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34-013-20535

Well Details

Well ID: 34-013-20535
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Country: United States
State: Ohio
County: Belmont
Municipality: Wayne Township
Operator Name: NGO DEVELOPMENT CORP.
Well Pad ID:
Farm/Lease Name: WARFIELD WILLIAM
License Status: Final Restoration
License Date: 2017-08-24
Spud Date: 1988-11-30
Spud Drilling Contractor: G-R CONTRACTING
Final Drill Date: 1988-12-08
Well Total Depth: 2691.00 ft
Configuration: Vertical
Latitude: 39.870000
Longitude: -81.110000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1988-11-22 Issued Date 11/22/88 Expired Date 11/22/89 Acres 0020000 Tool Type RTA Proposed Formation GORDON Proposed Depth 02691 Proposed Drill Depth 02691
Original Spud 1988-11-30 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT
Completed 1988-12-08 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT
Reached Total Depth 1988-12-08 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT
CO 1989-01-14 1815 TRANS ATLANTIC ENER CORP GeoDate 11/22/88
Completion Report Received 1991-06-03 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT
CO 1995-06-27 4381 PELICAN PRODUCING INC GeoDate 11/22/88
CO 1997-03-04 4695 P P & G OIL GeoDate 11/22/88
Change of Owner 2005-10-05 Operator changed from 4695, P P & G OIL to 1634, NORTHWOOD ENERGY CORP
Change of Owner 2013-08-09 Operator changed from 1634, NORTHWOOD ENERGY CORP to 98, NGO DEVELOPMENT CORP.
APP 2017-08-24 Proposed Formations:BEREA, Issued Date:8/24/2017, Expired Date:8/24/2019 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2017-09-19 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT
Record Last Modified 2018-11-01 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT
Construction Permit Expires 2019-08-24 UPDATE COORDINATES PER DOGRM SURVEYOR-ALE 12/13/17. GMM UPDATED PLUG STATUS PER PLUG REPORT

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 2062 2078 0
2062 2078 0
2006-09-11 2073 2078 11
2073 2078 11
2062 2078 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1500 Bbl 2200 FRAC W/1500 BW & 220 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 TRANS ATLANTIC ENER CORP 1968.00 0.00 122
1990 TRANS ATLANTIC ENER CORP 1804.00 35.00 365
1991 TRANS ATLANTIC ENER CORP 822.00 0.00 365
1992 TRANS ATLANTIC ENER CORP 321.00 0.00 365
2005 NORTHWOOD ENERGY CORP 0.00 0.00 0
2006 NORTHWOOD ENERGY CORP 0.00 0.00 0
2007 NORTHWOOD ENERGY CORP 170.00 0.00 365
2008 NORTHWOOD ENERGY CORP 171.00 0.00 365
2009 NORTHWOOD ENERGY CORP 0.00 0.00 0
2010 NORTHWOOD ENERGY CORP 201.00 0.00 365
2011 NORTHWOOD ENERGY CORP 508.00 0.00 0
2012 NORTHWOOD ENERGY CORP 551.00 0.00 366
2013 NGO DEVELOPMENT CORP. 74.00 0.00 365
2014 NGO DEVELOPMENT CORP. 12.00 0.00 365
2015 NGO DEVELOPMENT CORP. 15.00 0.00 365
2016 NGO DEVELOPMENT CORP. 102.00 0.00 365
2017 NGO DEVELOPMENT CORP. 31.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 TRANS ATLANTIC ENER CORP Brine 0 122
1990 TRANS ATLANTIC ENER CORP Brine 0 365
1991 TRANS ATLANTIC ENER CORP Brine 0 365
1992 TRANS ATLANTIC ENER CORP Brine 0 365
2005 NORTHWOOD ENERGY CORP Brine 0 0
2006 NORTHWOOD ENERGY CORP Brine 0 0
2007 NORTHWOOD ENERGY CORP Brine 0 365
2008 NORTHWOOD ENERGY CORP Brine 0 365
2009 NORTHWOOD ENERGY CORP Brine 0 0
2010 NORTHWOOD ENERGY CORP Brine 0 365
2011 NORTHWOOD ENERGY CORP Brine 0
2012 NORTHWOOD ENERGY CORP Brine 0 366
2013 NGO DEVELOPMENT CORP. Brine 0 365
2014 NGO DEVELOPMENT CORP. Brine 0 365
2015 NGO DEVELOPMENT CORP. Brine 0 365
2016 NGO DEVELOPMENT CORP. Brine 0 365
2017 NGO DEVELOPMENT CORP. Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1103251669 2014-4-24 0:00: PW No Violations 2.00
-1138005359 2005-5-9 0:00:0 PW No Violations
-1229219627 2018-3-15 0:00: FR No Violations 0.50
-1277645639 2015-6-18 0:00: PW No Violations
-1566628653 2017-9-18 0:00: PB No Violations 5.70
-2032732820 2016-1-14 0:00: PW No Violations 1.00
-2097663844 2017-9-20 0:00: PB No Violations 2.00
-243350863 2015-7-9 0:00:0 PW No Violations 0.50
-400439903 2015-7-1 0:00:0 AM No Violations 0.50
-422638824 2017-9-19 0:00: PB No Violations 5.00
-74781749 2013-4-3 0:00:0 PW No Violations 5.00
0074781749 2013-04-03 Production Wells Violations Noted On the day of my inspection the well was shut in. Landowner claims that the meter has not moved in a year and has pictures to prove this. Previous inspector noted that well was idle from 1992-2005. Compliance Action was issued and resolved stating that landowner was using it for natural gas. I spoke with the landowner and the well has never been hooked up for domestic gas I did not see a domestic line coming from the well. (well has been shut in) Owner is receiving gas from other wells on property. WELL SHALL BE PLUGGED WITHIN 30 DAYS of mail out date of CA. 04/19/2013. UPDATE: Well production records have been submitted. RESOLVED.
0243350863 2015-07-09 Production Wells No Violations I spoke with Scott Kees regarding metering changes being made to this well. He informed me that he was installing a digital meter system with a smaller orifice to alleviate the concern of adequate well production.
0329969264 2015-06-25 Production Wells Violations Noted
0400439903 2015-07-01 Administrative Inspection No Violations I received a call from Scott Kees. He informed me that the well has been remediated. I will check and confirm the well status in the near future. He also stated that the well had been shut in and he did not know who had done that. Per our conversation, the well had went from a pressure of 25lbs to 60lbs over night. He was also concerned about the metering systems and believes that the metering may not be representative of the amount of gas actually produced by the well. He will speak with upper management about putting an electronic metering system on the well to obtain a more accurate reading.
0422638824 2017-09-19 Plug / Plug Back No Violations

