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34-035-61203

Well Details

Well ID: 34-035-61203
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: EMERGENCY PLUGGING
Well Pad ID:
Farm/Lease Name: AMERI-CON HOMES
License Status: Final Restoration
License Date:
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.380000
Longitude: -81.580000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 2007-03-28 INSPECTED BY TOM HILL ON MARCH 15, 2007. WELL IS IN ORPHAN WELL PROGRAM. WELL IS LEAKING GAS AND A HOME AT 170 CREEKSIDE WAS EVACUATED BY EAST OHIO GAS DUE TO HIGH LEL READINGS. REFERRED AS AN EMERGENCY WELL BUT NO BIDDERS TO DATE BECAUSE OF THE TENDANCY
APP 2007-06-28 Proposed Formations:UNKNOWN, Issued Date:6/28/2007, Expired Date:6/27/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2007-07-17 Plugged by Orphan Well Program
Plugged/Abandoned 2007-07-17 INSPECTED BY TOM HILL ON MARCH 15, 2007. WELL IS IN ORPHAN WELL PROGRAM. WELL IS LEAKING GAS AND A HOME AT 170 CREEKSIDE WAS EVACUATED BY EAST OHIO GAS DUE TO HIGH LEL READINGS. REFERRED AS AN EMERGENCY WELL BUT NO BIDDERS TO DATE BECAUSE OF THE TENDANCY FOR ORPHAN WELLS IN THIS AREA TO UNLOAD DURING THE PLUGGING JOB. CONTRACTORS ARE CONCERNED ABOUT THE LIABILITY.

I&O CN 2005 10 058

Record Last Modified 2013-03-14 INSPECTED BY TOM HILL ON MARCH 15, 2007. WELL IS IN ORPHAN WELL PROGRAM. WELL IS LEAKING GAS AND A HOME AT 170 CREEKSIDE WAS EVACUATED BY EAST OHIO GAS DUE TO HIGH LEL READINGS. REFERRED AS AN EMERGENCY WELL BUT NO BIDDERS TO DATE BECAUSE OF THE TENDANCY FOR ORPHAN WELLS IN THIS AREA TO UNLOAD DURING THE PLUGGING JOB. CONTRACTORS ARE CONCERNED ABOUT THE LIABILITY.

