X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-031-22325

Well Details

Well ID: 34-031-22325
Loading map...
Country: United States
State: Ohio
County: Tuscarawas
Municipality: Bucks Township
Operator Name: ELEPHANT EXPLORATION INC.
Well Pad ID:
Farm/Lease Name: FRANK RAYMOND J
License Status: Final Restoration
License Date: 2014-04-21
Spud Date: 1974-02-26
Spud Drilling Contractor:
Final Drill Date: 1974-03-05
Well Total Depth: 4515.00 ft
Configuration: Vertical
Latitude: 40.420000
Longitude: -81.710000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1974-02-04 124 MOORE JERRY INC GeoDate 2/4/74
Original Spud 1974-02-26
Completed 1974-03-05
Reached Total Depth 1974-03-05
Change of Owner 1999-10-21 Operator changed from 4884, EASTERN STATES OIL & GAS INC to 5352, ARTEX OIL COMPANY
Change of Owner 2001-08-17 Operator changed from 5352, ARTEX OIL COMPANY to 3059, MFC DRILLING INC
Change of Owner 2012-11-26 Operator changed from 3059, MFC DRILLING INC to 3122, ELEPHANT EXPLORATION INC.
APP 2014-04-21 Proposed Formations:CLINTON, Issued Date:4/21/2014, Expired Date:4/20/2016 12:00:00 PM, Drilling unit acres:75, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-10-13
Construction Permit Expires 2016-04-20
Record Last Modified 2017-02-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4328 4370 3
4328 4370 3
4328 4370 3