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0837930334 2015-10-19 Production Wells No Violations I attempted to contact Omar with NGO to discuss the metering system and the values shown on the metering system. Later this day, I received a follow up call from Rob who looks after this well for NGO and is familiar with the metering system in place. Rob informed me that the number present on the meter represented MCF in value. This would make the 43 denoted on the meter have a value of 43 MCF.
1038335799 2017-06-19 Production Wells No Violations I spoke to the landowner on this day and he informed me that he had reached an agreement with the owner of the well and the well shall be plugged in the near future. The company had removed all the electronic metering devices that were previously installed at the metering site. All other equipment remained the same as in the previous inspection.
1085490020 2004-05-24 Production Wells No Violations WARFIELD WELL HAS BEEN RESOLVED OPERATOR HAS MADE DOMESTIC GAS AVAILABLE TO LANDOWNER.
1103251669 2014-04-24 Production Wells No Violations On the day of my inspection the valve on the well was in the off position. Previous compliance notice has been resolved. Production records have been submitted. I spoke with Mr. Warfield and he advised that this well is currently under litigation. No violations noted.
1138005359 2005-05-09 Production Wells No Violations NON-PRODUCING SINCE 1992.
1229219627 2018-03-15 Final Restoration No Violations Accompanied Belmont County Inspector Andrew Corder, Reference his Report for further details
1238559090 2016-04-21 Production Wells No Violations On this day I was accompanied by Brent Bear. This inspection was as a result of an email forwarded to me by John Flemming that the landowner Dan Warfield had sent him. The landowner is concerned with the production records of this well. The well was equipped properly to be considered capable of production. The pressure on the well head was approximately 25 lbs. This well is still being metered electronically.
1272939721 2004-03-25 Production Wells Violations Noted WELL APPEARS TO HAVE BEEN IDLE FOR SOME TIME.
1277645639 2015-06-18 Production Wells No Violations This inspection is in response to complaint # 5055. Dan Warfield sent a letter to the Chief with allegations of false production reporting from the past companies. I received a request to inspect the site accompanied by Eric Vendel and John Flemming. I emailed those parties in regards to setting up a time to inspect the well.
1345488421 2018-08-02 Final Restoration No Violations On the day of my inspection I witnessed that the well and equipment had been removed. There was a 2-inch diameter gas line that appeared to be providing domestic gas near the well location. The gauge on the 2-inch diameter flow line read 60 pounds per square inch. I spoke with the land owner Dan Warfield and he informed me that the 2-inch diameter line belonged to Northwood Energy and was once tied into his wells across the road. From what I witnessed the Final Restoration met the requirements of the Ohio Revised Code 1509.072.
1367892215 2016-01-13 Production Wells No Violations On this day I inspected the well to follow up on the existing complaint. The well was equipped to be capable of production and the metering system is in place. No environmental threats were evident.
1436883638 2015-07-14 Production Wells No Violations On the day of my inspection well casing had been remediated. The existing compliance notice is now resolved. The metering system had been moved from the well head to the sales line area. An electronic metering system has been installed. The meter on this day did not appear to be working. Photos were taken on this day.
1437991638 2015-07-24 Production Wells No Violations On this day The well was equipped to be considered capable of production. The electronic metering system was in place however, the meter did not present any numbers for me to record. Photos were taken on the day of this status check.
1438712345 2015-06-25 Administrative Inspection No Violations
1445366590 2015-10-16 Production Wells No Violations This inspection is in response to a complaint #5055. ODNR Oil and Gas Inspector Andrew Corder and myself and Mr. Warfield were on location to perform a status check. The well is an open flow with a .250 orifice plate on a 2 meter run equipped with an Eagle Research Metering system. There is also the same type of meter on the sale line with the same orifice plate size. (.250). At this time the well is capable of selling gas. All valves are open. The well pressure is 25 psi and the sales line is 25 psi.
1505752619 2017-09-14 Production Wells No Violations I received a call from Bill Mitton who informed me that they would be mobilizing the service rig to this location and plugging efforts would being on Monday 09/18/2017. I Bill told me he would also notify Inspector Pat Shreve of this plugging operation.
1566628653 2017-09-18 Plug / Plug Back No Violations

