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34-031-25324

Well Details

Well ID: 34-031-25324
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Country: United States
State: Ohio
County: Coshocton
Municipality: Keene Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: DREHER DAVID L UNIT
License Status: Final Restoration
License Date: 2014-06-26
Spud Date: 1984-08-10
Spud Drilling Contractor: NAU DRLG
Final Drill Date: 1984-10-04
Well Total Depth: 4063.00 ft
Configuration: Vertical
Latitude: 40.330000
Longitude: -81.830000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-03-27 Issued Date 3/27/84 Expired Date 9/23/84 Acres 0442100 Tool Type CT Proposed Formation CLINTON Proposed Depth 04063 Proposed Drill Depth 04063
Original Spud 1984-08-10
Completed 1984-10-04
Reached Total Depth 1984-10-04
CO 1985-01-29 124 MOORE JERRY INC GeoDate 3/27/84
Completion Report Received 1985-01-31
Change of Owner 1999-10-21 Operator changed from 4884, EASTERN STATES OIL & GAS INC to 1634, NORTHWOOD ENERGY CORP
APP 2014-06-26 Proposed Formations:CLINTON, Issued Date:6/26/2014, Expired Date:6/25/2016 12:00:00 PM, Drilling unit acres:442.1, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-09-09
Construction Permit Expires 2016-06-25
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3908 3990 0
3908 3990 0
3908 3990 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 0 0
H2O 0 43000 Gal 40000 FRAC;H2O,SAND,N2
ACID 15 300 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 JERRY MOORE INC 5654.00 199.00 365
1987 JERRY MOORE INC 1120.00 44.00 365
1988 JERRY MOORE INC 1239.00 31.00 365
1989 JERRY MOORE INC 292.00 59.00 365
1990 JERRY MOORE INC 339.00 51.00 365
1991 JERRY MOORE INC 38.00 30.00 365
1992 JERRY MOORE INC 0.00 0.00 365
1993 JERRY MOORE INC 0.00 0.00 365
1994 JERRY MOORE INC 46.00 0.00 365
1995 JERRY MOORE INC 16.00 0.00 365
1996 JERRY MOORE INC 9.00 0.00 365
1997 EASTERN STATES OIL & GAS INC 22.00 0.00 365
1998 EASTERN STATES OIL & GAS INC 65.00 0.00 365
1999 NORTHWOOD ENERGY CORP 95.00 0.00 365
2000 NORTHWOOD ENERGY CORP 2057.00 172.00 365
2001 NORTHWOOD ENERGY CORP 1829.00 42.00 365
2002 EASTERN STATES OIL & GAS INC 508.00 0.00 365
2003 NORTHWOOD ENERGY CORP 1527.00 0.00 365
2004 NORTHWOOD ENERGY CORP 1188.00 45.00 365
2005 NORTHWOOD ENERGY CORP 1253.00 35.00 365
2006 NORTHWOOD ENERGY CORP 1311.00 0.00 365
2007 NORTHWOOD ENERGY CORP 1166.00 55.00 365
2008 NORTHWOOD ENERGY CORP 901.00 0.00 365
2009 NORTHWOOD ENERGY CORP 644.00 42.00 365
2010 NORTHWOOD ENERGY CORP 692.00 69.00 365
2011 NORTHWOOD ENERGY CORP 620.00 70.00 0
2012 NORTHWOOD ENERGY CORP 548.00 66.00 366
2013 NORTHWOOD ENERGY CORP 419.00 69.00 365
2014 NORTHWOOD ENERGY CORP 428.00 122.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 JERRY MOORE INC Brine 0 365
1987 JERRY MOORE INC Brine 0 365
1988 JERRY MOORE INC Brine 0 365
1989 JERRY MOORE INC Brine 0 365
1990 JERRY MOORE INC Brine 0 365
1991 JERRY MOORE INC Brine 0 365
1992 JERRY MOORE INC Brine 0 365
1993 JERRY MOORE INC Brine 0 365
1994 JERRY MOORE INC Brine 0 365
1995 JERRY MOORE INC Brine 0 365
1996 JERRY MOORE INC Brine 0 365
1997 EASTERN STATES OIL & GAS INC Brine 365
1998 EASTERN STATES OIL & GAS INC Brine 365
1999 NORTHWOOD ENERGY CORP Brine 365
2000 NORTHWOOD ENERGY CORP Brine 365
2001 NORTHWOOD ENERGY CORP Brine 365
2002 NORTHWOOD ENERGY CORP Brine 365
2003 NORTHWOOD ENERGY CORP Brine 0 365
2004 NORTHWOOD ENERGY CORP Brine 0 365
2005 NORTHWOOD ENERGY CORP Brine 0 365
2006 NORTHWOOD ENERGY CORP Brine 0 365
2007 NORTHWOOD ENERGY CORP Brine 44 365
2008 NORTHWOOD ENERGY CORP Brine 0 365
2009 NORTHWOOD ENERGY CORP Brine 26 365
2010 NORTHWOOD ENERGY CORP Brine 0 365
2011 NORTHWOOD ENERGY CORP Brine 38
2012 NORTHWOOD ENERGY CORP Brine 0 366
2013 NORTHWOOD ENERGY CORP Brine 0 365
2014 NORTHWOOD ENERGY CORP Brine 45 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1583816189 2014-9-10 0:00: PB No Violations
-715918791 2006-3-6 0:00:0 PW No Violations
0715918791 2006-03-06 Production Wells No Violations Well in production , 1-100 bl. Tank at well site , not diked .
1173205438 2007-03-06 Production Wells No Violations Complaint of lease road erosion . Lease road is approximately 3/4 of a mile long . Last 1/4 mile going into well has tire ruts 6 to 8 deep in road way . Meet with Bill Arnolt 5/4/07 went over work needed at site . Restoration of lease road is to be comp
1399987924 2007-06-04 Production Wells No Violations Lease road repaired , compliance . Meet with landowner this date .
1410184409 2014-09-08 Plug / Plug Back No Violations On the day of my inspection Cemenco bullheaded a 400 bottom plug through 2.875 casing. Appalachian Well Surveys shot the casing off at 2900. RB Drilling pulled the casing up to 2828 and Cemenco tried to break circulation. The pressure repeatedly increased to 1000 psi indicating that the hole was caving in around the pipe, so RB Drilling pulled 100 of casing. Cemenco tried to break circulation again. The lift pressure decreased to show that the cave in was moving up the hole. Cemenco pumped a 300 Big Lime plug. RB Drilling pulled the casing up to 1122. Cemenco established circulation and pumped a 174 Berea plug. RB Drilling pulled the remaining 2.875 casing from the well. The 8.625 casing parted down hole when they tried to pull it. The casing was rotted off and full of large holes. RB Drilling got 65 of 8.625 casing out of the well.
1583816189 2014-09-10 Plug / Plug Back No Violations On 9/9/14 RB Drilling ran 1.5 tubing to 560 and Cemenco cemented the well to surface with 165 sacks of class A cement. On the day of my inspection I found that the cement had settled to approximately 8 down. Northwood Energy cut the casing off and capped the well with a steel plate inscribed with the permit number.
1755990223 2015-05-11 Final Restoration No Violations On the day of my inspection I met with Mark Fluharty, pumper for Northwood, to go over the restoration. I found that the pit was closed, and the production equipment was removed. The site was graded out to the approximate contour of the surrounding landscape. The site was covered in well established vegetation. I found no signs of erosion. Northwood had a landowner waiver (form 5) signed to leave the road in place.

For data sources see[9]

References