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34-031-25460

Well Details

Well ID: 34-031-25460
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Country: United States
State: Ohio
County: Coshocton
Municipality: Washington Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: JEWITT RUSSELL
License Status: Producing
License Date: 1984-09-21
Spud Date: 1984-10-24
Spud Drilling Contractor: H & S DRLG
Final Drill Date: 1984-12-07
Well Total Depth: 3532.00 ft
Configuration: Vertical
Latitude: 40.170000
Longitude: -82.080000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-09-21 Issued Date 9/21/84 Expired Date 3/20/85 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03532 Proposed Drill Depth 03532
Original Spud 1984-10-24 FDT=GRAY
Completed 1984-12-07 FDT=GRAY
Reached Total Depth 1984-12-07 FDT=GRAY
Completion Report Received 1984-12-21 FDT=GRAY
CO 1984-12-28 6 BENATTY CORP GeoDate 9/21/84
Construction Permit Expires 1985-03-20 FDT=GRAY
Change of Owner 1998-09-22 Operator changed from 1619, BROWN PHILLIP OIL & GAS to 1634, NORTHWOOD ENERGY CORP
Record Last Modified 2017-02-15 FDT=GRAY

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3478 3526 0
3478 3526 0
2006-09-11 3479 3515 14
3479 3515 14
3478 3526 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 63000 Gal 30000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 BENATTY CORP 0.00 1221.00 0
1986 BENATTY CORP 0.00 586.00 365
1987 BENATTY CORP 0.00 579.00 365
1988 BENATTY CORP 0.00 382.00 365
1989 BENATTY CORP 0.00 298.00 365
1990 BENATTY CORP 0.00 266.00 365
1991 BENATTY CORP 0.00 223.00 365
1992 BENATTY CORP 0.00 215.00 326
1993 BENATTY CORP 0.00 148.00 365
1994 BENATTY CORP 0.00 0.00 0
1995 BENATTY CORP 0.00 225.00 365
1996 BENATTY CORP 0.00 546.00 365
1997 BROWN PHILLIP H JR. CORPORATIO 0.00 335.00 275
1998 BROWN PHILLIP H JR. CORPORATIO 0.00 0.00 0
1999 NORTHWOOD ENERGY CORP 0.00 560.00 365
2000 NORTHWOOD ENERGY CORP 0.00 341.00 365
2001 NORTHWOOD ENERGY CORP 0.00 265.00 365
2002 NORTHWOOD ENERGY CORP 0.00 155.00 365
2003 NORTHWOOD ENERGY CORP 0.00 226.00 365
2004 NORTHWOOD ENERGY CORP 0.00 273.00 365
2005 NORTHWOOD ENERGY CORP 0.00 213.00 365
2006 NORTHWOOD ENERGY CORP 0.00 184.00 365
2007 NORTHWOOD ENERGY CORP 0.00 194.00 365
2008 NORTHWOOD ENERGY CORP 0.00 185.00 365
2009 NORTHWOOD ENERGY CORP 0.00 161.00 365
2010 NORTHWOOD ENERGY CORP 0.00 188.00 365
2011 NORTHWOOD ENERGY CORP 0.00 212.00 0
2012 NORTHWOOD ENERGY CORP 0.00 255.00 366
2013 NORTHWOOD ENERGY CORP 0.00 143.00 365
2014 NORTHWOOD ENERGY CORP 0.00 137.00 365
2015 NORTHWOOD ENERGY CORP 0.00 170.00 365
2016 NORTHWOOD ENERGY CORP 0.00 153.00 365
2017 NORTHWOOD ENERGY CORP 0.00 240.00 365
2018 NORTHWOOD ENERGY CORP 0.00 141.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 BENATTY CORP Brine 0 0
1986 BENATTY CORP Brine 0 365
1987 BENATTY CORP Brine 0 365
1988 BENATTY CORP Brine 0 365
1989 BENATTY CORP Brine 0 365
1990 BENATTY CORP Brine 0 365
1991 BENATTY CORP Brine 0 365
1992 BENATTY CORP Brine 0 326
1993 BENATTY CORP Brine 0 365
1994 BENATTY CORP Brine 0 0
1995 BENATTY CORP Brine 0 365
1996 BENATTY CORP Brine 0 365
1997 BROWN PHILLIP H JR. CORPORATIO Brine 0 275
1998 BROWN PHILLIP H JR. CORPORATIO Brine 0 0
1999 NORTHWOOD ENERGY CORP Brine 365
2000 NORTHWOOD ENERGY CORP Brine 365
2001 NORTHWOOD ENERGY CORP Brine 365
2002 NORTHWOOD ENERGY CORP Brine 365
2003 NORTHWOOD ENERGY CORP Brine 0 365
2004 NORTHWOOD ENERGY CORP Brine 0 365
2005 NORTHWOOD ENERGY CORP Brine 0 365
2006 NORTHWOOD ENERGY CORP Brine 0 365
2007 NORTHWOOD ENERGY CORP Brine 0 365
2008 NORTHWOOD ENERGY CORP Brine 14 365
2009 NORTHWOOD ENERGY CORP Brine 30 365
2010 NORTHWOOD ENERGY CORP Brine 29 365
2011 NORTHWOOD ENERGY CORP Brine 0
2012 NORTHWOOD ENERGY CORP Brine 2 366
2013 NORTHWOOD ENERGY CORP Brine 2 365
2014 NORTHWOOD ENERGY CORP Brine 2 365
2015 NORTHWOOD ENERGY CORP Brine 0 365
2016 NORTHWOOD ENERGY CORP Brine 7 365