I&O CN 2005 10 058

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1504421197 2007-7-6 0:00:0 DD No Violations
-1845989218 2007-6-26 0:00: DD No Violations
-2078697436 2007-7-17 0:00: PB No Violations 8.00
-314963015 2007-6-29 0:00: OR No Violations
-352565882 2007-7-2 0:00:0 OR No Violations
-57660391 2007-7-10 0:00: DD No Violations
0055196539 2007-07-05 Drill / Deepen / Reopen No Violations drilling cement 0-40
0057660391 2007-07-10 Drill / Deepen / Reopen No Violations driling at 115 finner cutting gassing 116 bit dropped 6-8 gassing and unload oil into 1/2 tank approx 70 bbls. Water truck on way to empty 1/2 tank.
0126892935 2007-10-02 Final Restoration No Violations
0314963015 2007-06-29 Orphan No Violations onsite started to clean out 10 approx 30 drilling something hard cant make any holeran vido camera on rod to see what we ar on nothing clear.10 still loose rigged up startto drive 10 made approx 4 casing still loosed rigged up pulled 10 pulled out the top 15 of the 10 and on bottom was the evadecne we drove on the lip of the clean out the inside of the 10 and set 85/8 inside the 10 and cemented with grout.shut in vented over weekend.
0352565882 2007-07-02 Orphan No Violations on site started to drill BOP on the 85/8 slow going .
0909522534 2007-07-11 Drill / Deepen / Reopen No Violations working on 1/2 tank and drilling 130 brick change bit to mill made 12 started to gas odor strong cheked area with gas meters 0% well and 1/2 tank and road.
1032961954 2007-07-03 Drill / Deepen / Reopen No Violations drilling to 108 well flowing back into 1/2 tank oil posible cable spiral patterns on collars . Cemented frim 100 to surface to lock in cable so it can be drilled out
1182883542 2007-06-26 Orphan No Violations Met on site with contractor Doug Gonzalez, representing Gonzoil Inc. Present is Rick Simmers, Harold Moravy, and Norburt Lowder of ODNR. Gonzoil is beginning to build location in preperation for plugging the oil and gas well across the street from 180 Creekside Drive in Garfield Heights, Ohio. At the end of the work day the silt fence has been installed. Earthen dike and sump is built to stop any spillage of fluids from leaving the site. Straw bails and sand bags are delivered to the site. Orange saftey fence has been constructed around the peremeter of the drilling location. Garfield Heights Fire department personel visited the site today. OUPS contractors arrived and located all utilities on the working area of the site. Work to continue on Wednesday, June 27,2007. Hot, 95 degrees.
1182953095 2007-06-27 Orphan No Violations Moved in service rig on well. Removed fence and post around well vent. Gasscope readings are 15% lel in post holes on south east side and 2% lel on south west side. 0% lel on north side of vent pipe. Removed plastic vent pipe and exposed 10 casing. Casing is angled in borehole. Pulled on 10 casing and set it straight in borehole. Bishop Well Service recommended drive casing be cemented and set for 24 hours before drilling inside casing. Staged 300 barrel tanks and 150 open barrel tanks on location. Bishop Well Service cut 10 casing off 4 below ground level with a cutting torch after lighting gas. Garfield Heights Fire Department was on site during cutting and welding of casing, but did not have to extiguish fire. All gas scope readings were 0 % lel during operations. Hot, 90 degrees.
1183036658 2007-06-28 Orphan No Violations Location is finished constructed according to plan and is approved to begin plugging process. Inspector has approved a change in surface casing from 8 5/8 casing to 7 casing to be set at approximatley 100 and cemented to surface. Started drilling out 10 casing to a depth of 20. Encountered rock ,red brick and wood. Circulation of drilling mud on annular side of 10 casing. Tripped out bit and drove 10 casing. It parted at 8. Pulled 8 of 10 casing and vented well . Gonzoil removed oil in steel pit before leaving location. Cloudy, 80 degrees. Wind west northwest.
1183138451 2007-06-29 Orphan No Violations Removed vent pipe and installed 23 of 8 5/8 casing inside 10 casing. Cemented 8 5/8 casing to surface with cement slurry. Bailed cement out of inside of casing to allow gas to vent over the weekend. Attached vent pipe on 8 5/8 casing. Replaced safety fence around location. Police Department will monitor site over weekend. Notified Fire Department Chief Tom Nemetz of schedule on Monday, July, 2, 2007. Called Mike McCormac and updated progress of well. Sun, 75 degrees.
1183380296 2007-07-02 Orphan No Violations Case # 01-008 I&O notified residents at 160, 170, 180, 190,195 Creekside Dr. that drilling is commencing today at 12:00 pm. Attached diverter to 8 5/8 casing and began to drill out brick, wood and fire clay. Reached depth of 97 and encountered crude oil in samples. Advised Doug Gonzalez to set 7 casing at this depth. Sun, 75 degrees. Mike McCormac and Norburt Lowder was on site.
1183546773 2007-07-03 Orphan No Violations Pulled drill pipe and bit to run 7 casing and well began to flow oil and gas. Called fire department on scene. Well continued to flow. Decision made to cement top 100 in well due to cable rapping around drill pipe. Pumpped 100 of class A cement with 2% cacl2. Well began to push cement out. Swedged in casing and vented well untill 7-5-2007.
1183585125 2007-07-05 Orphan No Violations Removed 8 5/8 swedge from casing and attached divertor head. Started drilling cemnt at top of casing and drilled 40 of cement by days end. Tripped out bit and attached heavy collars to add more weight to drill string. Gas still venting thru cement. Attached vent to casing and vented thru drilling pit. Sun, 85 degrees.
1183656497 2007-06-25 Drill / Deepen / Reopen No Violations on site Jay Cheslock Harold M. and Myself

put notices on all home on creek side And Knock on five home within area of well 190,180,170,160,and 175. Made personal contact with addrerss at 190,170,175 Met with Fire Dept to explain what to exect to see when drill out starts.

