X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-019-21850

Well Details

Well ID: 34-019-21850
Loading map...
Country: United States
State: Ohio
County: Carroll
Municipality: East Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: BRYAN UNIT
License Status: Final Restoration
License Date: 2005-06-27
Spud Date: 1997-03-13
Spud Drilling Contractor: IPSCO
Final Drill Date: 1997-03-30
Well Total Depth: 9458.00 ft
Configuration: Vertical
Latitude: 40.670000
Longitude: -80.940000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1996-11-25 5512 NEWSTAR ENERGY USA INC GeoDate 11/25/96
Oil and Gas 1996-11-25 Issued Date 11/25/96 Expired Date 11/25/97 Acres 0160000 Tool Type RTAF Proposed Formation DOH thru CPRG Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1997-03-13 RBDMS Rec
Completed 1997-03-30 RBDMS Rec
Reached Total Depth 1997-03-30 RBDMS Rec
End of Confidential Data 1998-03-30 RBDMS Rec
Change of Owner 2000-04-17 Operator changed from 5512, NEWSTAR ENERGY USA INC to 1634, NORTHWOOD ENERGY CORP
APP 2004-06-02 Proposed Formations:ROSE RUN, Issued Date:6/2/2004, Expired Date:6/2/2005 6:00:00 AM, Drilling unit acres:160, Proposed Well Type:OG, Proposed Well Class:
Plugged Back 2005-05-26 RBDMS Rec
APP 2005-06-27 Proposed Formations:BEREA, Issued Date:6/27/2005, Expired Date:6/27/2006 6:00:00 AM, Drilling unit acres:160, Proposed Well Type:OG, Proposed Well Class:EOUT
Plugged/Abandoned 2005-06-27 RBDMS Rec
Completion Report Received 2006-01-06 RBDMS Rec
Construction Permit Expires 2006-06-27 RBDMS Rec
Record Last Modified 2016-01-23 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-03-06 1032 1052 42
8931 8953 35
9077 9108 35
1997-10-16 8931 8953 35
1032 1052 42
1032 1052 42
1997-10-16 9077 9108 35

