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34-031-23481

Well Details

Well ID: 34-031-23481
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Country: United States
State: Ohio
County: Coshocton
Municipality: Bethlehem Township
Operator Name: KMFAD OIL AND GAS LLC
Well Pad ID:
Farm/Lease Name: HARTSOCK GEORGE
License Status: Producing
License Date: 1979-03-16
Spud Date: 1979-03-17
Spud Drilling Contractor:
Final Drill Date: 1979-04-03
Well Total Depth: 3627.00 ft
Configuration: Vertical
Latitude: 40.360000
Longitude: -81.990000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-03-16 124 MOORE JERRY INC GeoDate 3/16/79
Original Spud 1979-03-17
Completed 1979-04-03
Reached Total Depth 1979-04-03
Change of Owner 2003-03-06 Operator changed from 124, MOORE JERRY INC to 7404, A S N F PRODUCING INC
Change of Owner 2014-08-19 Operator changed from 7404, A S N F PRODUCING INC to 9316, KMFAD OIL AND GAS LLC
Record Last Modified 2019-06-04

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3528 3586 52
3528 3586 52
3528 3586 52

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
N2 0 100 0 SCF/BBL.
H2O 0 48400 Gal 45000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 JERRY MOORE INC 3795.00 430.00 0
1985 JERRY MOORE INC 2462.00 309.00 0
1986 JERRY MOORE INC 1724.00 73.00 365
1987 JERRY MOORE INC 1098.00 196.00 365
1988 JERRY MOORE INC 1554.00 116.00 365
1989 JERRY MOORE INC 3886.00 350.00 365
1990 JERRY MOORE INC 3332.00 250.00 365
1991 JERRY MOORE INC 621.00 150.00 365
1992 JERRY MOORE INC 1360.00 97.00 365
1993 JERRY MOORE INC 1063.00 37.00 365
1994 JERRY MOORE INC 1178.00 97.00 365
1995 JERRY MOORE INC 1388.00 122.00 365
1996 JERRY MOORE INC 883.00 92.00 365
1997 JERRY MOORE INC 2529.00 240.00 365
1998 JERRY MOORE INC 244.00 0.00 365
1999 JERRY MOORE INC 900.00 91.00 365
2000 JERRY MOORE INC 2205.00 104.00 365
2001 JERRY MOORE INC 447.00 45.00 365
2002 JERRY MOORE INC 564.00 27.00 365
2003 JERRY MOORE INC 15.00 0.00 365
2004 A S N F PRODUCING INC 103.00 56.00 365
2005 A S N F PRODUCING INC 99.00 23.00 365
2006 A S N F PRODUCING INC 48.00 43.00 365
2007 A S N F PRODUCING INC 44.00 16.00 365
2008 A S N F PRODUCING INC 33.00 67.00 365
2009 A S N F PRODUCING INC 52.00 40.00 365
2010 A S N F PRODUCING INC 42.00 43.00 365
2011 A S N F PRODUCING INC 0.00 41.00 365
2012 A S N F PRODUCING INC 0.00 61.00 366
2013 A S N F PRODUCING INC 0.00 36.00 365
2014 KMFAD OIL AND GAS LLC 0.00 23.00 365
2015 KMFAD OIL AND GAS LLC 0.00 0.00 365
2016 KMFAD OIL AND GAS LLC 0.00 32.00 365
2017 KMFAD OIL AND GAS LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 JERRY MOORE INC Brine 0 0
1985 JERRY MOORE INC Brine 0 0
1986 JERRY MOORE INC Brine 0 365
1987 JERRY MOORE INC Brine 0 365
1988 JERRY MOORE INC Brine 0 365
1989 JERRY MOORE INC Brine 0 365
1990 JERRY MOORE INC Brine 0 365
1991 JERRY MOORE INC Brine 0 365
1992 JERRY MOORE INC Brine 0 365
1993 JERRY MOORE INC Brine 0 365
1994 JERRY MOORE INC Brine 0 365
1995 JERRY MOORE INC Brine 0 365
1996 JERRY MOORE INC Brine 0 365
1997 JERRY MOORE INC Brine 0 365
1998 JERRY MOORE INC Brine 0 365
1999 JERRY MOORE INC Brine 0 365
2000 JERRY MOORE INC Brine 0 365
2001 JERRY MOORE INC Brine 0 365
2002 JERRY MOORE INC Brine 0 365
2003 JERRY MOORE INC Brine 0 365
2004 A S N F PRODUCING INC Brine 0 365
2005 A S N F PRODUCING INC Brine 0 365
2006 A S N F PRODUCING INC Brine 0 365
2007 A S N F PRODUCING INC Brine 0 365
2008 A S N F PRODUCING INC Brine 20 365
2009 A S N F PRODUCING INC Brine 0 365
2010 A S N F PRODUCING INC Brine 15 365
2011 A S N F PRODUCING INC Brine 0 365
2012 A S N F PRODUCING INC Brine 0 366
2013 A S N F PRODUCING INC Brine 0 365
2014 KMFAD OIL AND GAS LLC Brine 0 365
2015 KMFAD OIL AND GAS LLC Brine 0 365
2016 KMFAD OIL AND GAS LLC Brine 0 365
2017 KMFAD OIL AND GAS LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1059963885 2020-7-16 0:00: PW No Violations 0.40
-119640330 2016-8-18 0:00: AM No Violations 0.50
-166851786 2017-2-6 0:00:0 PW No Violations 1.50
-1864354217 2016-8-19 0:00: PW No Violations 2.00
0119640330 2016-08-18 Administrative Inspection No Violations I received an email from Carrie Moore of KMFAD Oil and Gas requesting another 30 day extension on the compliance notice to plug this well. I spoke with Southeast District Supervisor Mike Moreland about the request. We agreed to grant the extension only after contacting Carrie to get a more detailed account of the action plan for the well. I called Carrie and spoke with her about her plan. She claimed that they were in the process of reconnecting the electric box, and installing a high speed gear in order to pump the well. I asked if she could meet me at the well to demonstrate the actions being taken to put the well back into production. She agreed to meet me on 8/19/16. I will grant the extension if she can show that they are actively working to resolve the issues preventing the well from being produced.