1183734073 2007-07-06 Orphan No Violations Well continues to vent gas thru divertor and in pit. Mud pump is not pumping properly. Shut down to repair pump before continue drilling of cement. Bishop Well service removed pit cuttings from drilling pit and stored in second steel pit on site. Pumped oil and drilling mud in 300 barrel tank to separate oil from mud. Pumped mud back to drilling pit before commencing drilling operations. Sun, 85 degrees.
1184021388 2007-07-09 Orphan No Violations Continued drilling out cement at 37. Hard drilling,four feet per hour. Stopped at 75 at end of day. Called by Sun Newspaper reporter and gave interview of plugging procedure and site construction. Referred contract requirements to Rick Simmers. Well still making gas thru vent. Circulated hole before shutting down. Hot, Sun 95 degrees.
1184151856 2007-07-10 Orphan No Violations Drilled out cement plug at 120 and well unloaded gas and oil for 3 hours. Approximatley 50 barrels of crude oil flowed in steel pit. Gonzoils water truck hauled out crude oil from pit. Doug Gonzalez stayed on site overnite to monitor gas venting from well. Norburt Lowder and Harold Moravy advised residents of situation. Fire Department stayed on site until 6:00 pm. Sun, Hot, Humid, 95 degrees.
1184251297 2007-07-12 Orphan No Violations Natural Gas continues to blow thru vent in steel pit. Obstruction at 130 and Bishop Well Service is fishing on obstruction. Preventor is used during fishing. Steel line attached to secondary steel pit to allow oil and gas to escape. Well will not blow down untill obstruction is removed. Wood from plug in hole is causing mud pump to build up pressure. Mill in well is plugged from wood chips. Removed small mill and installed 5 mill and drilled 50 thru wooden plug. Hole took 35 barrels of fluid. Oil and gas is subsiding at 180. Sun, 75 degrees
1188403539 2007-06-27 Orphan No Violations site construction rigging up
126892935 2007-10-2 0:00: FR No Violations
1359775128 2007-06-28 Orphan No Violations on site rigging up getting well ready to work on
1504421197 2007-07-06 Drill / Deepen / Reopen No Violations rebuilding mud pump not drilling today
1652927857 2007-07-11 Orphan No Violations Oil flow stopped overnite but gas continues to vent thru steel pit. Continue clean out of well bore. Changed over to a mill at 130 due to obstruction. 6 mill would not penetrate obstruction. Changed to 4 1/2 mill and drill string began to move down hole. After milling 4 wood chips plugged off mill ports and gas and oil began to flow at high pressure. Shut down engines and mud pumps to allow well to blow off oil and gas. Called water truck in to pump steel pit of oil. Approximatley 20 barrels of oil flowed. Sun, 78 degrees.
1845989218 2007-06-26 Drill / Deepen / Reopen No Violations On site Harold M. Rick S. Myself and contracted company

make site spill controls Dikes along east and south perimeterssump in south west corner

1947255672 2007-07-09 Drill / Deepen / Reopen No Violations drilling at 100 just making head way able to put weight on bit
2078697436 2007-07-17 Plug / Plug Back No Violations Plugged and abandoned well today. Set Class A cement plug from 1580 - 1180. Pulled drill pipe to 400 and set a class a cement plug from 400 - 100. Pulled drill pipe to 100 and set a 100 - surface class a cement plug. Topped off well and shut in on swedge. Lost 3 7/8 mill in well while pulling drill string. Division has to pat for loss of mill and change over pin. Approximate cost is $ 3500.00.
55196539 2007-7-5 0:00:0 DD No Violations
909522534 2007-7-11 0:00: DD No Violations

For data sources see[3]

References