2017 NORTHWOOD ENERGY CORP Brine 18 365
2018 NORTHWOOD ENERGY CORP Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1074861557 2003-4-2 0:00:0 PW No Violations
-1263423290 2017-5-19 0:00: PW No Violations 3.00
-1309323188 2006-2-13 0:00: PW No Violations
-1595345641 2017-12-11 0:00 PW No Violations 0.70
-693318001 2017-5-11 0:00: PW No Violations 2.00
00CENA1007 1999-09-24 Production Wells Violations Noted 1501:9-1-07
0571372866 2017-05-10 Production Wells Violations Noted I received a phone call from Jessica Williams to report oil contamination from a leak at a well on her property. I met Mrs. Williams at the site to look at the well. She claimed that back in January, 2017 her and her husband found the well spraying oil from the stuffing box while the pumping unit was in operation. The unit is powered with an electric motor and cycles automatically. The unit turned on two times while I was conducting my inspection. Mrs. Williams claimed that no one came out to check the well until two days after she reported the issue. She said that Corp Oilfield Services came back out one to two weeks later with a mini hoe and a dump truck. Northwood Energy did not notify me of the leak. The front of the unit was covered in crude oil spray. The soil around the front of the unit and around the wellhead was black with crude oil. There was also oil soaked peat spread around the wellhead, around the perimeter of the affected area and in the vegetation where the oil had run down into the woods. There was a 10 to 15 foot diameter area of bare soil in front of the wellhead. I dug into the soil and found no contamination underneath. The bare soil extended another 15 to 20 feet into the woods. There were multiple empty peat bags left around the unit and in the woods. I called Mike Corp, contractor for Northwood Energy to ask about the leak. He claimed that they lost 25 to 30 gallons of oil. I told Mike that the area still needed a lot of work and I let him know I was issuing a compliance notice to Northwood. I gave Mike 30 days to get the site cleaned up. I also found a 3 foot by 15 foot path of oil stained, water soaked soil running down hill from the 100 barrel production tank toward CR 436. There was not a dike around the tank, and the side of the tank was stained from being run over. The path of oil stained soil did not extend to the roadside ditch. All contaminated soil and oil soaked peat must be removed from around the pumping unit, wellhead and surr
0693318001 2017-05-11 Production Wells No Violations On the day of my inspection I found that a crew from Corp Oilfield Services was on site to work on the clean-up. They used a skid-loader to remove the oily soil and peat from the tree line, and they shoveled out around the wellhead. The crew also constructed a small dike around the wellhead. Mike Corp called to ask my opinion while I was still at the well site. I told him that the tree line and wellhead still needed work and they still left old peat moss bags and a five gallon bucket around the pumping unit. I also told Mike that they need to address the oil impacted soil around the 100 barrel tank. He said that he would call me when they were finished.
1074861557 2003-04-02 Production Wells No Violations n.o.v. resolved .
1263423290 2017-05-19 Production Wells No Violations I received an email from Jessica Williams to let me know that they were not happy with Corp Oilfield Services clean-up. On the day of my inspection I found that the oil stained soil around the production tank was still in place. It had been scratched at with shovels, but remained in place. I also noticed a small pool of discolored water collected in the soil next to the tank. I conducted a field test for chlorides with a high range Quantab test strip. The titrator maxed out at 9.0 units, which indicated that the chloride content of the water was greater that 6907 ppm(mg/L) or 1.139% NaCl. Nothing has been done around the pumping unit or in the tree line. I called Bill Arnholt with Northwood Energy and left a voice message. Bill returned my call and we set up a meeting at the site on Monday morning.
