If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-019-20436 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.61,"lon":-81.24,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Carroll | |
Municipality: Rose Township | |
Operator Name: WILLIAM S MILLER INC | |
Well Pad ID: | |
Farm/Lease Name: GROSENBAUGH | |
License Status: Plugged and Abandoned | |
License Date: 2018-05-30 | |
Spud Date: 1969-10-21 | |
Spud Drilling Contractor: | |
Final Drill Date: 1970-05-12 | |
Well Total Depth: 5510.00 ft | |
Configuration: Vertical | |
Latitude: 40.610000 | |
Longitude: -81.240000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1969-05-20 | 311 STOCKER & SITLER INC GeoDate 5/20/69 |
Original Spud | 1969-10-21 | UPDATE COORDAINTES PER DOGRNM SURVEYOR |
Completed | 1970-05-12 | UPDATE COORDAINTES PER DOGRNM SURVEYOR |
Reached Total Depth | 1970-05-12 | UPDATE COORDAINTES PER DOGRNM SURVEYOR |
Change of Owner | 1999-07-20 | Operator changed from 311, STOCKER & SITLER INC to 5785, M-J OIL COMPANY INC. |
Change of Owner | 2001-03-13 | Operator changed from 5785, M-J OIL COMPANY INC. to 5894, G & O RESOURCES LTD |
Change of Owner | 2012-04-10 | Operator changed from 5894, G & O RESOURCES LTD to 2512, MILLER WILLIAM S INC |
APP | 2018-05-30 | Proposed Formations:CLINTON, Issued Date:5/30/2018, Expired Date:5/29/2020 12:00:00 PM, Drilling unit acres:160.98, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-07-07 | UPDATE COORDAINTES PER DOGRNM SURVEYOR |
Record Last Modified | 2019-05-10 | UPDATE COORDAINTES PER DOGRNM SURVEYOR |
Construction Permit Expires | 2020-05-29 | UPDATE COORDAINTES PER DOGRNM SURVEYOR |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5312 | 0 | |
2006-09-11 | 5348 | 5357 | 0 |
5312 | 0 | ||
5312 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 10000 Bbl | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | STOCKER & SITLER INC | 321.00 | 373.00 | 365 |
1985 | STOCKER & SITLER INC | 1221.00 | 481.00 | 0 |
1986 | STOCKER & SITLER INC | 840.00 | 278.00 | 365 |
1987 | STOCKER & SITLER INC | 646.00 | 305.00 | 365 |
1988 | STOCKER & SITLER INC | 559.00 | 323.00 | 0 |
1989 | STOCKER & SITLER INC | 592.00 | 434.00 | 365 |
1990 | STOCKER & SITLER INC | 1136.00 | 734.00 | 365 |
1991 | STOCKER & SITLER INC | 596.00 | 367.00 | 365 |
1992 | STOCKER & SITLER INC | 528.00 | 263.00 | 365 |
1993 | STOCKER & SITLER INC | 576.00 | 252.00 | 365 |
1994 | STOCKER & SITLER INC | 839.00 | 279.00 | 0 |
1995 | STOCKER & SITLER INC | 13.00 | 229.00 | 0 |
1996 | STOCKER & SITLER INC | 0.00 | 0.00 | 0 |
1997 | STOCKER & SITLER INC | 0.00 | 0.00 | 365 |
1998 | STOCKER & SITLER INC | 179.00 | 159.00 | 365 |
1999 | M-J OIL COMPANY INC. | 62.00 | 13.00 | 100 |
2000 | M-J OIL COMPANY INC. | 0.00 | 67.00 | 365 |
2001 | M-J OIL COMPANY INC. | 0.00 | 43.00 | 49 |
2002 | G & O RESOURCES LTD | 0.00 | 47.00 | 365 |
2003 | G & O RESOURCES LTD | 0.00 | 53.00 | 365 |
2004 | G & O RESOURCES LTD | 0.00 | 34.00 | 365 |
2005 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2006 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2007 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2008 | G & O RESOURCES LTD | 0.00 | 18.00 | 366 |
2009 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2010 | G & O RESOURCES LTD | 0.00 | 11.00 | 365 |
2012 | WILLIAM S MILLER INC | 0.00 | 0.00 | 0 |
2013 | WILLIAM S MILLER INC | 0.00 | 0.00 | 0 |
2014 | WILLIAM S MILLER INC | 0.00 | 0.00 | 0 |
2015 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2016 | WILLIAM S MILLER INC | 0.00 | 0.00 | 0 |
2017 | WILLIAM S MILLER INC | 0.00 | 0.00 | 0 |
2018 | WILLIAM S MILLER INC | 0.00 | 0.00 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1135914317 | 2018-7-8 0:00:0 | PB | No Violations | 0.40 |
-1275162986 | 2013-8-22 0:00: | AM | No Violations | |
-1353779248 | 2018-5-21 0:00: | PW | No Violations | 0.70 |
-1458764444 | 2015-10-15 0:00 | PW | No Violations | |
-184620718 | 2018-5-29 0:00: | PW | No Violations | 3.00 |
-1938592777 | 2018-10-30 0:00 | FR | No Violations | 0.50 |
-325544109 | 2019-10-28 0:00 | FR | No Violations | 1.00 |
-803697649 | 2015-5-20 0:00: | PW | No Violations | |
0184620718 | 2018-05-29 | Production Wells | No Violations | I was on site to conduct a compliance notice follow-up from a release which was discovered on 05/08/2018. The diked area around the well head contained water with oil product, and the water appeared to have breached the contained area. Sheen was present in the excavated area around the well. I met with the George Miller of William S Miller Inc. on site who agreed to plug the well during June of 2018. I stated that any product needs to be removed and recommended in the interim of plugging the well that a lined pit be installed near the well to contain any further contamination leaching from around the well, and the pit be regularly monitored for water levels. The compliance notice will be closed once all visible contamination has been removed. |
0268041942 | 2017-03-08 | Production Wells | No Violations | I spoke to David Miller of William S. Miller Inc. on 03/08/2017 regarding the plugging status of the well. He informed me that this well is on the list to be plugged and is hoping to start plugging operations in 2017. |