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 0 PERF'D UNDER ACID…1 MCF GAS AFTER
ACID 15 2000 Gal 0
ACID 15 1100 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1997 NEWSTAR ENERGY USA INC 6482.00 0.00 92
2000 NORTHWOOD ENERGY CORP 4973.00 0.00 365
2001 NORTHWOOD ENERGY CORP 4763.00 0.00 365
2002 NORTHWOOD ENERGY CORP 158.00 0.00 365
2003 NORTHWOOD ENERGY CORP 350.00 0.00 365
2004 NORTHWOOD ENERGY CORP 44.00 0.00 365
2005 NORTHWOOD ENERGY CORP 0.00 0.00 0
2010 NORTHWOOD ENERGY CORP 0.00 0.00 0
2011 NORTHWOOD ENERGY CORP 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1997 NEWSTAR ENERGY USA INC Brine 5200 92
2000 NORTHWOOD ENERGY CORP Brine 7719 365
2001 NORTHWOOD ENERGY CORP Brine 10801 365
2002 NORTHWOOD ENERGY CORP Brine 880 365
2003 NORTHWOOD ENERGY CORP Brine 10801 365
2004 NORTHWOOD ENERGY CORP Brine 0 365
2005 NORTHWOOD ENERGY CORP Brine 280 0
2010 NORTHWOOD ENERGY CORP Brine 0 0
2011 NORTHWOOD ENERGY CORP Brine 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1117437473 2005-4-28 0:00: PB No Violations 2.50
-1313890817 2005-3-28 0:00: PB No Violations 1.00
-1403872781 2005-5-16 0:00: PB No Violations 2.00
-1425471104 2005-4-19 0:00: PB No Violations 1.50
-1598362060 2005-4-27 0:00: PB No Violations 1.50
-1623209466 2010-11-1 0:00: PW No Violations 1.50
-1991929595 2005-5-18 0:00: PB No Violations 2.50
0709071448 2005-04-21 Plug / Plug Back No Violations Inspection revealed that they are still trying to pull the 8 5/8 casing ; nobody on location at this time . No violations at this time .
1112615752 2005-04-01 Plug / Plug Back No Violations On site to witness the bottom hole plug ; Roserun / Beekmantown formation . Plug from 9108 to 8731 with 30 sks. Class A cement , Petroset Cementing . Should be ready to finish plugging the well at the end of next week or the beginning of the following week .
1115288488 2005-05-04 Plug / Plug Back No Violations They are still tryingto pull the 8 5/8 casing . The have about 3000 of 8 5/8 casing out of the well so far . They are fishing for the other 1200 with a casing spear and tubing . Earl Barnes advised that it would probably be sometime next week before they would be finished fishing out the casing and running tubing back into the well to finish plugging the well.
1117437473 2005-04-28 Plug / Plug Back No Violations Inspection revealed that they are pulling the 8 5/8 casing . They should have the approximately 3000 of casing out of the hole by the end of this week or early next week . Ill check the site again next week to check on the status of the plug job . They need to go back in after they get the first 3000 of casing and fish out another 1200 of casing that is stuck in the wellbore.
1288630841 2010-09-14 Production Wells Violations Noted On site with Earl Bryan (landowner). He advised that the well has been idle for quite some time. The inspection revealed that the well head consists of a gate valve on top of the tubing. There is a gas meter at the well head but it is not hooked up. There is no flowline hooked to the wellhead at this time. Inspection of the tank battery revealed a one hundred barrel oil storage tank and no identification sign posted at either the well head or tank battery. I advised Mr. Bryan that the Division has to give the operator the option of either plugging or producing the well. I also advised him about the procedure the Division has to follow to obtain compliance. I contacted Northwood Energy and left a message (verbal compliance notice) that they needed to plug or produce the well by October 20th, 2010. RBDMS revealed that the last reported production was in 2005.
1313890817 2005-03-28 Plug / Plug Back No Violations
1403872781 2005-05-16 Plug / Plug Back No Violations Inspection revealed that the service rig is fishing for parted tubing . On last Friday while trying to fish for the 8 5/8 casing the tubing parted approximately 18 joints down . The service rig went in with fishing tools earlier today , but couldnt get ahold of the tubing . They tripped out the tools and ran back in with other fishing tools in an attempt to get ahold of the tubing . They have decided to try to get ahold of the tubing and try to release the 8 5/8 casing spear and bring it out of the hole . After getting the spear out , they are going back into the hole with tubing to finish plugging the well . The operator has decided to leave the rest of the 8 5/8 casing in the well .
1425471104 2005-04-19 Plug / Plug Back No Violations Inspection revealed that the service rig is still trying to pull the 8 5/8 casing . They are having trouble pulling the 8 5/8 casing . No violations at this time .
1451576871 2015-12-28 Final Restoration No Violations I was on site to conduct a final restoration inspection of this site. The wellhead and production equipment had been removed. The wellsite was stable and vegetated. The lease access was still intact and being utilized for farm access to the adjacent fields. The is a report in the state database that shows the well to have been plugged in 2011. Final restoration passed.
1598362060 2005-04-27 Plug / Plug Back No Violations Inspection revealed that the service rig is still pulling the 8 5/8 casing . Nobody from the rig crew or operator on location this morning ; rig shut down .
1623209466 2010-11-01 Production Wells Violations Noted Inspection revealed that the well is idle. The well head consists of a gate valve on top of the tubbing. There is no flowline attached to the well head at this time. There is a meter at the well head that is not hooked up either. The tank battery consists of a one hundred barrel oil storage tank. There is no identification posted at either the well head or the tank battery at this time. I spoke with Bill ( Northwood Energy 614-457-1024) and advised him that the well is idle and that I was going to send Northwood Energy a Compliance Notice today to either plug or produce the well. He advised that he spoke with Chip Smith (ChipCo) last week and that he is moving his service rig onto the Toalston well and then he is moving onto the Bryan well after that. He advised, that Chip Smith advised him that they had to finish working on the rig and then he would move onto these wells. They are going to conduct a mini-frac on this well and see if that will stimulate the well. He advised that if this mini-frac is not successful, then they will probably plug the well at that time. I am giving a remedial action date of December 6th,2010 for the Compliance Notice.
1991929595 2005-05-18 Plug / Plug Back No Violations Inspection revealed that the tubing is still in the well . It appears that they are still fishing for the 8 5/8 casing . There is nobody on location at this time (7:00am) . I will return to the location later today to see if the rig crew is on site and to see what progress the rig has made in fishing out the casing . On site later this afternoon (12:30pm) and no rig crew on site at this time . Nobody has been on site today . I will call Earl Barnes ( Northwood Energy) and check on the progress of the fishing job .
709071448 2005-4-21 0:00: PB No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1288630841 US-OH-108145 2010-11-01 Well shall be plugged
1623209466 US-OH-115955 2010-11-01 Well shall be plugged

For data sources see[9]

References