X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-031-22876

Well Details

Well ID: 34-031-22876
Loading map...
Country: United States
State: Ohio
County: Coshocton
Municipality: Tiverton Township
Operator Name: W H PATTEN DRILLING CO
Well Pad ID:
Farm/Lease Name: HAYS
License Status: Final Restoration
License Date: 2008-10-27
Spud Date: 1976-10-07
Spud Drilling Contractor:
Final Drill Date: 1976-11-11
Well Total Depth: 3426.00 ft
Configuration: Vertical
Latitude: 40.410000
Longitude: -82.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-09-29 372 PATTEN W H DRLG CO GeoDate 9/29/76
Original Spud 1976-10-07
Completed 1976-11-11
Reached Total Depth 1976-11-11
CO 1992-01-13 372 PATTEN W H DRLG CO GeoDate 1/13/92
Unknown 1992-01-13 Issued Date 1/13/92 Expired Date 1/12/93 Proposed Purpose OG Was Plug Supervised Who Superivsed Plug and Abandon Date
APP 2004-05-14 Proposed Formations:CLINTON, Issued Date:5/14/2004, Expired Date:5/14/2005 6:00:00 AM, Drilling unit acres:120, Proposed Well Type:OG, Proposed Well Class:
APP 2007-06-20 Proposed Formations:CLINTON, Issued Date:6/20/2007, Expired Date:6/19/2008 6:00:00 AM, Drilling unit acres:120, Proposed Well Type:OG, Proposed Well Class:
APP 2008-10-27 Proposed Formations:CLINTON, Issued Date:10/27/2008, Expired Date:10/27/2009 6:00:00 AM, Drilling unit acres:120, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2009-03-16
Construction Permit Expires 2009-10-27
Record Last Modified 2013-03-14

