppg. The well was static during plugging operations. |
0980294123 | 2018-05-21 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew is rigged up and ready to commence the drill out of the well. The crew pulled the existing 3 inch diameter casing. They have began to run 10 imch diameter casing into the open wellbore. Crew left location to pick up more 10 inch casing. |
114651983 | 2018-5-17 0:00: | PB | No Violations | |
1415819342 | 2018-05-22 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew has drove 52 feet of 10 inch diameter casing into the open wellbore and grouted the back side of the 10 inch with 42, 80 lbs sacks of type s mortar. The natural gas escaping from the well bore has been sealed off on the backside of the 10 inch casing. |
1496846735 | 2017-06-07 | Orphan | No Violations | Ron Gibson, of Ron Gibson & Associates, on site to give estimate to expose well casing, determine depth of 3 diameter tubing and re-configure existing vault & vent system. |
1502946678 | 2018-06-07 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The rig crew ran the 2 3/8 inch tubing into the well and tagged the plug at 970 ft. Petroset is on location to set the remainder of the cement plugs in the well. Petroset rigged up, broke circulation and set a 160 sacks of Class A Cement that mudscaled at 15.6 ppg from 900 ft to 400 ft. The crew pulled the tubing up to 400 ft in preparation for the final plug. After waiting two hours, Petroset rigged up, broke circulation and pumped 60 sacks of Class A Cement that mudscaled at 15.6 ppg from 400 ft to surface. The tubing was removed from the well and the hole was topped off with cement. |
1509462756 | 2017-10-31 | Orphan | No Violations | On location this date to obtain gas readings. Utilizing Sperian meter as well as Tango meter, no readings were noted in the area surrounding the well and vent line. |
1527607110 | 2018-05-15 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. Currently installing mating and excavating around the well in prepartion for the drill out and plug job. |
1527699791 | 2018-05-30 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew has cleaned out the well to 1148 feet and has hit a reduction in the wellbore size. They will trip out the 7 7/8 inch bit and run a 4 inch tri cone on 2 3/8 inch tubing back into the well tomorrow to continue the clean out process. |
1527771291 | 2018-05-31 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew mixed up pot ash into the mud to condition the wellbore before tripping out the 2.375 inch tubing for the bit change. The crew has a mechanical failure with the rig and has to shut down for the day to get the parts to commence the operation for tomorrow. |
1527866442 | 2018-06-01 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew has made repairs to fix a mechanical failure with the service rig. They tripped the 7 7/8 inch bit from the well to inspect it and ran back into the well with a 4 inch tapered mill to commenceme drilling out the well. The main pump was clogged with wood and was repaired. The decision was made to shut down the operation for the weekend. |
1528378311 | 2018-06-04 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. Crew has drilled the well down to 1205 feet. Crew has worked to clean and condition the wellbore before shutting down for the evening. The 7 inch casing believed to be ripped at 1148, working to determine if a 7 inch mill is needed to clean up the ripped casing in order to continue the drill out. Currently dragging the drill string on the rip point making it hard to continue drilling. |
1528737603 | 2018-06-11 | Plug / Plug Back | No Violations | On location with Doug Gonzalez with Gonzoil. Crew has removed all of the equipment from the location and are in the process of prepping the location for the vault and vent. |
1792194191 | 2018-05-29 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew has drilled through an obstruction at 37 feet before running into another obstruction at 630 feet. The obstruction is clay and they have made it down to 762 feet before shutting down for the evening. |
1793051379 | 2016-11-03 | Orphan | No Violations | Met on site this date with landowner and Lakewood Fire Chief Scott Gilman concerning possible orphaned well in back of property. Landowner stated that vegetation around suspected well will not grow. I probed soil, took readings with Sperian meter with no indications of gas leaking. Gaining access to the top of the 8 vent line, approximately 15 in the air, Sperian meter indicated 100% LEL, despite no apparent odor of gas. I advised landowner of the various programs available to get this well taken care of, and gave her the name/number of an approved contractor to possibly have the vent line reconfigured so as to possibly be less intrusive. New ROE form to be submitted. |
1936462261 | 2018-05-23 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew installed the well diverter and 4.5 inch hard lines to the steel pit to continue the drill out of the well. |
2116141340 | 2018-05-18 | Plug / Plug Back | No Violations | On location with Doug Gonzalez from Gonzoil. The crew is setting up the secondary containment for the two steel tanks, and pump in preparation to plug the well. |
558033627 | 2018-12-6 0:00: | FR | No Violations | |
620100490 | 2015-7-22 0:00: | OR | No Violations | |
692484941 | 2018-6-6 0:00:0 | PB | No Violations |
For data sources see[3]