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34-019-20400

Well Details

Well ID: 34-019-20400
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Country: United States
State: Ohio
County: Carroll
Municipality: Rose Township
Operator Name: ALLIANCE PETROLEUM CORPORATION
Well Pad ID:
Farm/Lease Name: COOPER VL
License Status: Final Restoration
License Date: 2004-10-25
Spud Date: 1968-11-03
Spud Drilling Contractor:
Final Drill Date: 1968-11-11
Well Total Depth: 5414.00 ft
Configuration: Vertical
Latitude: 40.600000
Longitude: -81.270000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1968-10-18 1383 OHIO L & M CO INC GeoDate 10/18/68
Original Spud 1968-10-30
Completed 1968-11-11
Reached Total Depth 1968-11-11
APP 2004-10-25 Proposed Formations:CLINTON, Issued Date:10/25/2004, Expired Date:10/25/2005 6:00:00 AM, Drilling unit acres:39.02, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2005-06-06
Construction Permit Expires 2005-10-25
Change of Owner 2006-07-14 Operator changed from 1383, OHIO L & M CO INC to 6288, ALLIANCE PETROLEUM CORPORATION
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5271 5368 0
5271 5368 0
5271 5368 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2200 Bbl 43000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 OHIO L & M CO INC 1.00 335.00 0
1985 L & M PETROLEUM CO 0.00 303.00 0
1986 L & M PETROLEUM CO 0.00 0.00 365
1987 L & M PETROLEUM CO 0.00 526.00 365
1988 OHIO L & M CO INC 17.00 428.00 365
1989 OHIO L & M CO INC 0.00 294.00 365
1990 OHIO L & M CO INC 0.00 164.00 365
1991 OHIO L & M CO INC 0.00 400.00 365
1992 OHIO L & M CO INC 0.00 301.00 365
1993 OHIO L & M CO INC 0.00 245.00 365
1994 OHIO L & M CO INC 0.00 222.00 365
1995 OHIO L & M CO INC 0.00 181.00 365
1996 OHIO L & M CO INC 0.00 220.00 365
1997 OHIO L & M CO INC 0.00 167.00 365
1998 OHIO L & M CO INC 0.00 233.00 365
1999 OHIO L & M CO INC 0.00 117.00 365
2000 OHIO L & M CO INC 0.00 100.00 365
2001 OHIO L & M CO INC 0.00 111.00 365
2002 OHIO L & M CO INC 0.00 219.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 OHIO L & M CO INC Brine 0 0
1985 L & M PETROLEUM CO Brine 0 0
1986 L & M PETROLEUM CO Brine 0 365
1987 L & M PETROLEUM CO Brine 236 365
1988 OHIO L & M CO INC Brine 0 365
1989 OHIO L & M CO INC Brine 0 365
1990 OHIO L & M CO INC Brine 0 365
1991 OHIO L & M CO INC Brine 0 365
1992 OHIO L & M CO INC Brine 0 365
1993 OHIO L & M CO INC Brine 0 365
1994 OHIO L & M CO INC Brine 0 365
1995 OHIO L & M CO INC Brine 0 365
1996 OHIO L & M CO INC Brine 0 365
1997 OHIO L & M CO INC Brine 0 365
1998 OHIO L & M CO INC Brine 0 365
1999 OHIO L & M CO INC Brine 0 365
2000 OHIO L & M CO INC Brine 0 365
2001 OHIO L & M CO INC Brine 0 365
2002 OHIO L & M CO INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-602713324 2007-5-31 0:00: FR No Violations 0.50
0063369205 2005-06-07 Plug / Plug Back No Violations Inspection revealed that the surface plug dropped approximately 8 from ground level . No violations at this time . Talked with the rig operator ( Terry Jones ) and he advised that they were taking the rig to Cambridge for new wireline and then they would be going to Stark County on Rt. 44 ( Bechtol Lease ) to plug a well .
0602713324 2007-05-31 Final Restoration No Violations Inspect the wellsite for the Huff Run Water Shed Project . Inspection revealed that the well has been plugged and reclaimed . No violations at this time .
1118151917 2005-06-07 Plug / Plug Back No Violations Inspection revealed that the plugging rig is moving off location . The cement was down aprroximately 8 from ground level. Rig operator , Terry Jones , advised that they are going to move to the Bechtol well in Stark County later today or early tomorrow morning . Inspection of the plugging pit revealed that the liner is intact and fluid levels are acceptable . No violations at this time .
63369205 2005-6-7 0:00:0 PB No Violations 1.50

For data sources see[9]

References