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34-013-21254

Well Details

Well ID: 34-013-21254
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Country: United States
State: Ohio
County: Belmont
Municipality: Washington Township
Operator Name: GULFPORT APPALACHIA LLC
Well Pad ID: US-OH-001520
Farm/Lease Name: HORSESHOE 210011
License Status: Producing
License Date: 2017-12-11
Spud Date: 2017-12-18
Spud Drilling Contractor: PIONEER DRILLING
Final Drill Date: 2018-05-02
Well Total Depth: 21448.00 ft
Configuration: Horizontal
Latitude: 39.900000
Longitude: -80.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2017-05-25 Proposed Formations:TRENTON, Issued Date:5/25/2017, Expired Date:5/25/2019 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT
APP 2017-12-11 Proposed Formations:UTICA/POINT PLEASANT, Issued Date:12/11/2017, Expired Date:12/11/2019 12:00:00 PM, Drilling unit acres:678.867, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2018-05-02
Record Last Modified 2018-08-27
Correction to Well 2018-08-31 TAKE TARGET AS-DRILLED
Construction Permit Expires 2019-12-11

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
21174 10995 0
21174 10995 0

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-556234077 2018-1-29 0:00: DD No Violations 1.00
0556234077 2018-01-29 Drill / Deepen / Reopen No Violations On the day of my inspection Pioneer Rig 71 was drilling in the 12.25-inch diameter open hole section of the well bore at a depth of 9825 feet. Once the open hole section of the well bore is completed, the 9.625-inch diameter casing string will be ran and cemented.
0910867743 2019-04-11 Completion Testing No Violations Status check inspection found Stingray pressure pumping service along with Nine Energy wireline on location completing wells # 4 #5&#6 on location. The #1 #2 and # 3 wells will have the stimulation process started on 04/15/2019. The said well is equipped with a lower A and upper B section with 2 primary master valves present. The 2 primary master valves present are owned by B&B. All annular pressures are being recorded daily.
1513624843 2017-12-18 Casing String Witnessed No Violations Location address: 55950 Goddard Rd, Beallsville. On the day of my inspection I witnessed Lightning had augured a 36 inch diameter hole to 110 feet. 110 feet of 26 inch diameter conductor casing was run. Stingray was onsite with 430 sacks of class A cement. Additives include 2% CaCl and .25 lb./sack cello-flake. Cement weighed with mudscale at 15.6 ppg and yield of 1.21. 30 percent excess ran. 15 barrels of gel ahead of cement. Cement was displaced with 58 barrels of fresh water. 20 barrels of cement returned to surface.
1564508368 2019-7-30 0:00: PL No Violations 0.40
1808307772 2020-2-25 0:00: PW No Violations 0.20
233250221 2020-4-29 0:00: PW No Violations 0.20
660529447 2019-6-13 0:00: CT No Violations 0.20
906841152 2020-10-20 0:00 PW No Violations
910867743 2019-4-11 0:00: CT No Violations 0.20

For data sources see[4]

References