0317877821 | 2018-07-06 | Plug / Plug Back | No Violations
-down operations for the night. | |
0348137348 | 2018-05-15 | Production Wells | No Violations | I conducted a compliance notice follow-up on the well for pollution and contamination. The area around the well head, which was excavated and diked, contained water and visible oil product. Oil soak pads were in place. The well is located a low section of a farm field and intersects a natural drainage path. A shallow ditch west of the well was put in place to catch any drainage, and a boom was deployed. The boom appeared clean at the time of inspection. Cleanup was on going at the time of inspection. A stockpile of excavated and contaminated soil was located north of the well and on a liner proper disposal. |
0803697649 | 2015-05-20 | Production Wells | Violations Noted | Inspection showed the well is equipped with an electrically powered pump jack. The tubing valve is open. There is a line with a closed valve that is partially buried that may be the flow line or an old domestic line. The well head is overgrown with vegetation. One, 100 bbl. White rusty steel tank and 1, 50 bbl. Green steel tank are near the well. There is not a meter or separator at the tanks. The identification at the well shows G & O as the owner. The Division of Oil and Gas records show William Miller is the owner. The tank battery is overgrown with vegetation. There has been 0 production reported from 2012 through 2014. 0 barrels of oil were produced between 2005 and 2007. 18 barrels of oil were produced in 2008.0 barrels in 2009 and 11 barrels of oil in 2010. This well used to produce into the same tank battery as P. 435, 437 and 438. All four wells reported the same production. G & O and William Miller have been contacted to determine ownership and plans for this well. |
0860511096 | 2018-12-11 | Final Restoration | No Violations | I was on site for a final restoration inspection. The equipment and tank has been removed, but a pile of scrap was still present on site. It also appeared that the area still needed more grading and seeding. I will contact the operator. I witnessed plugging operations for this well which were finished on 07/07/2018. Plugging of the well has been fulfilled and the compliance notice issued to plug the well can be closed at this time. |
1105735354 | 2018-07-07 | Plug / Plug Back | No Violations
<- | |
1135914317 | 2018-07-08 | Plug / Plug Back | No Violations | I was on site to verify the cement top after plugging operations commenced on 07/07/2018. The service rig was off location and the temporary pit which was used during plugging operations had been emptied. I located the cement top to be at surface. |
1275162986 | 2013-08-22 | Administrative Inspection | No Violations | I was on inspection with Helen Halter. My inspection found the well to be shut in. Last reported production was in 2010, the operator reported 11 barrels of oil produced. There was no identification posted at the well or the tank battery. The well needs put back into production or plugged. Identification needs posted at the well site. Please contact Brett Farnsworth and advise him of your schedule for putting the well back into production or plugging. Bretts cell phone number is (330) 284-1409. |
1353779248 | 2018-05-21 | Production Wells | No Violations | I conducted a compliance notice follow-up inspection of the well for a release which was discovered on 05/08/2018. The water around the well head was near the brim of the dike and contaminated oil pads as well as free product was visible on the water. I contacted David Miller of William S Miller Inc. and requested the contaminated water be emptied to prevent overflowing. He stated a pumper was in route to change the contaminated oil soak pads. We also discussed the plugging schedule of the well which he stated should take place in June of 2018. |
1357819755 | 2018-05-31 | Production Wells | No Violations | I was on site for a compliance notice follow-up for the well causing pollution and contamination. A lined pit had been installed south of the well head to contain any further contamination leaching from the soil, and will remain in place until plugging operations commence. The pit was dry at the time of inspection. The contamination in the area west of the well head, which was visible on 05/29/2018, was no longer present, as well as most of any product located in the diked area around the well. The compliance notice will remain open at this time until further monitoring to ensure that all pollution and contamination has been removed. The precautionary containment pit is planned to stay in place until plugging operations are finished. |
1446047373 | 2015-10-26 | Production Wells | No Violations | Inspection showed the well is not in production and there is not a domestic connection. Weeds have been cut down around the tank battery and pump jack. A new Identification sign with William Miller, Inc. as owner has been posted. Bill Miller Jr. has been in discussion with Supervisor Hill and would like to put together a timeframe for plugging or producing the wells they own in this area that are not in production. The current compliance date for plugging this well is 12/01/2015. |