0166851786 2017-02-06 Production Wells No Violations On the day of my inspection I found that there was an electric motor mounted on the pumping unit. The drive belts were in place. The electric was connected to the motor and in the box, but the breaker was in the off position. The flow lines were connected at the wellhead, but the all of the valves were closed. The main valve to the separator was also closed. There was a gauge on the separator that showed 2 pounds. The 100 barrel steel tank was empty. No production reports have been filed for 2015. I called Carrie Moore about the status of this well. She claimed that they had treated the well with solvent and it was capable of production. She said that she has been in legal negotiations with the landowner George Hartsock and that has prevented her from doing anything with well. She claimed that they have come to an agreement and she was scheduled to put the well into production on 2/15/17. She also said that she has contracted Jim Dunfee to pump the wells for her.
0844534268 2016-04-19 Production Wells Violations Noted This inspection was conducted in response to complaint #5306. On the day of my inspection I met with the landowner George Hartsock to inspect the well. I found that the well was equipped with an electric powered pumping unit. The surface casing head was buried and not accessible. The tubing valves were both closed. The electric was disconnected at the box. The belts were off of the motor, and the drive shaft and sheave had been removed from the gear box. I conducted a field inspection of this well on 4/30/15 and found the well to be in the same condition. The inspection documents that I contacted Carrie Moore about the well, and she claimed that parts were on order to repair the pumping unit. Mr. Hartsock claimed that the well has been sitting in its current condition for 3 years and he wants the well plugged. The tank battery consisted of one 100 barrel steel tank and one horizontal separator. There was no earthen dike around the production equipment. The tank battery is shared with permit 3445. The identification on the tank only shows information for permit 3481 and there was no identification posted at the wellhead. I found no leaks or spills around the wellhead. There was some staining on the ground under the motor valve on the separator. The well is incapable of production in its current condition. The well owner/operator shall submit a written plugging schedule to Chris Grimm at 5880 Memory Rd, Zanesville, OH 43701 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
0953120596 2016-10-14 Production Wells No Violations On the day of my inspection I found that the electric was wired in the box and connected at the motor. The drive belts were in place. The tubing and casing valves were closed. The polished rod showed some signs of recent use. I called Carrie Moore to get an update on the status of the well. She said that it is currently capable of pumping, but there was quite a bit of paraffin downhole that was diminishing there fluid and gas production. She claimed that the well was pumping too fast and they were currently in the process of procuring a jack shaft to decrease the strokes and start to pump the paraffin out. I reminded her that the compliance notice was due to be resolved by 10/19/16. She said that they would get to work on it, and asked that I meet her out here on 10/18/16 to observe their progress.
1156412027 2018-11-07 Production Wells No Violations On the day of my inspection I found that the access road to the well was clear and easily passable. The solvent tank and extra motor had been removed from the well site. There were still no drive belts on the motor that was mounted on the pumping unit. The casing valves were open and the tubing valve was closed. There was not a gauge in place to determine if there was any gas pressure at the wellhead. The gauge on the separator showed 10 pounds. The 100 barrel tank was empty. A compliance notice was issued in 2016, requiring this well to be plugged by 10/19/16. There are no records of a plugging permit ever being issued for this well.
1411732582 2017-08-07 Production Wells No Violations On the day of my inspection I found that the well was still idle. I called Carrie Moore and got no answer. I called the pumper Rick Pace and he said that they have treated the well with solvent, but they cant get it to pump. He said that they need a service rig, but he could not give me an idea of when or if they will get a rig in to change the pump.
1444015614 2017-03-20 Production Wells No Violations On the day of my inspection I found that the well was still idle. The electric and the motor were all connected, but the well showed no signs of recent use. I met with Carrie Moore at the tank battery site. She was out to work on the compressor unit. She claimed that they wanted to give the well one more treatment with condensate and then it would be ready to produce.
1452159957 2015-04-30 Production Wells No Violations On the day of my inspection I found that the wellhead was equipped with a pumping unit. The valve was open. The motor was disconnected from the gearbox. I called Carrie Moore, who claimed that the parts were on order to repair the unit. The tank battery consisted of one 100 barrel tank and one separator. Identification was posted and I found no leaks or spills. This well shares a tank battery with permit 3445.