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1400 Bbl 10000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 W H PATTEN DRILLING CO 2205.00 980.00 0
1985 W H PATTEN DRILLING CO 1537.00 455.00 104
1986 W H PATTEN DRILLING CO 517.00 259.00 104
1987 W H PATTEN DRILLING CO 1462.00 222.00 104
1988 W H PATTEN DRILLING CO 1383.00 454.00 104
1989 W H PATTEN DRILLING CO 1097.00 302.00 104
1990 W H PATTEN DRILLING CO 995.00 261.00 104
1991 W H PATTEN DRILLING CO 691.00 187.00 104
1992 W H PATTEN DRILLING CO 301.00 76.00 104
1993 W H PATTEN DRILLING CO 307.00 111.00 104
1994 W H PATTEN DRILLING CO 0.00 75.00 104
1995 W H PATTEN DRILLING CO 0.00 71.00 50
1996 W H PATTEN DRILLING CO 193.00 77.00 365
1997 W H PATTEN DRILLING CO 493.00 149.00 365
1998 W H PATTEN DRILLING CO 588.00 223.00 365
1999 W H PATTEN DRILLING CO 147.00 410.00 365
2000 W H PATTEN DRILLING CO 372.00 151.00 365
2001 W H PATTEN DRILLING CO 175.00 131.00 365
2002 W H PATTEN DRILLING CO 98.00 142.00 365
2003 W H PATTEN DRILLING CO 138.00 25.00 365
2004 W H PATTEN DRILLING CO 3.00 142.00 365
2005 W H PATTEN DRILLING CO 0.00 147.00 365
2006 W H PATTEN DRILLING CO 178.00 80.00 0
2007 W H PATTEN DRILLING CO 162.00 74.00 365
2008 W H PATTEN DRILLING CO 0.00 0.00 365
2009 W H PATTEN DRILLING CO 0.00 0.00 365
2010 W H PATTEN DRILLING CO 0.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 W H PATTEN DRILLING CO Brine 0 0
1985 W H PATTEN DRILLING CO Brine 128 104
1986 W H PATTEN DRILLING CO Brine 42 104
1987 W H PATTEN DRILLING CO Brine 290 104
1988 W H PATTEN DRILLING CO Brine 260 104
1989 W H PATTEN DRILLING CO Brine 400 104
1990 W H PATTEN DRILLING CO Brine 0 104
1991 W H PATTEN DRILLING CO Brine 690 104
1992 W H PATTEN DRILLING CO Brine 60 104
1993 W H PATTEN DRILLING CO Brine 80 104
1994 W H PATTEN DRILLING CO Brine 120 104
1995 W H PATTEN DRILLING CO Brine 0 50
1996 W H PATTEN DRILLING CO Brine 320 365
1997 W H PATTEN DRILLING CO Brine 175 365
1998 W H PATTEN DRILLING CO Brine 150 365
1999 W H PATTEN DRILLING CO Brine 45 365
2000 W H PATTEN DRILLING CO Brine 370 365
2001 W H PATTEN DRILLING CO Brine 110 365
2002 W H PATTEN DRILLING CO Brine 105 365
2003 W H PATTEN DRILLING CO Brine 95 365
2004 W H PATTEN DRILLING CO Brine 45 365
2005 W H PATTEN DRILLING CO Brine 0 365
2006 W H PATTEN DRILLING CO Brine 0
2007 W H PATTEN DRILLING CO Brine 70 365
2008 W H PATTEN DRILLING CO Brine 0 365
2009 W H PATTEN DRILLING CO Brine 0 365
2010 W H PATTEN DRILLING CO Brine 35 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1027782462 2009-6-29 0:00: PB No Violations
-1512295041 2009-6-2 0:00:0 PB No Violations
-1629099425 2004-7-9 0:00:0 PB No Violations
-1801862126 2004-12-9 0:00: PB No Violations
-1999010135 2004-11-9 0:00: PB No Violations
-219083009 2004-11-30 0:00 PB No Violations
-251615868 2008-1-14 0:00: PB No Violations
-280443851 2007-5-22 0:00: PB No Violations
-489434303 2008-12-3 0:00: PB No Violations
-521234915 2009-3-16 0:00: PB No Violations
-534706858 2008-8-28 0:00: PW No Violations
-692778532 2003-11-26 0:00 PW No Violations
-846730784 2010-3-24 0:00: FR No Violations
0027502148 2005-10-03 Plug / Plug Back No Violations Trying to get back in 4.5 casing . Running mandrel at 188 .
0219083009 2004-11-30 Plug / Plug Back No Violations milling 5 casing @ 187 .
0251615868 2008-01-14 Plug / Plug Back No Violations Call from Terry Rice , said he was going to try and complete plugging for company . Ran a down hole camera in well , showed 7 and 4.5 casing rusted off and bent over .
0280443851 2007-05-22 Plug / Plug Back Violations Noted Rig set up on well for plugging . Casing in hole is parted @ 160 , 7 and 4.5 . 8 casing has been ran in hole to try and get inside casing in hole to complete plugging . Rig has been idle for several months . Plugging permit has ran out and needs reissued .
0489434303 2008-12-03 Plug / Plug Back No Violations Drilling inside 4.5 casing @ 563 .
0496731562 2004-06-30 Plug / Plug Back No Violations 4.5 casing rusted into @ 175 , 7 fell down hole when 4.5 was pulled . Trying to get back inside 4.5
0521234915 2009-03-16 Plug / Plug Back No Violations Surface plug set . Plugging completed .
0534706858 2008-08-28 Production Wells No Violations 8 has been pulled since last inspection . Complaint called and said they were waiting for Terry Rice well service to move on to complete plugging of well .