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 46000 Gal 45000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 JERRY MOORE INC 498.00 0.00 0
1985 JERRY MOORE INC 146.00 0.00 0
1986 JERRY MOORE INC 71.00 0.00 365
1987 JERRY MOORE INC 21.00 14.00 365
1988 JERRY MOORE INC 0.00 0.00 365
1989 JERRY MOORE INC 0.00 0.00 0
1990 JERRY MOORE INC 0.00 0.00 365
1991 JERRY MOORE INC 0.00 0.00 365
1992 JERRY MOORE INC 25.00 0.00 365
1993 JERRY MOORE INC 0.00 0.00 365
1994 JERRY MOORE INC 0.00 0.00 365
1995 JERRY MOORE INC 15.00 0.00 365
1996 JERRY MOORE INC 0.00 0.00 365
1997 EASTERN STATES OIL & GAS INC 48.00 0.00 365
1998 EASTERN STATES OIL & GAS INC 76.00 0.00 365
1999 EASTERN STATES OIL & GAS INC 153.00 0.00 365
2000 ARTEX OIL COMPANY 0.00 0.00 365
2001 MFC DRILLING INC 133.00 0.00 365
2002 MFC DRILLING INC 364.00 0.00 365
2003 MFC DRILLING INC 196.00 0.00 365
2004 MFC DRILLING INC 166.00 0.00 365
2005 MFC DRILLING INC 134.00 0.00 365
2006 MFC DRILLING INC 104.00 0.00 365
2007 MFC DRILLING INC 101.00 0.00 365
2008 MFC DRILLING INC 104.00 0.00 365
2009 MFC DRILLING INC 114.00 0.00 365
2010 MFC DRILLING INC 114.00 0.00 365
2011 MFC DRILLING INC 89.00 15.00 365
2012 MFC DRILLING INC 58.00 0.00 366
2013 ELEPHANT EXPLORATION INC. 40.00 7.00 365
2014 ELEPHANT EXPLORATION INC. 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 JERRY MOORE INC Brine 0 0
1985 JERRY MOORE INC Brine 0 0
1986 JERRY MOORE INC Brine 15 365
1987 JERRY MOORE INC Brine 0 365
1988 JERRY MOORE INC Brine 0 365
1989 JERRY MOORE INC Brine 0 0
1990 JERRY MOORE INC Brine 0 365
1991 JERRY MOORE INC Brine 0 365
1992 JERRY MOORE INC Brine 0 365
1993 JERRY MOORE INC Brine 0 365
1994 JERRY MOORE INC Brine 0 365
1995 JERRY MOORE INC Brine 0 365
1996 JERRY MOORE INC Brine 0 365
1997 EASTERN STATES OIL & GAS INC Brine 365
1998 EASTERN STATES OIL & GAS INC Brine 365
1999 EASTERN STATES OIL & GAS INC Brine 365
2000 ARTEX OIL COMPANY Brine 0 365
2001 MFC DRILLING INC Brine 0 365
2002 MFC DRILLING INC Brine 0 365
2003 MFC DRILLING INC Brine 0 365
2004 MFC DRILLING INC Brine 0 365
2005 MFC DRILLING INC Brine 0 365
2006 MFC DRILLING INC Brine 0 365
2007 MFC DRILLING INC Brine 0 365
2008 MFC DRILLING INC Brine 0 365
2009 MFC DRILLING INC Brine 0 365
2010 MFC DRILLING INC Brine 0 365
2011 MFC DRILLING INC Brine 0 365
2012 MFC DRILLING INC Brine 0 366
2013 ELEPHANT EXPLORATION INC. Brine 20 365
2014 ELEPHANT EXPLORATION INC. Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-100853840 2014-10-13 0:00 PB No Violations
-1937892661 2014-10-10 0:00 PB No Violations
-792376847 2014-10-14 0:00 PB No Violations
0100853840 2014-10-13 Plug / Plug Back No Violations Timco shot the 2.875 casing off at 3122 and Thompson Well Service pulled it from the well. They went back in with 1.5 tubing to 3115. Formation Cementing pumped cement plugs at the top of the Big Lime, through the Berea, at the base of the surface casing and at the surface. Luq Yaccub reported that they had good circulation for the plugs and the cement was staying up.
0179812700 2015-07-14 Final Restoration No Violations On the day of my inspection I found that the site had been graded and re-seeded. It was growing with grasses and broadleaf vegetation. Drainage had been installed to divert excess water off of the location. I found no standing water and no signs of erosion. This site passes final restoration.
0520867331 2014-10-08 Plug / Plug Back No Violations On the day of my inspection Josh Thompson moved in and rigged up to plug the well. Appalachian Well Surveys attempted to shoot the 1.5 tubing off inside of 2.875 casing. They made two attempts and both were unsuccessful.
0792376847 2014-10-14 Plug / Plug Back No Violations On the day of my inspection I found that the well was still open. There was solid cement approximately 2 feet down. The hole was full of water and I observed some bubbling from inside of the 8.625 casing. I had Mark Fluharty excavate around the casing and bail the water out. The bubbling was slight and I did not detect the odor of natural gas. I requested that they leave the well open for a couple days to monitor it.
1260981997 2009-12-16 Production Wells No Violations Gas well capable of production .
1413385202 2014-10-15 Plug / Plug Back No Violations On the day of my inspection I found that the bubbling had stopped. I authorized Mark Fluharty to cut the casing off and cap the well.
1431350952 2015-05-11 Final Restoration No Violations On the day of my inspection I found that the site had been seeded and it was approximately 70% covered in rye grass. The production equipment had been removed. There were no materials or debris at the site. The site still needed a final grade and a drainage ditch to divert rain water off of the site. I did receive a landowner waiver to leave the lease road. I contacted Luq to request that he address the issues with the restoration. He claimed that he would get someone out to finish it.
179812700 2015-7-14 0:00: FR No Violations
1937892661 2014-10-10 Plug / Plug Back No Violations Josh Thompson tried to pull on the 1.5 tubing again and found that it was free. Cemenco pumped a 500 cement isolation plug through 1.5 tubing, inside of 2.875 casing. Thompson Well Service reported that they suspected a hole in the 2.875 casing, because there was fluid circulating out of the 8.625 casing when they were pumping the plug. I requested that they pull the 2.875 casing and go back in with 1.5 tubing to finish the plug job.
520867331 2014-10-8 0:00: PB No Violations

For data sources see[9]

References