1463581818 2016-05-18 Administrative Inspection No Violations I received phone calls from Carrie Moore of KMFAD Oil & Gas, and from landowner George Hartsock in regards to the complaint on this well. Carrie called to update me on her course of action to bring the well into compliance. She claimed that she had both Hartsock wells shut in to test the system and Mr. Hartsocks house gas would be shut off during this phase. Mr. Hartsock called to report that his house gas was shut off, and he wanted to know what she was doing to the well. He was also wanted to know if she was allowed to put the well back into production rather than plug, and what she had to do to bring the well into compliance with regards to production. I told Mr. Hartsock that she had until October 19, 2016 to either plug the well or demonstrate that it is capable of viable production. I also told Mr. Hartsock that minimum production is defined as 100 mcf gas or 15 barrels of oil in one year.
1476975368 2016-10-19 Production Wells No Violations On the day of my inspection I met with Mike Ingalls of KMFAD at the well site. The pumping unit was in operation when I arrived. Mike had a container to catch fluid attached to a nipple off of the tubing. He claimed that he thought he could pump the paraffin out. The jug was empty when he shut the unit down. Mike claimed that the rods and pump were free, but there was too much paraffin downhole to make any fluid. He claimed that the well was making gas, but had no was of proving that gas was being produced in commercially viable quantities. I reminded Mike that they have had six months to either make the well capable of production, or have it plugged. I recommended that he take immediate actions, such as solvent treatment, or steaming the tubing and rods to remedy the paraffin. I also reminded him that the well has a complaint filed on it and a compliance notice that was due today. I also spoke with Carrie Moore of KMFAD to discuss the same options. I am not granting them an extension.
1527874072 2018-06-01 Production Wells No Violations On the day of my inspection I found that the access road was passable by vehicle, but it was completely grown over with waist high grass. There were no signs of any recent vehicle or foot traffic to the well. The pumping unit was in a state of abandonment. There were two electric motors at the pumping unit. One was mounted to the unit and the other was laying to the side. There were no drive belts to connect the motor to the gear box. There was a solvent drum next to the wellhead and the lines were connected. The tubing valves were closed and the casing valve was partially opened. I tried to call Carrie Moore and she would not answer her phone. This well was required to be plugged and abandoned by 10/19/16. Nothing has been done recently to put this well back into production, and there has been no application submitted for a permit to plug this well.
1555504605 2019-04-16 Production Wells No Violations On the day of my inspection I was accompanied to the well site by SE Regional Supervisor Brent Bear. We found that the well was equipped with an electric powered pumping unit. There was an electric motor mounted to the unit, but there were no drive belts and the electric switch was in the off position. The flow lines were connected at the wellhead. The tubing valves were closed. One casing valve was open to the solvent drip bottle, and the other casing valves was partially opened to the flow line. There were no leaks around the wellhead. The production equipment is shared with permit 3445. We did not inspect the production equipment on this day. The landowner claims that his well has not been produced since 2013. There has been zero oil or gas production reported for this well since 2016. This well has an outstanding compliance notice to be plugged, with a remedy date of 10/19/2016. I took updated photographs of the pumping unit and production equipment site.
1708127471 2019-10-10 0:00 PW No Violations 0.70
1864354217 2016-08-19 Production Wells No Violations On the day of my inspection I met with Carrie Moore at the well site. She demonstrated that the high speed reduction gear had been replaced in the gear box. She was working on re-establishing the electrical connection at the box. She claimed that once the electric was hooked up they would bring in a rig to pull the rods and tubing, and service the downhole pump. Then the well would be ready to go back into production. Carrie said that she would call me when she was ready to turn the well on. She plans to share the gear between the Hartsock 2-A and the Hartsock 3 in a six month rotation. She provided a statement showing that the Hartsock 3 had produced 30.16 barrels of oil in 2016. Carrie had petitioned for an extension on the compliance notice. I informed her that the compliance notice resolve date was 10/19/16, so she did not need an extension at this time.
844534268 2016-4-19 0:00: PW No Violations 2.50
953120596 2016-10-14 0:00 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0844534268 US-OH-129620 2016-06-06 Well shall be plugged

For data sources see[9]

References