1309323188 2006-02-13 Production Wells No Violations Well in production , 1-100 bl. Tank not diked
1494860817 2017-05-15 Production Wells No Violations I was contacted by landowner Jessica Williams to ask if I could meet her out at the site to look at the work that had been done to clean the area up. I found that nothing more had been done. There was still oily peat caked around the base of the pumping unit and the soil packed around the wellhead was still oil stained. Corp Oilfield Service had pushed soil around the wellhead as a partial dike, but the soil was littered with oily rags and old work gloves. There were also several spots on the dike where oil stains were coming up through the soil. Corp pushed some of the oily soil up against the trees around the perimeter of the area that they attempted to clean in the tree line. There were several spots where oil staining was coming up through the soil. I dug down into the soil and hit pockets of crude oil that were buried. The hillside below the dike was scratched up with some shovel marks, but it was still oil stained. I called Mike Corp again and he said that he would be back out to look at the site.
1495469882 2017-05-22 Production Wells No Violations On the day of my inspection I met Bill Arnholt and Mike Corp at the well site. Corp already had a crew there working on the clean-up. The crew excavated all of the remaining oily soil from the tree line and from the wellhead dike. They removed all of the old oily rags, gloves and pieces of gas line. They also removed all of the old oily peat from around the pumping unit. I told Bill and Mike that I was satisfied with the work, but I still wanted them to treat the area with a mixture of lime and fertilizer or BioSorb before seeding and covering with straw. We also looked at the 100 barrel tank site. Bill and Mike agreed to eliminate the tank site along the road and put a new tank in back by the well. They plan to excavate all of the oil and brine affected soil at the tank site once they get the old tank removed. I called Jessica Williams and she met me at the site after the crew had left. We walked around the site and she said that she was also satisfied with the current state of the clean-up. I explained to her that I would have them treat the area to neutralize any residual hydrocarbons and then they would establish a vegetative cover to prevent erosion.
1496758218 2017-06-05 Production Wells No Violations On the day of my inspection I found that the 100 barrel tank had been removed from the roadside location. The oil stained soil had been removed and the area was covered in straw. The well site was also covered in straw. There was a different 100 barrel tank set in an earthen dike back near the wellhead. Correct, legible identification was posted and there were no leaks. The compliance notice is resolved.
1595345641 2017-12-11 Production Wells No Violations On the day of my inspection I found that the area where the production tank used to be located was completely restored. The grass and weeds were grown in and there were no signs of residual contamination. The well site was also covered in vegetation and free of crude oil. There was no identification on the tank or pumping unit. I called Mike Corp who said that the sign had blown off and he would paint the ID on the side of the tank. I asked that call me when it was up.
571372866 2017-5-10 0:00: PW No Violations 3.00
CENA1007 1999-9-24 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
00CENA1007 US-OH-131496 Well operation causing pollution and contamination
0571372866 US-OH-126417 2017-06-14 Well operation causing pollution and contamination

For data sources see[9]

References