1458764444 | 2015-10-15 | Production Wells | No Violations | I conducted a status check of this well with DOGRM Regional Supervisor Tom Hill. The well is equipped with an electrically-driven pumpjack. The production valves were in the open position, but the polish rod did not appear to be lubricated, and the joints of the pumpjack showed signs of corrosion. The tank battery consists of one 100 bbl production tank and one 50 bbl brine tank. Proper identification had been posted at the well. A review of records in the State database shows that the last reported production was 11 bbls in 2006. The well is not equipped to produce at this time. The operator shall submit a plugging schedule to inspector Ashley Raff for approval within 30 days of 11/06/2015 at: Ohio Department of Natural Resources, Division of Oil and Gas, 3575 Forest Lake Drive Suite 150, Uniontown, Ohio 44685, per OAC 1501:9-11-05(B). The well owner/operator will be notified if the plugging schedule is approved or denied. As per the Compliance Notice on 06/01/2015, the well is to be plugged by 12/01/2015. |
1480582169 | 2018-12-19 | Production Wells | No Violations | I spoke to David Miller of William S. Miller on 12/13/2018 and informed him that I could not pass final restoration during my last inspection on 12/11/2018 due to debris from the well present on site and because the area did not appear graded and seeded. He stated that he was unaware that any debris was on site. As of my inspection on 12/19/2018, the stockpiled debris was still on site and further grading needed to be done. In response to the compliance notice issued on 05/18/2018 for the well causing pollution and contamination, all contamination appeared to have been remediated so the compliance notice can be closed. |
1527775855 | 2018-05-08 | Production Wells | Violations Noted | I conducted a compliance notice follow-up which was issued to plug the well on 01/06/2015. At the time of inspection, a leak appearing to come from around the well head was active, and contamination and mobile oil was present measuring approximately 50 x 10. The contamination travelled west in the field for approximately 150 west where visible contamination and scald diminished. I contact Dave Miller of William S Miller Inc, who met me on site. Visible product was excavated and area of well head exposed where it was discovered that the leak appeared be from a failed section of flowline near the well. An area around the well head was dug out and diked to holed water and further contamination leached from the soil. Clean up is ongoing. The operator agreed to apply for a plugging permit and plug the well as soon as possible. |
1545332908 | 2018-07-05 | Plug / Plug Back | No Violations
-1000 lbs. The plug was set from 5492-4980 with 50 sacks of Class A cement with cottonseed hulls. I weighed the cement at 15.4 ppg. The pH of the mix water was 7.0 and chlorides were <-in overnight. | |
1938592777 | 2018-10-30 | Final Restoration | No Violations | I was on site for final restoration. The production tank had been removed from site, but debris from the well was still present on location and vegetation had not yet been established. Final restoration cannot be passed at this time. |
2095219012 | 2015-10-15 | Production Wells | Violations Noted | I conducted a status check of this well with DOGRM Regional Supervisor Tom Hill. The well is equipped with an electrically-driven pumpjack. The production valves were in the open position. The polish rod did not appear to be lubricated, and the joints of the pumpjack showed signs of corrosion. Proper Identification was posted at the well. The tank battery consists of one 100 bbl production tank and one 50 bbl brine tank. A review of records in the State database shows that the last reported production was 11 bbls in 2006, and has not produced the regulatory-required minimum production since 2008, and has only once since 2004. No production has been reported for over two consecutive reporting periods. The well is not equipped for production at this time. The operator shall submit a plugging plan to inspector Ashley Raff for approval within 30 days at: Ohio Department of Natural Resources, Division of Oil and Gas, 3575 Forest Lake Drive Suite 150, Uniontown, Ohio 44685. |
268041942 | 2017-3-8 0:00:0 | PW | No Violations | |
317877821 | 2018-7-6 0:00:0 | PB | No Violations | 2.00 |
348137348 | 2018-5-15 0:00: | PW | No Violations | 1.00 |
860511096 | 2018-12-11 0:00 | FR | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0803697649 | US-OH-129125 | 2015-08-03 | Failure to legibly identify well | |
0803697649 | US-OH-129126 | 2015-08-03 | Well shall be plugged | |
1527775855 | US-OH-114629 | 2019-01-15 | 9-1-07 | Well operation causing pollution and contamination |
2095219012 | US-OH-121394 | 2019-01-15 | NONE | Well shall be plugged |
For data sources see[9]