0692778532 2003-11-26 Production Wells Violations Noted Idle well. Motor removed from unit . Vine growing up polish rod . Void this nov , reissued to complete plugging .
0768155790 2008-12-29 Plug / Plug Back No Violations Wait for log truck to shoot 4.5 casing .
0846730784 2010-03-24 Final Restoration No Violations Restoration passed
0994320025 2008-06-19 Production Wells No Violations Plugging permit ran out this date , 2 issued . Rig still on well to plug no change in well status , pipe is parted down hole . Request chiefs order to plug .
1027782462 2009-06-29 Plug / Plug Back No Violations Rig at well site , all other equipment removed , area graded .
1093969334 2004-08-31 Plug / Plug Back No Violations Service rig moved from well site . Waiting for spudder to move on well . No rig at site this inspection .
1097683288 2004-10-13 Plug / Plug Back No Violations Patten moved rig on well to try and complete plugging . Pit lined
1224084995 2008-10-15 Plug / Plug Back No Violations Milling on 7 and 4.5 casing .
1224176970 2008-10-16 Plug / Plug Back No Violations Milling @ 160 .
1224701055 2008-10-22 Plug / Plug Back No Violations Running camera down hole , trying to get back in 4.5 casing to complete plugging .
1228237444 2008-12-02 Plug / Plug Back No Violations Drilling inside of 4.5 casing @ 530 . Milled 7 and 4.5 down to 187 . Ran 187 of 7 in hole to old casing . Milled 4.5 casing down to 210 ran 4.5 casing with 5.5 drive shoe over old 4.5 casing . Drilling clay, shale and some steel from 210 to 530 . Notified company to try and get down to 600 and fish 4.5 casing below Big Injun sand , then shoot holes in 7 casing below Injun Sand then plug to surface with cement .
1228418419 2008-12-04 Plug / Plug Back No Violations Drilling at 570 .
1228844030 2008-12-09 Plug / Plug Back No Violations Drilling at 630 going to drill for 2 more days if they dont get passed Berea , going to shot 4.5 casing and plug with cement .
1230911582 2009-01-02 Plug / Plug Back No Violations Rig shut down this inspection , 4.5 casing has been shoot off around 800 . Fishing for casing .
1236348547 2009-03-06 Plug / Plug Back No Violations 7 & 4.5 casing parted @ 200 recovered 7 & 4.5 down to 200 , Ran 200 of 4.5 casing with 4 to 5 swedge on bottom to go over old casing milled down to 800 . Ran 4.5 casing cutter to 800 . Casing cut @ 800 could not pull any casing . Set cement plug @ 800 back to 500 inside 4.5 casing . Going to try and shoot 4.5 casing @ 175 and plug to surface . There is 7 casing thru Berea formation .
1236611452 2009-03-09 Plug / Plug Back No Violations Set plug from 400 back to 200 .
1237479933 2009-03-19 Plug / Plug Back No Violations Well plugged , order in Compliance .
1266125492 2008-10-24 Plug / Plug Back No Violations 7 casing ran down to old casing in hole , 4.5 casing ran to old casing in hole , milling to get back in 4.5 casing .
1457082124 2008-10-31 Plug / Plug Back No Violations Running 6 mill @ 180 .on 4.5 casing .
1512295041 2009-06-02 Plug / Plug Back No Violations Well plugged rig still on location , 1-100 bl. Storage tank , 7 casing along side of location . Pits closed .
1629099425 2004-07-09 Plug / Plug Back No Violations Fishing for casing .
1723487350 2005-07-19 Plug / Plug Back No Violations Tools in hole . Rig shut down .
1801862126 2004-12-09 Plug / Plug Back No Violations Milling casing @ 200 , 177 of 4.5 casing in hole above 5.5 casing .
1910746979 2004-06-22 Plug / Plug Back No Violations Start bottom plug . Set up all plugs for well .
1999010135 2004-11-09 Plug / Plug Back No Violations Milling on casing .
2011630624 2009-01-06 Plug / Plug Back No Violations Rig shut down , 4.5 casing not recovered from hole this inspection .
2045191421 2005-01-06 Plug / Plug Back No Violations Rig shut down .
2130802817 2007-07-30 Plug / Plug Back No Violations Rig still rigged up on well , 8 casing has been ran in hole to try and get back inside 4.5 casing to complete plugging . There has been no activity at site . Permit reissued to plug , plugging not completed .
27502148 2005-10-3 0:00: PB No Violations
496731562 2004-6-30 0:00: PB No Violations
768155790 2008-12-29 0:00 PB No Violations
994320025 2008-6-19 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0280443851 US-OH-122916 2007-05-22 Failure to proceed with due diligence until completed
0280443851 US-OH-122917 2007-05-22 Plugging without a permit
0692778532 US-OH-127842 2003-11-26 Well shall be plugged

For data sources see[8]

References