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Well ID: 34-013-20698 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Somerset Township | |
Operator Name: GULFPORT ENERGY CORPORATION | |
Well Pad ID: US-OH-000532 | |
Farm/Lease Name: STUTZMAN | |
License Status: Lost Hole | |
License Date: 2013-07-26 | |
Spud Date: 2013-07-12 | |
Spud Drilling Contractor: UNION DRLG | |
Final Drill Date: 2013-08-10 | |
Well Total Depth: 17749.00 ft | |
Configuration: Horizontal | |
Latitude: 39.890000 | |
Longitude: -81.170000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2013-06-12 | Proposed Formations:TRENTON, Issued Date:6/12/2013, Expired Date:6/12/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2013-07-26 | Proposed Formations:POINT PLEASANT, Issued Date:7/26/2013, Expired Date:7/26/2015 12:00:00 PM, Drilling unit acres:1247.796, Proposed Well Type:OG, Proposed Well Class:EDPW |
Reached Total Depth | 2013-08-10 | |
Correction to Well | 2013-12-06 | CHANGE IN TARGET AND TAKE-POINT INFORMATION (FOOTAGE AND COORDINATES) FROM AS DRILLED SURVEY PLAT. |
Construction Permit Expires | 2015-07-26 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1192000507 | 2013-7-24 0:00: | DD | No Violations | 2.00 |
-1745349260 | 2013-8-21 0:00: | DD | No Violations | 2.00 |
-1813726923 | 2013-10-8 0:00: | AM | No Violations | 0.50 |
-1964655865 | 2018-9-19 0:00: | PW | No Violations | 0.50 |
-206916894 | 2013-7-29 0:00: | DD | No Violations | 1.00 |
-2090729341 | 2013-10-7 0:00: | PB | No Violations | 0.50 |
-248166570 | 2013-8-14 0:00: | DD | No Violations | 2.00 |
-336277985 | 2013-8-19 0:00: | DD | No Violations | 2.00 |
-760996896 | 2013-8-2 0:00:0 | DD | No Violations | 2.00 |
-989982387 | 2016-3-14 0:00: | PL | No Violations | 1.00 |
0003702203 | 2013-07-30 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder # 64 was drilling ahead to kick off point. No violations noted. |
0138725729 | 2013-07-12 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Express Energy was drilling the 32 conductor hole and was almost to total depth. No violations noted. |
0206916894 | 2013-07-29 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder #64 would be continuing to drill ahead to kick off point soon. No violations noted. |
0248166570 | 2013-08-14 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder 64 was working on top drive. No violations noted. |
0305600640 | 2013-07-15 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder 64 was rigging up on location. No violations noted. |
0336277985 | 2013-08-19 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder 64 was attempting to begin running their 5.5 casing. No violations noted. |
0596325048 | 2013-10-09 | Plug / Plug Back | No Violations | On the day of my inspection I witnessed plugs being set in this well. See ticket for details. No violations noted. |
0760996896 | 2013-08-02 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder #64 was drilling ahead to kick off point. No violations noted. |
0989982387 | 2016-03-14 | Preliminary Restoration | No Violations | On this day I visited this pad to perform a preliminary restoration inspection. The pad appeared to be in satisfactory condition. Vegetation has been established and the erosion and sediment controls appear to be functioning properly. Preliminary restoration for this site has passed. |
1192000507 | 2013-07-24 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder #64 was drilling ahead to set 10.34 casing string. No violations noted. |
1354522993 | 2013-07-22 | Casing String Witnessed | No Violations | On the day of my inspection Stingray was on location to cement the 16 casing. See cement ticket for details. No violations noted. |
1381205450 | 2013-10-07 | Plug / Plug Back | No Violations | On the day of my inspection Stingray Cementing was setting a bottom hole plug. No violations noted. |
1382764275 | 2013-10-08 | Plug / Plug Back | No Violations | On the day of my inspection Gulfport had decided to run a cement retainer in the hole against recommendation. They attempted to pump cement but was unable. Retainer will be drilled out and cement plugs will be placed through open ended drill string. No violations noted. |
138725729 | 2013-7-12 0:00: | DD | No Violations | 1.00 |
1404194433 | 2013-07-16 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder 64 was rigging up on location. No violations noted. |
1695103577 | 2013-10-10 | Plug / Plug Back | No Violations | On the day of my inspection the final plugs were being set. See ticket for details. No violations noted. |
1745349260 | 2013-08-21 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder 64 was attempting to begin running their 5.5 casing. No violations noted. |
1813726923 | 2013-10-08 | Administrative Inspection | No Violations | Andrew Corder called on well That was going to be plugged back to surface. They ran in with stinger and insert and was setting around 2250 which is the bottom of the 10.75casing. There was a plug across the Clinton formation. They did not set the lime plug and tried to squeeze cement thru the insert. Andrew called and they were going to drill out the insert and spot plug across the lime and set a 200in and 200out across the 10.75casing bottom. |
1826061845 | 2013-07-22 | Drill / Deepen / Reopen | No Violations | On the day of my inspection Sidewinder 64 was drilling ahead for the surface casing. Casing should be set later tonight. No violations noted. |
1964655865 | 2018-09-19 | Production Wells | No Violations | On the day of my inspection I witnessed that the well was equipped with 5.5-inch diameter production casing, and 2.875-inch diameter tubing that appeared to be open flowing with no artificial lift technology. Annular pressure monitoring was in place for the 9.625-inch diameter intermediate casing gauge read 1100 pounds per square inch, and the 13.375-inch diameter casing gauge read 400 pounds per square inch. Production equipment included a Sand Separator, Gas Processing unit and four 400-barrel production fluid tanks, and a 50-barrel produced water tank shared with the other producing wells on the well pad. There were multiple Emergency Shutoff Devices on location, Identification tags were present, and production was up to date. |
2090729341 | 2013-10-07 | Plug / Plug Back | No Violations | Gulfport Energy has decided to plug this well. Well had reached total depth but casing could not be ran. This is a LOST HOLE. |
305600640 | 2013-7-15 0:00: | DD | No Violations | 1.00 |
3702203 | 2013-7-30 0:00: | DD | No Violations | 2.00 |
596325048 | 2013-10-9 0:00: | PB | No Violations | 12.00 |
For data sources see[3]