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1628988854 2015-06-30 Administrative Inspection No Violations I received a call from Scott Kees requesting directions to the well. I supplied him with directions and told him to contact me when the company reached a determination on how to remediate this well.
1673771434 2018-03-16 Final Restoration No Violations An inspection conducted of this site confirms that the company has completed the final restoration of the affected area and the site has vegetation established. The company has fulfilled their duty under the Ohio Revised Code and the final restoration is now passed.
1933871537 2015-06-26 Production Wells No Violations On this day at 11:28 am I contacted Scott Kees who is a representative of NGO. I notified him that there was a leak on the well casing just below ground level and gas was escaping into the atmosphere. I notified him that a compliance notice will be issued and the company shall comply within 14 days.
2032732820 2016-01-14 Production Wells No Violations A phone conference was held with Central Office concerning the complaint on this well. It was determined that the well is capable of production and is currently producing. No violations currently exist at the well head. This well will continue to be monitored. Annual production report for the well will be reviewed.
2047128049 2015-10-16 Production Wells No Violations On this day I visited the well for a follow-up inspection accompanied by Inspector John Fleming. The landowner, Mr. Warfield, was also present. During my inspection the well appeared to have proper equipment to be considered capable of production. The electronic metering system showed a value of 43. It is undetermined at this time what volume amount this number represents. I will contact the company regarding this reading to determine the volume that the number present represents. John took pictures and Mr. Warfield was informed that I would contact the company concerning this matter.
2097663844 2017-09-20 Plug / Plug Back No Violations The well head was dug up 30-inches below ground level and the identification plate was welded onto the casing. The operator then put the location back to grade.
2134827605 2015-06-23 Production Wells No Violations I contacted the landowner Dan Warfield to schedule a time when he could meet me and other division representatives to evaluate the well and the allegations. The meeting will be held on 06/25/2015 at 10:00am.
329969264 2015-6-25 0:00: PW No Violations 3.00
837930334 2015-10-19 0:00 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0074781749 US-OH-128498 2014-05-12 Nonproduction; well shall be plugged or placed in temporary inactive status
0329969264 US-OH-123445 2015-11-10 Well insufficiently equipped to prevent escape of oil and gas
1272939721 US-OH-107589 2004-03-25 Well shall be plugged

For data sources see[9]

References