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34-031-27232

Well Details

Well ID: 34-031-27232
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Country: United States
State: Ohio
County: Coshocton
Municipality: Pike Township
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name: MOORE ALICE
License Status: Producing
License Date: 2013-11-29
Spud Date: 2014-02-26
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2014-03-02
Well Total Depth: 3355.00 ft
Configuration: Vertical
Latitude: 40.190000
Longitude: -82.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2013-11-29 Proposed Formations:BEREA THRU CLINTON, Issued Date:11/29/2013, Expired Date:11/29/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Correction to Well 2013-12-06 CORRECTION TO SURFACE FOOTAGE.
Reached Total Depth 2014-03-02
Completion Report Received 2014-06-05
Construction Permit Expires 2015-11-29
Record Last Modified 2019-06-11

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2014-03-21 H2O 15 55192 Bbl 30000 Producers Service Corporation

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 KNOX ENERGY INC. 0.00 451.00 182
2015 KNOX ENERGY INC. 0.00 569.00 365
2016 KNOX ENERGY INC. 0.00 267.00 365
2017 KNOX ENERGY INC. 0.00 317.00 365
2018 KNOX ENERGY INC. 0.00 278.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 KNOX ENERGY INC. Brine 188 182
2015 KNOX ENERGY INC. Brine 19 365
2016 KNOX ENERGY INC. Brine 1 365
2017 KNOX ENERGY INC. Brine 0 365
2018 KNOX ENERGY INC. Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-719464871 2014-2-27 0:00: CS No Violations
0464169712 2014-02-27 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Kilbarger Drilling rig 5 had set 70 of new 11.75 conductor casing that was cemented to surface by Petroset. They were drilling the 11 surface hole at a depth of 291. The permit was posted, there were no sags or tears in the pit liner and I found no leaks or spills.
0719464871 2014-02-27 Casing String Witnessed No Violations On the day of my inspection I found that Kilbarger Drilling rig 5 ran new 8.625 casing to 537. Petroset broke circulation and cemented the casing to surface with 150 sacks of class A cement. Good circulation was maintained throughout the job, with approximately 8 barrels of cement returns.
1393138431 2014-03-05 Drill / Deepen / Reopen No Violations On the day of my inspection I found that Kilbarger Drilling had reached a total depth of 3355. Petroset cemented 3330 of used, tested and drifted 4.5 casing with 100 sacks of class A cement on 3/3/14. The pits were still open. The fluid level was approximately 10 to 12 inches down and there were no sags or tears in the pit liners. The well was shut in and I found no leaks or spills around the drill site.
1525214494 2020-9-8 0:00:0 PW No Violations 0.50
1544338676 2014-08-15 Preliminary Restoration No Violations On the day of my inspection I found that the drill site had been graded out and planted. The site was approximately 90% covered in well established tall grasses. I found no drilling materials or debris. This site passes preliminary restoration.
464169712 2014-2-27 0:00: DD No Violations

For data sources see[8]

References